Thursday, March 03, 2016

Junk Plant Seabroook Had Problems Controlling Steam Generator Level




Power ReactorEvent Number: 51765
Facility: SEABROOK
Region: 1 State: NH
Unit: [1] [ ] [ ]
RX Type: [1] W-4-LP
NRC Notified By: MIKE TAYLOR
HQ OPS Officer: STEVEN VITTO
Notification Date: 03/02/2016
Notification Time: 18:13 [ET]
Event Date: 03/02/2016
Event Time: 13:12 [EST]
Last Update Date: 03/02/2016
Emergency Class: NON EMERGENCY
10 CFR Section:
50.72(b)(3)(iv)(A) - VALID SPECIF SYS ACTUATION
Person (Organization):
WILLIAM COOK (R1DO)

UnitSCRAM CodeRX CRITInitial PWRInitial RX ModeCurrent PWRCurrent RX Mode
1NN0Hot Standby0Hot Standby
Event Text
VALID ACTUATION OF EMERGENCY FEEDWATER

"On 3/2/2016, [at] 1312 hours EST, while in the process of a plant cooldown, a valid actuation of the emergency feedwater system (EFW) occurred when B steam generator levels were reduced to 20 [percent]. The lowering level was a result of the unanticipated tripping of the start up feed pump on low condensate storage level while it was the feed source to the steam generators. The start up feed pump was restarted and feed flow had been restored when the actuation took place. The EFW flow was secured per procedure and the start up feed pump remains the feed source to the steam generators.

"This is reportable under 50.72(b)(3)(iv)(A).

"The licensee notified the NRC Resident Inspector."

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