Saturday, June 02, 2012

Iran's Response to Israel and the USA


Just for full disclosure...I got buddies in the FBI?
Translation:
 
You two ain't shit. You know I've already taken out a USA nuclear powered sub in Maine and its reactor. Think of what we will do to you if you militarily take our illegal nuclear weapons production sites? We will proportionally decimate Israel and the USA?

Iran vows 'proportionate' response to any strike on nuclear sites


Agence France-Presse Jun 3, 2012
TEHRAN // Iran will respond to any Israeli or US attack against its nuclear sites with a "proportionate" reaction, the military adviser to the country's supreme leader Ali Khamenei said on Saturday.
General Yahya Rahim Safavi, quoted by Fars news agency, said however that such an attack was unlikely.
Despite warnings from Washington and Israel that "all options are on the table" if negotiations between Iran and major powers on Tehran's controversial nuclear programme fail, conditions do not favour an assault, he said.
"They may be able start one but they can not end it and it remains in Iran's hands," the general said.
"The domestic political, economic and social conditions in America and the Zionist regime are not such as to have a new war in the region," he said.
US President Barack "Obama wants to get re-elected (in November) ... the cabinet of Mr (Israeli prime minister Benjamin) Netanyahu is a fragile one," he said.
However, in case of an attack, "we will act against their military operation smartly, proportional to any damage that they inflict on us ... meaning we will hurt them as much as they hurt us."

New: Asymmetric warfare

Scenario: They are politically and war gaming this right now in the pentagon.

Al Qaeda might be grasping to make a last statement. Iran or Syria might be fearing eminent attack by the USA. With our cyber warfare viruses attacking the middle East and Iran, we have admitted we have committed an act of war against Iran. The USA says it's a act of war if somebody does cyber terrorism act against us.

What if Iran preemptive or reactively demonstrates a show of force by secretly hitting a high profile American military target? By its demonstration you will understand our reach if you go to a proportional limited war against us. Do you really want to start a war with us when you are so economically weak and we can hit so many of your high profile targets to the world's media delights?

The evidence points to it and there are some wild rumors out there. Did Iran or Syria, or them both and with unknown parties conspire and commit a direct act of war by sabotaging a high profile United States nuclear attack submarine sitting naked and unprotected in a naval shipyard? Did Iran fire bomb the USS Miami SSN 755? What will the next one look like?

How would we know if this was a United State's false flag operation, to provoke us into attacking Iran and others?

Do you trust the Navy department to investigate this on their own? Remember the battleship the USS Ohio during the Reagan administration? Would they want to hide their own flaws and give us a partial investigation.

What Institution would you trust to tell us the truth and what level of truth and transparency is a necessity for a democracy?

Would the Navy department bury a terrorist attack or a act of war against us in anticipation of a upcoming presidential election? Would the administration provoke an attack to throw an election or take our minds off a upcoming depression? Is the new stimulus to save us from a depression, a war with Iran? Would the Department of the Defense and their related corporate interest start a war in order to mitigate the upcoming massive defense cuts?

I could make a case a new greater middle east is worth a lot of blood and guts. It has been the dream for 50 years of the greater world to modernize them. We are half way there? My philosophy is you don't provoke a wild and wounded rabid dog to attack you, so you can feel good about putting the dog down out of its misery.

What if the conflagration in the sub USS Miami was stupid accident and Iran is using the disaster to stick out its chest to the world and bag to its population how strong they are?

What if you are on the scene and the big story is different than what you know?

Who do you serve? Who do your trust? What do you believe?

Have you ever been so alone!







Friday, May 25, 2012

Al Queda attack on USS Miami submarine notes


Snowe, Collins: Navy will rebuild fire-damaged sub

KITTERY, Maine
(NEWS CENTER) -- The U.S. Navy is determined to rebuild the submarine damaged by fire at the Portsmouth Naval Shipyard. That word came from both of Maine's U.S. Senators after visiting the shipyard Friday. They also had high praise for all the firefighters and the sub's crew members who battled the fire for more than 12 hours.

The Senators say that shipyard workers are still ventilating the remaining smoke and fumes from inside the submarine and pumping out the three million gallons of water used to fight the fire.

The Navy is starting its investigation to determine how the fire started.

The flames broke out Wednesday night in what's called the forward compartment of the Miami, and officials report significant damage to that part of the sub. Senator Snowe and Collins say the Navy will investigate the cause, the extent of the damage and whether there was any criminal activity involved.

Sen. Snowe says there is no reason to suspect any wrongdoing, but regulations require that to be included in the investigation.

The Senators the submarine will be repaired and sent back to sea, and that the work will be done at the Kittery yard. They say Congress will have to find the money to make the repairs.

Snowe says it is believed to be the most serious fire ever at the shipyard, and possibly the worst on a Navy nuclear sub.

...Is she sick or what? If the fire was the shipyard fault, they get double bonus,  and get to benefit for their negligence.

Maine Congresswoman Chellie Pingree:

Pingree said Capt. Bryant Fuller told her the fire came at a good time because the USS Miami had been at the yard for three months, and so workers had already removed a lot of equipment from the damaged area. "It's in their favor that it had been emptied out."

...Ultimately, he is accountable for this fire, he is defending his bad behavior. The fire was good for us because we get a double bonus.

Capt. Bryant Fuller

The USS Miami's reactor was not operating at any time the fire broke out and remained unaffected and stable throughout, said Capt. Bryant Fuller, commander for the shipyard, which is in Kittery, Maine.

...pumped a million gallons out of the submarine, that is about 8 million pounds inside the hull. They are dam lucky the sub never collapsed into the dry dock. And the sub was up on blocks. Certainly the sub was never designed for that weight and that is probably the reason why the sub will never see the sea again.

..."Oops"

"All told, the firefighters rotated 75 times to battle the fire, using 3 million gallons of water, nearly filling some compartments, Snowe said."

Aluminum, cabling and insulation caught on fire?
24 million pounds
1200 tons
300 semis...

...where do they keep the diesel generator fuel oil in a sub for the diesel generator...did that contribute to the fire?

