Friday, August 19, 2016

Troops On The Boarder Protecting Us From Massachusett Heroin?

 Wonderful and current reference information on the epidemic

NH1 News Investigates: Taking back NH from the drug crisis
Lawrence and Holyoke Ma is where 90% of the heroin comes from in the Surrounding Hinsdale area.


By Joshua Miller Globe Staff  August 19, 2016

American politicians often campaign with promises to send troops to the Mexican border.
Donald Trump has, infamously, called for building “a great wall” and making Mexico pay for it.
But now Jeanie Forrester, a New Hampshire state senator and gubernatorial candidate, has a different kind of idea: troops to protect the Granite State from drug dealers from Massachusetts.
Aiming to fight the scourge of opioid abuse and staunch the flow of heroin, Forrester said she would consider deploying the New Hampshire National Guard to patrol the state’s southern border with Massachusetts, according to the Concord Monitor newspaper.
Mike Dennehy, a senior strategist for the campaign, told the Globe Forrester wasn’t available to chat Friday. He said her original idea was to deploy the New Hampshire Guard, with other states and federal approval, to the Texas-Mexico border.
But he said Forrester wouldn’t hesitate to use the National Guard to support law enforcement in their interdiction efforts with drugs coming in from other states.
Jeanie Forrester, a New Hampshire state senator and gubernatorial candidate.
“The bottom line is that Jeanie takes this issue very seriously and is thinking outside the box,” he said. “The same old politicians coming up with failed ideas that
Yep, same old response from politicians for a unprecedented crisis. NH is the hot bet of heroin nationwide. Did I hear it right, if the NH rate was the same nation wide we would have a death rate of 100,000 a year.
aren’t working won’t cut it, especially in Manchester where they are overwhelmed. The drug issue in New Hampshire is a crisis and needs to be treated like a crisis. And she will be the governor who begins the rollback and end to our present drug crisis.”
But one of Forrester’s top opponents for the GOP nomination for governor brushed aside the idea of sending troops to the border with Massachusetts.
“I don’t think that’s a well thought-out plan,” said Ted Gatsas, the mayor of Manchester, the state’s biggest city. “Putting National Guardsmen on the border — are you going to stop every car coming from Massachusetts? It just doesn’t make sense.”
Gatsas said he’s tough on drug dealers, proposing increasing penalties. But he also supports other approaches, such as instituting a seven-day initial prescription limit on opioids, similar to a law passed this year in Massachusetts.
So what does Massachusetts Governor Charlie Baker think of the idea of a neighboring state’s chief executive deploying troops to the common border to protect the Granite State from opioids?
Baker spokesman Brendan C. Moss wouldn’t say. But in a statement Moss noted that Baker recently led a group of almost 50 governors in signing a compact about fighting opioid addiction, “calling for a coordinated approach between states to combat the opioid epidemic, including collaboration with law enforcement to end opioid trafficking.”
A spirited campaign for governor is underway in New Hampshire, which elects its chief executive every two years. Governor Maggie Hassan, a Democrat, is running for US Senate so the gubernatorial race is for an open seat and has drawn several Republican and Democratic candidates.
The primary is Sept. 13.
Joshua Miller can be reached at joshua.miller@globe.com. Follow him on Twitter @jm_bos and subscribe to his weekday e-mail update on politics at bostonglobe.com/politicalhappyhour

Legalized All Drugs: Insanity

Honestly, this sounds like a libertarianism. Librarians are government haters and are out to destroy government. They are all around us.

I think pot is relatively harmless. It certainly is a lot safer than booze. I am for legalization. Regulated like booze. I think this would take the pressure off cops and reduce crimes.

In excess of 50% to 75% of the jail population are people who have mental condition. So he says 90% of the jail population is related to drugs. The high functioning mentally ill generally are riddled with addictions of all sorts.

There are methadone programs all over the place. I would agree to a heroin maintenance program if the government ran it. We going to have to feed and house them too? Why not go off welfare to get on the gravy train of heroin. You talking about open heroin stores. They would have to trade giving their identities and DNA to the feds…get it on a government data base. The way this will play out is it would be administrated and the councilors would be barely be trained. All these clinics would be fly-by-night operations. The methadone programs are really expensive to the uninsured. I would agree to if if heroin users on a maintenance program were required to live responsible lives and try to better themselves. I think the cartels response to this would be ever lower prices of heroin and higher concentrations. These guys would be supplementing their government supplied heroin with really cheap on the street heroin.

I would favor a new safe heroin intoxicant that would disrupt the cartels. It would have to be a intoxicant creating a better high than heroin. The people who become addicted to heroin are basically trying to blot out their lives.

Remember prohibition came about because of wide spread abuse of alcohol. There were drunks lying all over the place. We used alcohol at a much higher rate in the beginning of the 20th century than today. I think the anti heroin conservatives would gain a lot more political leverage over this than the liberals.

I think we need to pick a few large heroin producing countries…then crush them as example to everyone else. Remember the apex of terrorism occurs in un-governable heroin areas throughout the world.




Van Wickler speaks out against war on drugs


By Xander Landen Sentinel Staff | Posted: Friday, August 19, 2016 12:00 pm

Richard Van Wickler, the superintendent of the Cheshire County jail, remembers when he first questioned the war on drugs. He was working his first job as a correctional officer in the Merrimack County Department of Corrections in the 1980s, when one day, he was tasked with putting a man accused of homicide and a young contractor accused of marijuana possession in the same holding cell.

“I’m looking at this contractor, who is frightened to death, who is about to be convicted next this person who has just committed homicide. ... It was that moment that I realized that there’s something very odd about these types of laws,” Van Wickler said in an interview with The Sentinel.

