Wednesday, July 03, 2019

ANO 2: What Happened To This Guy Since May 28

So they were at the end of a outage when they had this short? 

Either they had a short in the wiring or the pump? You get it, big piece of equipment fails, over and over again, that is how you get this long repair period.


Just saying, they got the all clear from the column 4 fiasco. 
INSPECTION SCOPES In accordance with Inspection Manual Chapter (IMC) 0305, Section 10.02.d.7, this inspection report is a follow-up inspection of your improvement initiatives completed since the Confirmatory Action Letter (CAL) (EA 16-124) was closed to verify that performance improvement was sustained in selected areas.  Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted.  Currently approved IPs with their attached revision histories are located on the public website at  http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html.  Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with IMC 2515, “Light-Water Reactor Inspection Program - Operations Phase.”  The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess licensee performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.


Unit SCRAM Code RX Crit Initial PWR Initial RX Mode Current PWR Current RX Mode
2 A/R Y 100 Power Operation 0 Hot Standby

Event Text

AUTOMATIC REACTOR TRIP DUE TO A REACTOR COOLANT PUMP TRIP ON GROUND FAULT

"This is a 4-hour Non-Emergency 10 CFR 50.72(b)(2)(iv)(B) notification due to a Plant Protection System (PPS) actuation. Arkansas Nuclear One, Unit 2, automatically tripped from 100 percent power at 0512 CDT. The reactor automatically tripped due to 2P-32B Reactor Coolant Pump tripping as a result of grounding.

"No additional equipment issues were noted. All control rods fully inserted. Emergency Feedwater (EFW) actuated and was utilized to maintain Steam Generator (SG) levels. The EFW actuation meets the 8-hour Non-Emergency Immediate Notification Criteria of 10 CFR 50.72(b)(3)(iv)(A). No Primary safety valves lifted. Main Steam Safety Valves (MSSVs) did lift initially after the trip.

"The NRC Resident Inspector has been notified.

"Decay heat is being removed via the steam dump valves to the main condenser. Unit 2 is in a normal shutdown electrical lineup. Unit 1 was not affected by the transient on Unit 2. The licensee notified the State of Arkansas."

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