...Ultimately it questions if the fleet of nuclear submarines are fit for combat and fire casualties...unfit for human habitation out to sea.


Miami fire probe will take at least 3 weeks
By
Christopher P. Cavas - Staff writer
Posted : Friday Jun 1, 2012 11:40:24 EDT


Investigators are continuing their work to determine the cause of the fire that burned through the fore end of the nuclear submarine Miami over the night of May 23-24.

The conflagration, which struck while the sub was in drydock at Portsmouth Naval Shipyard in Kittery, Maine, burned for nearly 10 hours but, according to the Navy, did not endanger the vessel’s nuclear reactor.

Shipyard workers returned to work on the ship Tuesday, shipyard spokesperson Deb White said.

The effort to fix the cause and assess the damage to Miami is expected to take about three weeks, White said in a news release issued Wednesday.

Several Navy investigations already are underway, said Naval Sea Systems Command spokesman Chris Johnson, including a safety review, a Judge Advocate General investigation and a NAVSEA technical review of the submarine’s condition — standard probes for this kind of incident.

The 22-year-old Miami was about two months into a scheduled 18-month engineering overhaul at the shipyard. The ship, planned for a service life of about 30 years, is scheduled to be decommissioned in fiscal 2020.

Navy authorities so far are declining to speculate about possible causes of the fire or whether the submarine can be repaired.

“Once all the inspections and reviews are complete, the Navy will take the time to look at every possible scenario in regards to the ship’s future,” Johnson said Thursday.

Unofficial reports indicate the fire burned at very high temperatures inside the ship.

Temperature “readings on the hull during the fire were very high,” said one source with knowledge of the incident. “It was indicative of an incredible fire on the inside.”

Although NAVSEA chief Vice Adm. Kevin McCoy proclaimed shortly after the fire that the submarine would be repaired, speculation has been widespread that Miami’s service life is over. The intense fire could have buckled hull frames or weakened the pressure hull, and the cost of repairs could be prohibitive.

If the ship can’t be returned to service, she might be useful as a moored training ship for the Navy’s nuclear power school at Charleston, S.C., where the former ballistic missile submarines Daniel Webster and Sam Rayburn are slated for replacement. Two Los Angeles-class submarines, La Jolla and San Francisco, are scheduled to be converted to the MTS role when they’re decommissioned in 2015. Miami, with her reactor and machinery sections intact, might be swapped for one of those.

If the submarine cannot be returned to active service, it would become the first submarine and the first nuclear ship lost through a U.S. shipyard accident. And while two ships — the transport Lafayette (the former French liner Normandie) in 1942, and the minesweeper Avenge in 1970 — have been lost in commercial shipyard fires, Miami could become the first ship lost in a U.S. naval shipyard since the 19th century.












Friday, May 18, 2012

A Failure Of Imagination, again?

This isn't a failure of a technology, maybe a failure to keep modern a technology. I think the Japanese nuclear disaster for us in groups, organization and as a culture, as individuals and collectively, it is a failure of us to manage our brains, thinking and our hearts. Oh, the sorrows over all our failures to manage our hearts...

A failure of imagination?
Is there a exercise plan in which you can make your imagination muscle stronger? Can you productively strengthen the individual and group imagination muscle. I believe there is such a muscle in out heads.
How many times we going to hear heart sick people, who were involved in trillions of dollars and damaging thousands of people lives, lamenting it was a failure of my imagination after the tragedy. Why does organization culture kill imagination? And I will tell you a fact, imagination ain't shit unless you get it recorded on the organization's paperwork. The ability to create a organization wider discussion on it.
Do we get the choice, in order to fit into the group I am required to cripple my imagination. Or I can have infinite conscience imagination if I leave the group. Is it choice of starving or not?
And we know we are forced to be in groups where our thinking is forced to be stove piped into artificial ideological, culture or organizational bins. This is what we tell everyone what we know and this is what we say we don't know, when we do?
You know, like, who and what do you serve?
And a little altruism can overshadow a much larger altruism...altruisms abuse or altruism blindness. To what ends do to we use altruism for, to open up our eyes to the spectacularly beautiful wider world or to limit ours or our organizational field of view for selfish purpose?
Our greatest failures and sins occur over altruism blindness...our inability to discriminate altruism for self interest over altruism for our common good. Does doing good for another make me feel good or does it set another free? Does it make me feel good, when i should feel very troubled and compelled to act.
Isn't that at that at the bottom of the failures of the philosophy of our free and completive economic markets...?
Kyodo
The man who was the Ministry of Economy, Trade and Industry's top official when the Fukushima disaster unfolded said he regretted underestimating the tsunami danger when METI was reviewing earthquake-resistance guidelines for nuclear plants before the crisis.
"We should have used our imagination," said Kazuo Matsunaga, who was vice minister of economy, trade and industry when the meltdowns began in March last year, told a Diet-appointed panel probing the disaster Wednesday.
I consider this an intentional distraction that allowed him to drive intoxicated?
..."My mind was occupied with handling the accident at Kansai Electric Power Co.'s Mihama plant," Matsunaga said, referring to a pipe rupture in August 2004 that killed five workers and injured six.

Wednesday, May 16, 2012

Does NRC's Director Troy Pruett Work in Region II?

Is the NRC's III Division Director Troy Pruett political disease in Region II?

I bet you if they had shut down Browns Ferry their could have concentrated their resources a lot more effectively. It would have made their job as a regulator a lot more easy?

Sounds like Swafford is saying, bug off NRC or I will sic my mad dog southern Republicans and the gang of four pro industry commissioners at you.

Browns Ferry isn't ready to inspect

excerpts:

TVA's nuclear operations chief told officials with the Nuclear Regulatory Agency on Tuesday that Browns Ferry is not ready yet for a third and final special NRC inspection to clear its "red" safety rating.

"We will not invite an inspection team in until have confidence we are ready. ... I can't even give you a ballpark estimate now when that will be."

NRC's regional administrator, Victor McCree, said after the meeting that the federal regulatory agency will take that answer in stride.

