Tuesday, December 20, 2016

Junk Plant Columbia:More Coponents Fail During Lastest Hard Scram

Why wasn't this picked up during normal testing and inspections?

Power ReactorEvent Number: 52443
Facility: COLUMBIA GENERATING STATION
Region: 4 State: WA
Unit: [2] [ ] [ ]
RX Type: [2] GE-5
NRC Notified By: DAVID PORTER
HQ OPS Officer: BETHANY CECERE
Notification Date: 12/19/2016
Notification Time: 07:39 [ET]
Event Date: 12/18/2016
Event Time: 23:20 [PST]
Last Update Date: 12/19/2016
Emergency Class: NON EMERGENCY
10 CFR Section:
50.72(b)(3)(v)(D) - ACCIDENT MITIGATION
50.72(b)(3)(ii)(A) - DEGRADED CONDITION
Person (Organization):
RAY KELLAR (R4DO)

UnitSCRAM CodeRX CRITInitial PWRInitial RX ModeCurrent PWRCurrent RX Mode
2NN0Hot Shutdown0Hot Shutdown
Event Text
UNISOLABLE LEAK ON HIGH PRESSURE CORE SPRAY

"On December 18, 2016 at 2320 [PST], a leak was discovered on the High Pressure Core Spray (HPCS) system minimum flow line. The leak is located at a bolted flange downstream of the manual isolation valve HPCS-V-53. The location of the leak is not isolable from the suppression pool. This provides a direct path from inside the Primary Containment to the Reactor Building.

"High Pressure Core Spray system is a single train Emergency Core Cooling System (ECCS) system, therefore inoperability is reportable per 10 CFR 50.72(b)(3)(v)(D).

"Based on the location of the leak, Primary Containment integrity is compromised. Primary Containment was declared inoperable and is reportable per 10 CFR 50.72(b)(3)(ii)(A).

"The cause of the leak is under investigation. Actions are underway to cool down and enter MODE 4."

The licensee has notified the NRC Resident Inspector.

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