"I've been at the mindset that there's no point stressing accountability for procedures we know will change. Holding people accountable to inferior products isn't fair to the employees," Swafford said.

Thursday, May 10, 2012

If I Won The NRC's $700 Million Dollar Reform Lottery

You know he is downplaying it...it is huge. And it's a spreading cancer on the nukes.

Exelon's CEO Mayo Shattuck:

"Even the existing fleet is feeling a little bit of the pressure in this kind of environment,” he said. The U.S. has 104 commercial operating reactors."

?
I would get the Allegation department outside the NRC...make them a stand alone entity.

 
US Senator Bernie Sanders and Vermont Attorney General William Sorrell to speak at rally to support Vermont.

April 6, 2012
Saturday, April 14, 2012, Noon to 2:00 pm
Brattleboro Common, Brattleboro, Vermont 05301
(rain location: Brattleboro Union High School)
statements issued day-of from
Governor Peter Shumlin and
Former Governor Madeline Kunin
and other elected officials
Special Musical Guest:
Fenibo (a rousing 12-piece Afro-beat ensemble
1) April 2, 2012

...I have spent an enormous of time talking to NRC officials and local NRC plant inspectors over the last year at VY, Palisades and Peach Bottom nuclear plant. I've submitted many 2.206s. A lot of NRC officials know my name and have spoken with me over the phone and in person.

If you really wanted to help me and the nation...you would help me reform the NRC's 2.206 petition process.

The below is in a condensed from...it designed to protect careers. It is in a nuclear industry technical lingo-speak that the NRC understands. They know these people are Root Cause Analysis professionals and have broad vision over many plants.

I am absolutely certain we have understated the problem. I am certain if this was investigated and mandatory testimony...we could prevent a lot of trouble.

Remember, I think they think doing a RCA gives factual ammunition to the NRC and in pending regulatory or court proceedings.

My blog: 'The Popperville Town Hall'


http://steamshovel2002.blogspot.com/

What we are talking about here in broad terms: it is the immune system of every nuclear plant in the nation and the nuclear industry.

...Of course, taking out the NRC Allegations section and the 2.206 petition process, that is call being in heaven.

I would want the NRC to be in partnership with me, not as a hyper rules based prosecutor or judge where I have no chance of ever getting past this corporate sponsored rules mandated to the NRC. I got to go up against this highly legalistic system even when it not really designed to be that way, where it is mostly laissez-faire and voluntary rules to a nuclear power plant. It is a check valve regulator!

They got a tons of laws and tools that limits my transparency to the problems of a plant and the agency; with very limited rules that mandates transparency to the public or me.

It is like a one way check valve on a host of issues, very little is spun my way in the interest of the USA (public), the vast majority are spun in the industry direction.

The overriding issue here is transparency and truth telling...the single most important determinate to nuclear and public safety is the nuclear industry showing their cards.

These guys got a lot of incentives to take shortcuts!

I won't bug you any more unless you ask for advice.

...Honest to god last time:

When I go through these NRC government processes...the 2.206 and Allegations...I feel it as the government is in a word, language, rules and process war with me. My government is at war against me and is using language as a weapon of war to me. It is not as a tool of understanding the issue or me. They become a understanding disruptor weapon.

A nuclear plant is so engineering, technically and organizationally complex...interacting with the NRC is 1000 times more complex.

I really need a seasoned senior NRC official who has seen everything and he has the horsepower to know the system and demand transparency. He needs to be assigned to me like my advocator and lawyer...his job is temporarily serve me and my issue ...to guide me through the agency's complex processes. All us outsiders need this kind of help.

I met and talked to a lot of NRC officials. Most of them are kind and decent when you get them by themselves. Most of them make us proud.

2) April 4, 2012

To who it may concern:

I can't believe I am doing this after having such a painful outcome talking to NRC Region 1 Allegation officials just a few days ago. I told myself I would never talk to Allegations again. If you want to talk to me I suggest it be outside Region I Allegations and preferably somebody from headquarters. I know there are lots more experienced people in the NRC than what I was recently exposed too.

I consider Region 1 Allegations compromised much like the March 2007 Peach Bottom sleeping guard incident where Allegations needed 500% absolute perfect inside evidence that was never obtainable in our existence. The NRC was too lazy to go down to Peach Bottom to investigate it on their own and they took the false assurances of Peach Bottom that there was no sleeping guards until the inside video came out that shook up the nation.


I consider the below a "cry for help" to me from multiple plant high nuclear employees and nuclear safety officials. And I certainly assert my confidentiality rights with this because this is so explosive to many careers. Nuclear Industry safety consultants might become blacklist from the nuclear industry. It exemplifies a pervasive of "I don't care" nuclear safety attitude throughout the nuclear industry. And these utilities are disrespectful to nuclear safety oversight in general.

I bet we are painting the most accurate leading indicator the NRC has seen in decades and we know the industry is in deep troubles as seen with all of your issues in recent years. These guys got a attitude problem and so doesn't the NRC!

I wish you would send a copy of this to the OIG?

 
...So is this about the reforming NRC Allegation process or RCA?

 Just kidding, or not.

 I kinda open here with my time. I could converse with you with within 24 hours, say tomorrow morning or beyond. I am good with before the end of the week, but I understand you people are busier than me.

What the hell does "specific information" mean?

 
...3:00pm on 4/10 is a excellent choice.

 By the way, what are my needs that enables the exercises of my democratic Constitutional ideals or rights with the agency's rules.

1) Full access to the target site, documents and employees of a nuclear power plant or NRC.

2) My sufficient funding, skills and education to do my own independent investigation to give the agency its rule enabler.

"Specific information (e.g., which site/plant, organization, personnel) is necessary, for the NRC to respond to any issues, which are raised by concerned citizens."

...Really, I am a ant...you would need a sufficient independent "organization" with sufficient uncontested access, resources and intellectual horsepower, which could counteract or challenge the Republican ideological influences over of the agency and the influences of the cohesive nuclear industry and their owners.

It should neither be pro nuke or anti nuke...just hunting for the truth!

You would need a transformational organization...

Wednesday, April 11, 2012

American Tissue Corp

American Tissue Corporation
I would gladly talk to people about my activities concerning American Tissue corp to any legitimate people. It is a fascinating story. I bankrupted the 4th largest paper mill company in the USA and this lead to putting executives in jail.

It was a fascinating learning experience for me. It was a $300 to $400 million dollar fraud case. It was a warning to us about the upcoming financial crisis we ignored.

Wednesday, March 28, 2012

Pilgrim's failed Target Rock SRV

New April 5, 2:30pm
The OIG gave me a call today.

...He humiliated and disrespected me with this phrase " if your were a decent whistleblower" you would have a complete report.

You know what I say, record and transcript every conversation I have with NRC official. If you were with me on my conversation you would see how disgraceful and uneducated some officials are.

Mostly the front line NRC inspectors and their bosses are really decent people...but the support people like Allegation and the OIG are atrocious and with their knowledge of the nuclear industry. They generally don't have the skills and are not trained to talk in a non threatening manner and have a open discussion.

This guy began exactly like the Allegation...what was the LER nmber?
  
...So were talking about target rock and why components immediately failed on new installs.

This guys didn't know what a safety relief valve did in a BRW. I had to educate him on its function.

You know what, these are really complicated components and organizational issues. You just can't come into a conversation with me without deeply researching my issues or I have to give you grammar school class in BWR designs. Both Allegation and the OIG did this.

If you don't do your background work before you get to me...i am going to lose you within the first five minutes.

The NRC OIG guy said its not fraud waste, misconduct or abuse within the rules of the OIG...so it a licensing or NRR thing. I said believe me i got it with your NRC people, you are going to pass me from one department to another because some NRC employees are too lazy to do their jobs. I am going to have to explain myself 100 times to different departments and NRC employees, who don't even know what the function of a SRV is. 
...The NRC is doing one of those teenager la la la la deals while covering their ears to the obvious.

Basically, I asserted LER's are insanely incomplete and inaccurate...

...I would say i was exposed to a militaristic use of language to disrupt communications....the use of rules and regulations in way to disrupt communication and knowledge of the problem to the
public. It is using words, language, rules and regulations, indeed government as weapons against the innocence...the intent is deny public participation with government. They militaristically trying to rule me and everyone out of public participation.

I think what we got here is systemic breakdown with the utilities and NRC to control vender repair, new parts and basic off site engineering services. I think these vendor component and engineering suppliers are not required to tell the truth. I would say since I been hitting them on these issues the NRC has tried to come to grips with their vender service provider problem.

Bottom line, they are having trouble getting replacement parts on these obsolete plants. Companies have gone out of business and ceased production streams, and the new deal is they are hiring companies who specialize in doing "reverse engineering" on replacement parts that are dangling without any new parts stream.

...As example, all the new Mitsubishi kids are making the San Onophe SGs and the old experienced engineers have retired or died.  


New March 28
I backed out of the NRC allegation process. They got hyper legalistic and evidence thingy on me...they knowing that the agency and the utility had all the cards. I said the Peach Bottom 2.206 administrator sent my issue into allegation...I didn't call in allegation on my own. I thought it was going to be a conversation between me and agency...not this one way deal where if i said i sneezed then I had to prove I sneeze. I asked, should I have brought my lawyers and engineers into the deal.

I didn't think the Allegations process was fair and opened...it was hyper legalistic and hyper regulatory rules thingy where you couldn't sneeze if it wasn't in the rules. The Alligation team went cold into this not even researching my involvement with VY and Peach Bottom, and the LERs and inspection reports.   

I said I withdrawal my concern and I don't want to be updated about this. They told me you can't withdrawal a concern once one was given to the NRC....but you can be anonymous.

  ...At the bottom of it over VY and the Peach Bottom SRV issue, I spent days researching everything i could about the SRVs. I spent a hour and half each with both inspectors at VY and Peach Bottom for a total of four plant inspectors and three hours talking to me. I knew the territory and what I was talking about...I was frustrated that these four officials went cold into this meeting. Then they played the, mike this thing is evidence driven and we got to know the LER number and we got to know who the VY inspector's names are. It was humiliating and disrespectful for me. There was one official talking to me as I was discussing my issue, then none of the other three officials could even do quick search on the VY docket for the LER document number to get us past the sticking point. What BS!

I got a e-mail trail from Don, lets schedule a meeting beginning last thurs. I say I ready right now, tomorrow and any time at your convenience next week. Just set the time and date and i will be there. I wanted to make it easy for him. Then I get a e-mail tues saying I can't find anyone to have a meeting with you without any explanation. Next day he tells me the following day the meeting is on, what time.

They don't even have the courtesy on their own to read my 2.206s and transcripts surrounding the VY and Peach Bottom seals. These Allegation idiots have in their documents I make a recent allegation by phone about VY seals again and they are the ones who made the VY inspectors call me without going though the Allegation process.

That is another more specfic information not disclosed in the VY LERs or inspection reports...the 400 degree vitol seals.


We should go through the VY seal LER and update, then contrast what got in the NRC inspector report and then what came out in the NRC inspectors meeting with me. We should then discuss what should have been disclosed in LERs and further inspection reports. As far as i am concerned, the inspectors at both plants should be on the phone bridge. We should go over it point by point and not have any other commitment to rush anyone, until everything is completely hashed out. We should do the same thing with the Peach Bottom LER.

Again, we don't have public participation with the NRC and utilities around our homes, unless all the aspects of the problem is out in the public arena.





March27 

Mr. Mulligan:
I have been unable to contact the appropriate NRC technical staff, for a telephone call with you. I will contact you when I know more.
Sorry for the late information.
v/r,
Ron Schmitt
USNRC

New




From: "Schmitt, Ronald"
To: "Michael Mulligan (steamshovel2002@yahoo.com)"
Cc: "James, Lois"
Sent: Thursday, March 22, 2012 8:33 AM
Subject: Time to discuss your concerns (RE: Quality Assurance program at Target Rock)
  

Dear Mr. Mulligan:
This email is in regards to your email that you sent to Mr. John Hughey, of the U.S. Nuclear Regulatory Commission (NRC) on March 17, 2012. In your email, you expressed concerns regarding the Quality Assurance program at Target Rock, as a result of failed safety relief valves at Vermont Yankee, Pilgrim and Peach Bottom nuclear power plants.
We would like to set up a call with you so that our staff can ask additional questions to better understand your concern.

Please respond to this email with some days and times that are convenient for you so that I can schedule the call.
Thank you for informing us of your concern. If you have any questions, please contact me or Ms. Lois James at .
 
Ronald V. Schmitt
Office Allegation Coordinator
Office of Nuclear Reactor Regulation
U.S. Nuclear Regulatory Commission

Pilgrim's failed Target Rock SRV
Licensee Event Report 2011-007-00: Safety Relief Valve leakage

So you get it, with the SRV threaded seals at VY and Peach Bottom they failed within the first cycle from degradation due to poor quality seals. Now at Pilgrim another SRV fails with months due to leakage and they blame poor pilot valve workmanship at Target Rock.

Sounds like systemic QA problems with Target Rock. I request a investigation of Target Rock and all similar safety valves.


I talked to your nice Peach Bottom inspectors over increasing the SRV's set inaccuracy from plus or minus 1% to plus or minus 3%. Does the NRC have any evidence that decreasing the margin of set point accuracy reduces the entry into applicable tech spec LCO. I see all the utilities have different guesses on what cause pilot valve bonding. Some say its oxygen or hydrogen that sets up bonding on the surfaces, others say its just bonding and they don't care. Others again say its outside insulation and temperatures that sets it up.

As far as the statement that increasing the relief valve testing set point inaccuracy will reduce entry into a LCO, I don't think that is true. The limited data I see indicates when you increase testing set point inaccuracy, you increase entry into a LCO in the long run.


PILGRIM NUCLEAR POWER STATION - NRC INTEGRATED INSPECTION


October 1, 2011 through December 31 , 2011

 The inspectors selected the issues of safety relief valve (SRV) and automatic depressurization system (ADS) valve leakage and setpoint test failures as an inspection sample for in-depth review to assess the corrective actions taken by Entergy to address these long-standing issues. Entergy's corrective actions included replacing the four ADS valves and the two safety relief valves with a Target Rock three-stage relief valve design, increasing the capacity of the two safety relief valves, and amending the license to allow for a set-point pressure band of +/- 3%. Additionally, the new valves were equipped with multiple leak detection temperature indicators.

The inspectors reviewed procedures, condition reports, engineering evaluations, modification packages, post maintenance testing, and license amendment correspondence, and interviewed plant personnel to assess Entergy's problem identification, evaluation, and corrective action effectiveness with respect to SRV and ADS valve leakage and set-point drift. Additionally, the inspectors reviewed the technical specifications and UFSAR to assess the change to the relief valves with respect to design and licensing bases requirements. Documents reviewed are listed in the attachment. Findinqs and Observations

Findinqs and Observations
No findings were identified.

The ADS valves and SRVs were originally a two-stage Target Rock-type design, consisting of a pilot-stage assembly and a main-stage assembly. Industry Operating Experience had shown that two-stage Target Rock relief valves exhibited some amount of pilot-stage leakage during plant operation. Additionally, the technical specification allowed valve setpoint pressure band was +/- 1%, which left little margin to maintain the valves operable in the event of valve leakage. As a result, SRV and ADS valve pilot stage leakage were challenges throughout the plant's operating history and caused several forced shutdowns.

The inspectors noted, based on nuclear industry operating experience, that the replacement of all the ADS and SRVs with the three-stage Target Rock design was a significant positive step in reducing the likelihood of relief valve seat leakage.

Additionally, the inspectors noted Entergy's evaluation of an expanded relief valve setpoint pressure band and subsequent license amendment have resulted in significantly more operating margin for the plant in the event that a valve does exhibit signs of leakage. Finally, the inspectors determined the addition of several temperature monitoring points on the valve would allow Entergy to more effectively evaluate the operability of the valve should any leakage occur.

Monday, March 26, 2012

Mike Mulligan's US Government Renaissance

First published as comments in the NYT's in: The Nurture of Nuclear Power

I always thought the problem with nuclear power was ideology not technology. The dominant control ideology of the industry has been increasingly the hard right wing conservatives and this ideology is dominant at every plant. There are very few democrats at any of these plants and certainly even less as you go up the management ranks.

The model has defaulted into a autocratic and a decentralized form...every plant is a one off. We serve profits and self interest, and not the greater good of our nation.

The true benefits of nuclear industry has never been shown. I propose a government take-over of the 25 Fukushima plants in the USA. As a national security issue, we should replace those plants with brand new identical models. Lets begin another grand experiment. They would be large plants and centrally controlled in the initial construction and early operation phase. Imagine the efficiency if these plants were built to one set of codes from both the regulator and the designer/builder stand point. It should be a government controlled and modeled like the TVA project.

What if we woke up one day and we discovered government could be more efficient and 'just' than any corporation...or at least could complete with them.

President Obama could say these plants are a dire threat to the USA and the only way out is to replace them. We just about got negative interest rates with QE2 and why couldn't we come up with a revolutionary borrowing mechanism. It would be a giant jobs and public works project. It would split the Republicans this fall and who knows the size of the political coalition we could create for the nation?

There is more value than the traditional economic benefits than cheap and reliable electricity over a project like this. We should value a project like this for how much advanced education and advance managerial experience it drives into our nation. How much advanced intellectual experienced it drives into all the employees who are associated with this voyage. This is, and always was, the real wealth of our nation!

Wednesday, March 21, 2012

An Unforgettable Night - ATC Operator Event at Palisades

There are a lot of these CRDM seal shutdowns at Palisades. No other plant in the nation has these kinds on troubles. These complex seal repair shutdowns have been involved with unpredictable interactions and incidences.

A initial plant design defect that is not corrected is driving enormous complicity into the control room and their employees are being overwhelmed by it.

I told the NRC this was a very important event for the industry and there should have been reports to the industry about what went on this night a Palisades. What nobody can get away from, the agency doesn't have the capability to capture events in such detail as this employee did.

This event occurred on Oct 23, 2010 and Palisades has had another seal shutdown on Jan of this year. We got to see this letter for the first time this March 8 2012.

I believe the event was entered into the Palisades ROP as a question of why did one of their employees leave the control room. Nobody has yet answered why were they winging this vacuum fill procedure, why did they lose reactor water level for a period of time worrying about vortexing and why did they allow so many distraction going on while they were manipulating core water level during a high risk alignment of the plant.



An Unforgettable Night - ATC Operator Event at Palisades

Introduction
On the early morning of October 23, 2010, I left the ‘at the controls’ area of Palisades nuclear plant without a proper relief or turnover. Up until that time, I had always considered myself to be a very conscientious and safe operator. I never imagined that I would leave the control room without a proper turnover – but I did. I hope by writing this article, others can learn from my mistakes and avoid making the same or any similar mistake. With that objective, this article describes the events that led to my actions, the effect this event has had on me, the lessons I have learned, and my experiences with the NRC investigative and enforcement processes.

Description of Events
Palisades was nearing the end of a refueling outage, which was on course to be our most successful ever due to the short duration and large number of major projects completed. We were about to enter our third reduced inventory period to perform a vacuum fill operation.

This vacuum fill procedure was relatively new for Palisades, having successfully

performed it for the first time during the previous refueling outage. It is a procedure to lower the water level in the reactor to the middle of the hot leg, and then draw a vacuum on the Primary Coolant System (PCS) to evacuate air and other non-condensable gasses. We devised this procedure in an effort to improve plant reliability—specifically to extend the life of our control rod drive mechanism pressure boundary seals.

Excerpts:

During the brief, I mentioned that during my turnover briefing, I heard that the reactor head did not have a vent path.

We lined up the drain path and commenced, but the PCS level indications did not respond as expected and we stopped the drain.

During this period, we had Auxiliary (non-licensed) Operators (AO's) troubleshoot the problem by verifying level glass and vent path lineups.

Concurrent with the PCS drain, most of the control room staff was at the Infrequently Performed Test and Evolutions (IPTE) brief for the vacuum fill work.

While this occurred, we had more issues with the EHC system; a reactor operator called the control room and stated he was not sure we had a good EHC flow path.

I felt this was a problem that required reviewing the prints and was too distracting with the PCS drain taking place while in reduced inventory, so I handed off the call to a different operator.

I told a Senior Reactor Operator that we were having issues with the EHC system, but he was busy overseeing the PCS drain.

A few moments later, however, the EHC low level alarm came in.

Several minutes later, the low level alarm was still not clear and I was concerned about a possible leak, so I secured the pump. I quickly heard back that there was a spill...

Consequently, they requested that the pump be placed in service for their vendor work, stating the cooling and flow path issues were solved.

This was all happening while the PCS level indication troubleshooting was in progress.

Eventually, Maintenance workers removed some temporary flange covers on the reactor head for a better vent path.

The drain that we initially briefed to be about 17 minutes ended up taking over three hours.

After we got to mid-loop, I lowered shutdown cooling flow to about 3100 gpm, which was the high end of the vacuum fill requirements.

...commented that he did not like the pace I was making my adjustments.

The previous time we performed the vacuum fill procedure, it worked flawlessly, but this time was different.

There was indication of a leak somewhere that was intermittently venting and allowing pressures to equalize throughout the system.

While Operator 1 and other members of the control room staff were troubleshooting the problems with vacuum fill, we received the low critical service water alarms and entered a procedure for "Loss of Service Water."

...the Control Room Supervisor (CRS) had to come down off the CRS’ “island” and speak with me directly to ensure effective communications during this very active period in the control room.

We soon learned that the work control center sent out a lube and stroke PM for the main lube oil service water isolations, and that was probably the cause of the low header pressure.

During the hold, I noticed the shutdown cooling flow rate had slowly started to trend down to 2900 gpm on its own and I voiced my concerns to the Control Room Supervisor. I showed him the one minute shutdown cooling flow rate trend on the Palisades Plant Computer (PPC), and said there may be some vortexing or other flow phenomenon that I did not understand.

He stated we could also enter the LCO, if necessary.

Suddenly, however, PCS level indication sharply fell to an elevation below the bottom of the hot leg.

As PCS pressure rose, the primary coolant level slowly recovered to an expected value and I received the order to raise the PCS level to exit reduced inventory.

By this time, it was early morning and we exited reduced inventory during SRO turnover.

Thursday, March 01, 2012

Byron Switchyard Insulator 2.206


So what would prevent all the defective switchyard insulators from breaking and shorting in a heavy storm, tornado or earthquake and then causing another LOOP...

The last LOOP at the plant was extraordenary, in that the plant was disconnected from grid for 31 hours. LOOPs are generially 1,2 to less than 4 hours duration.

March 20:

Exelon upgrades equipment at Byron nuclear plant

The Associated Press

BYRON, Ill. -- Exelon Energy says it has finished upgrading equipment at a northern Illinois nuclear plant where a power failure caused a reactor to shut down two months ago.
The company says it has replaced electrical insulators in the switchyards that help move power to and from the reactors at the Byron Generating Station, which is located about 95 miles northwest of Chicago.
In January, an insulator in Unit 2 switchyard failed and interrupted power, causing the reactor to automatically shut down as a precaution.
Insulators are protective equipment that helps regulate the flow of electricity. Exelon says Unit 1 was taken offline last week while upgrades were finished, and Unit 2 upgrades were finished over the weekend. Both units are back online at full power and generating electricity.

Read more here: http://www.bnd.com/2012/03/20/2107206/exelon-upgrades-equipment-at-byron.html#storylink=cpy

Saturday, February 18, 2012

Vermont's Appeal over VY

Interesting, the chairman posed the same question I did but in a more delicate manner...
Gregory B. Jaczko: "Looking to the Future”

February 9, 2012
"So the question is: what does that tell us about the use of risk? Is it an effective metric? To some extent one could argue that based on the risk models, accidents like Fukushima will happen -- hopefully with a very unlikely or low frequency, but they will happen -- and they are acceptable. They are well within our risk metrics, primarily because we ultimately had a robust system that allowed people to be evacuated and allowed ultimately for people to be relocated from any exposure to radiation.

Now, I think if I were to talk to an average person on the street and say that, people would say no, that was a pretty significant event. And I personally think that's right. I think that this was a significant event, and it was an unacceptable event. But if we look at the risk models that we use today, it is not -- in our risk model -- an unacceptable event."


Feb 18:
I also spoke, "imagine if we had a core meltdown without fatality in a severe accident in the USA. You people discount this, only consider a nuclear fatality. A nuclear accident with fatality is just marginally worst than a no fatality.

At Peach Bottom, it would destroy two plants because they are so close to each other even if the other one wasn't damaged. It would destroy the value of the largest utility in the USA. There would be massive investigations. What was once thought of as accepted behavior would be thought as gross negligence and a cover-up for decades. I am certain the investigation would rip the lid off the NRC and the whole industry...what other plants are threatened. Certainly the NRC losing their credibility and trust would be a accident in itself.

Remember, we have only had a meltdown in the pre internet period and pre social media interconnectivity period. TMI would be a drastically different accident in this social media and self publishing world....nobody could control the political fallout from this. It would cascade until the energy was spent. And Fukushima got us all teed up already....

Who knows what this stock and debt panic would do to the utilities in the outcome in the meltdown without fatality. That is 20% of our electricity, its a enormous amount of electricity and irreplaceable out for a decade or two. We'd have massive speculation, price spikes and shortages for a far as you can see. It would be disruptive to the whole nation. It would be disruptive to our political system. I am talking about a catastrophe of epic proportions for our electric system.

On a planetary level, the USA would be a nuclear technology disgrace...who knows how many plants would get kicked off the line. Our national stature and credibility would be threatened. Depending what they find under the sheets, we might even get a new president...it might just throw the election. You know everyone would play political football with this. Can you imagine the world we would live in if the antis had a current meltdown as ammo?  

Feb 17 (Reuters) - Vermont's Attorney General appealed on Saturday a federal judge's ruling that had prevented the state from shutting down its only nuclear power plant, escalating a two-year battle over state's rights and atomic energy.

Was that pretty neat yesterday in the 2.206 proceeding inviting all the NRC and Exelon employees to watch the Sunday CCN special about the NRC and VY...

Wasn't that neat when i said to them, "does anyone think this is a coincidence that I on am on a phone in my house and I got all you people in your offices listening to me today, and you got a CNN special about Vermont Yankee later this weekend. Does anyone not believe this was intentioned this way?

Then I give them my rendition of the Vermont Yankee problem..."it is excuses over and over again of the NRC and utilities with intentionally turning your heads away from immediately addressing and fixing known problems in the industry"...

Monday, February 13, 2012

NRC’s OIG: Confirmatory Action Letters



Feb 15: Yep, you got to wonder if the NRC OIG initiated the CAL investigation after reading my Casablanca-Palisades 2.206 on Feb 22, 2011... The NRC says the investigation started 9 months ago?

You notice I stayed with the themes of the Casablanca 2.206 on my newest 'Nothing Ever Matters-Palisades' 2.206.     


OIG-12-A-09 February 10, 2012

Audit of NRC’s Use of Confirmatory Action Letters

I think they got a lot of neat tools, but the NRC doesn't have the skills and training in order to properly and effectively use these neat tools. You catch the similarities with the OIG event reporting...mass confusion with contradictory NRC policies. Can you imagine all the confirmatory Actions letters awarded to Palisades and Entergy...and why are they so ineffective with getting a change of heart out of Entergy?  

    Jan 10, 2012: Request Emergency Palisades Shutdown

    "We are broadly worried about in 2009 over the Palisades security falsification, in the outcome of the violations...whether all the reports and employee cultural surveys with the assortment of NRC and Entergy processes over this very serious violation ever had any meaning at all. According to the Palisades Fukushima Emergency Power System DC short and plant trip, the most recent root cause Entergy admits there is deep and widespread safety cultural problems at the Palisades plant. I feel Palisades safety culture was in the pits in 2009 and before...and the cultural safety survey was a grand Entergy and NRC falsification. The NRC Alternate Dispute Resolution secession over this, the Confirmatory Order, the Entergy investigative reports and safety cultural survey, the willing acceptance of this insanity by the NRC and Entergy...the NRC created the inaccurate falsified impression to the outsiders that Entergy had discovered all the cultural safety problems and corrected them. Nothing could be farther from the truth, all these corporate and agency processes covered up and deepened, took the public’s eyes off fixing Entergy...where Entergy now is in much worst condition than they were then. I request independent outside investigation on this dangerous agency corruption before Palisades start-up."
Audit of NRC's Implementation of 10 CFR Part 21, Reporting of Defects and Noncompliance OIG-11-A-08 March 23, 2011 "NRC Regulations and Guidance for Implementing Section 206 Are Contradictory and Unclear

Part 21 component defect reporting issues exist because NRC regulations and guidance for implementing Section 206 are contradictory and unclear. Specifically, NRC regulations and guidance for implementing Section 206 contain stipulations that have been interpreted as not requiring a report under Part 21 if an LER was not required. This interpretation seemingly contradicts Section 206, which requires reporting of component defects that could cause substantial safety hazards. Furthermore, applicable NRC reportability guidance is not utilized by some licensees and NRC staff, and NRC’s Baseline Inspection Program does not include requirements to inspect licensee reporting of Part 21 defects."
Transcripts 2.206 Petition Review Board RE Palisades Nuclear Plant dated January 31, 2012
"And like I said, you know, we can -- all this survey -- cultural survey stuff, you know, words have meaning, and results having meaning and stuff. And that was inaccurate, that survey stuff was inaccurate. And it's a con job because, essentially, Entergy gets to hire their own people. And they probably tell the companies beforehand this is what we want, can you do it for us? And that's what they get.

You know, I don't know. Maybe the NRC ought to hire somebody independent or something like -- I don't know what the question is but, you know, that was -- we could have -- Entergy should have found the problem two years ago and they didn't.

The problem is they go through another ADR process. It began in 2010. It just came out as an enforcement finding with the employee that stormed out of the control room. Basically, the same thing is --another agreement. This thing isn't, you know --Entergy, you do it or stay shut down. This is another-- you know, a gentleman agreement, essentially -- I can't even say the word, confirmaternity [confirmatory action] letter, whatever you call it.

How many (confirmatory action letters) has Entergy had in the last few years --two or three at Palisades, and who knows what they've gotten over the fleet. I mean, how well does that work and stuff? So, you know, so another survey is going to be, done fleet-wide, more fleet training. These poor guys they're getting overwhelmed with all the fleet training on integrity and stuff. You know, it just bothers me that this thing wasn't prevented." 
US nuclear watchdog questions oversight of safety enforcement

By M. Alex Johnson, msnbc.com

The federal government's nuclear watchdog has faulted the Nuclear Regulatory Commission for failing to follow through on safety agreements with nuclear facilities, saying its system for tracking corrective action raises questions about its oversight of nuclear safety and security.

After an eight-month audit, the NRC's Office of Inspector General concluded last week that the commission has no centralized way to oversee or follow up on documents confirming that a nuclear facility has committed itself to address "significant concerns regarding health and safety, the environment, safeguards or security."

The documents — known as Confirmatory Action Letters, or CALs — are one of the last measures before the NRC cracks down with a stringent binding order like suspension or revocation of a nuclear plant's license.

Because CALs are reserved for a small number of potentially serious cases — 15 to 20 of the hundreds of incident reports the NRC issues each year, according to its records — effective oversight of the confirmation process is of "utmost importance," the inspector general said. But in some cases, the action letters are so poorly drafted that they don't even make it clear who the intended recipients are, the report asserts.

Bureaucracy to blame


The problem is one of red tape, not willful inaction or neglect, the report says. But the weaknesses — which include lack of consistent guidelines for regional NRC offices, regional offices' failure to comply with those guidelines and some offices' lack of any tracking system whatsoever — "degrade" the agency's accountability, it says.

 A spokesman for the NRC said the agency believes "the CAL process has been effective" and that it would have a formal reply "in the near future." In an informal meeting last month, the NRC generally agreed with the inspector general's recommendations to update its main enforcement manual, centralize tracking and submit to occasional audits of the action letter system, the report said.

Wednesday, February 01, 2012

Peach Bottom SRV Seal notes


Feb 21
Oversight of Nuclear Reactor Suppliers

See, they don't have broadly the proper quality framework to maintain standards...either operating and new.

Like I said, the NRC doesn't have the power or know how to us power and coercion to maintain standards againt the corporate interest of making profits...

Somebody's got to be the bad guy...not a consensus maker?
Feb 17 (Reuters) - Vermont's Attorney General appealed on Saturday a federal judge's ruling that had prevented the state from shutting down its only nuclear power plant, escalating a two-year battle over state's rights and atomic energy.
Was that pretty neat yesterday in the 2.206 proceeding inviting all the NRC and Exelon employees to watch the Sunday CCN special about the NRC and VY...

Wasn't that neat when i said to them, "does anyone think this is a coincidence that I on am on a phone in my house and I got all you people in your offices listening to me today, and you got a CNN special about Vermont Yankee later this weekend. Does anyone not believe this was intentioned this way?

Then I give them my rendition of the Vermont Yankee problem..."it is excuses over and over again of the NRC and utilities with intentionally turning your heads away from immediately addressing and fixing known problems in the industry"...


Main Steam Safety Relief Valves Buna-N thread seals (March17, 2002)

You like that picture, these electrical towers are what the back-up to the back-up Fukushima emergency supply of electricity get supplied to VY through...

First Transcripts

Second Transcripts
Some commonalities with the SRV seals

1) Buna-n.

2) Both facilities when they got new actuators ...during the next cycle their buna-n failed. VY had multiple seal failures after new actuators and Peach Bottom's seal failure came after they were just installed.

3) As a thumb rules, you can't trust the quality of buna-n material after 2002.

Mr Mulligan

I have also spoken with the Peach Bottom Resident Inspectors regarding your request to discuss the Peach Bottom safety relief valve (SRV) seal failure history with them prior to the PRB teleconference. The Senior Resident Inspector, Sam Hansell, and Resident Inspector, Adam Ziedonis, would be happy to speak with you. You can contact them directly at 717-456-7614.
The PRB met internally on February 3, 2012, and denied the request for immediate action to shutdown Peach Bottom Units 2 and 3, and replace the SRV pneumatic actuator threaded seals, because there was no immediate safety concern to the plant, or to the health and safety of the public. Specifically, the PRB determined that threaded seals with Buna-N material have been used in the PBAPS Unit 2 and 3 SRVs for 20 years with no seal failures until the subject failure in September 2011. The 3-ADS-SRV 71B seal had been in service for less than one year before its failure and the seals are replaced every 4 years. In addition, the insulation configuration on the Vermont Yankee SRVs that contributed to their 2 seal failures was confirmed to not be a contributing cause for the PBAPS Unit 3 ADS-SRV 71B failure. These facts support the conclusion that the failure of the 3-ADS-SRV 71B threaded seal was not a common mode failure, or an age related failure, but was isolated to the particular seal installed in the 3-ADS-SRV 71B actuator in November 2010. This information will be included in a future NRC Inspection Report regarding the subject SRV threaded seal failure.
Thank you,
John Hughey
Peach Bottom Project Manager
NRR / Division of Operating Reactor Licensing
Phone: 301-415-3204