Today, Van Wickler’s open about his opinions on U.S. drug laws. He believes all illegal substances should be decriminalized and that no one should be put in jail for possession or use of drugs.

He also believes that without enough government-funded treatment centers and services for drug addicts, the job of rehabilitation has fallen unfairly on the criminal justice system.

Van Wickler spoke about his opinions and advocacy against today’s drug policy at a meeting of the Kiwanis Club at The Pub Restaurant Wednesday.

His comments come as New Hampshire contends with a opioid crisis, and an unprecedented number of people in the state dying of drug overdoses.

Van Wickler also suspects that 90 percent of people currently serving sentences in the Cheshire County jail are doing so for crimes connected to their addictions or drug use. Among inmates who report to be drug users, the majority say they abuse heroin, he said.

Van Wickler told about 20 people at the meeting that since laws targeting drug users became stricter under the Richard Nixon and Ronald Reagan administrations, the government’s effort to create a drug-free society — also known as the war on drugs — hasn’t come close to reaching its goal.

According to data he cited at the meeting, one in three Americans today admits to using an illegal drug at some point in his or her lifetime.

“If the solution to create a drug-free society is to find these people, arrest them, incarcerate them and hope that when they’re released, they never use again, it’s not working,” Van Wickler said at the meeting.

If the war on drugs has succeeded in doing anything, he said, it’s putting people in jail. While the U.S. contains only 5 percent of the world’s population, it holds 25 percent of the world’s inmates due, in part, to laws that target drug users, according to Van Wickler.

Ideally, he said, he wants drugs to be legalized, which he claims would dramatically decrease both the number of people in jail and crime rates throughout the country. But he thinks a more realistic first step would be to decriminalize drugs throughout the country.

He’s also a member of an organization called Law Enforcement Against Prohibition (LEAP), which shares that same view. The group is comprised of 80,000 supporters — including police, prosecutors, judges and corrections officials — who support the decriminalization of drugs not only because of the effects drug laws have on users, but also the effects they have on law enforcement officers.

The group believes legalizing drugs would sharply reduce the amount violence that officers face in the field every day.

“The Drug Enforcement Agency has determined that the majority of gang violence and the reason why gangs exist is over illegal drug marketplace disputes,” Van Wickler said.

He serves as LEAP’s chairman of the board of directors as well as one of LEAP’s speakers, who represents the organization at public events. He said he’s the sole LEAP speaker who’s an active member of law enforcement, as many officers who participate in the organization fear disapproval or judgment from their colleagues.

Van Wickler said he’s never experienced any of that.

“The opposite is true. There’s great admiration. When I speak to law enforcement officers ... most of them agree. It’s not working,” he said.

Van Wickler stressed that although LEAP supports the legalization and decriminalization of drugs, neither he nor the organization are pro drug use. Members just believe the benefits of striking down the current drug laws would far outweigh its costs, he said.

Multiple Kiwanis Club members at the meeting were skeptical of the idea of a society in which drug users could not be punished and drugs could be obtained legally.

Junk Plant Pilgrim Shuting Down Again II

Here is my comment on the hot ocean water down power. Basically I think this is just a excuse to fix the MSIV. I think closing times were degrading...they knew it would be a few weeks at 75% power...so decided to take a look at the MSIV.
Two days ago: I suspect we will see them in repeated shutdowns and down powers for another month or more. It will beat the hell out of the plant. This environment is rich with screw-ups and breaking equipment, it is highly likely they will get a plant trip or other
The last MSIV event happened on Aug 22, 2015. I doubt this is a coincidence. Maybe something to do with summertime duty or temperatures. The main condenser cleaning down powers. the steam line vibrations from this.  

That bad boy.
Pilgrim shutting down for valve repair
Malfunctions in system have forced 2 closures in year.

By Christine Legere

Posted Aug. 18, 2016 at 6:46 PM
Updated at 9:41 AM

PLYMOUTH — Pilgrim Nuclear Power Station, already one step from being forced by federal regulators to close down based on poor performance, is now trying to figure out the cause of a malfunctioning valve designed to prevent radioactivity from leaking into the environment during a nuclear accident.

The plant was slowly powering down to full shutdown Thursday so the valve could be fixed. This is the second time in a year that a problem in the valve system has shut down the reactor.

Critics say it is further evidence that parts are wearing out and not being replaced in time at the 44-year-old reactor because owner-operator Entergy Corp. plans to permanently shutter the plant in mid-2019.

“Even with increased federal oversight, repetitive failure of critical safety equipment is yet another serious warning that Pilgrim's ongoing degradation continues to threaten our region,” Diane Turco, co-founder of the watchdog group Cape Downwinders, wrote in an email. “Pilgrim is an accident waiting to happen. Closure should be now, not in 2019.”

Eight “main steam isolation valves” regulate the flow of steam through four large lines that connect the nuclear reactor to the turbine, which spins and produces electricity.

Federal standards require that the valves close at a certain speed to prevent radioactive leaks in an emergency. Operators found during testing Tuesday that the valve at issue was closing too slowly.

This is not the first time the steam isolation valve system has malfunctioned. The plant went into automatic emergency shutdown in August 2015 to prevent a buildup of reactor pressure after a steam isolation valve closed when it should have remained open.

Just weeks after that incident, federal regulators shifted Pilgrim into its so-called Column 4 performance category — as low as a plant can go without being ordered to simply shut down.

Neil Sheehan, spokesman for the Nuclear Regulatory Commission, said the valve problem last summer was “one of the factors that contributed to the plant being moved to Column 4,” since it resulted in an emergency shutdown.

When Pilgrim workers discovered the valve was not closing fast enough to meet standards Tuesday, they closed one of the four steam lines and limited reactor output to 75 percent to prevent a pressure buildup. On Thursday, they were working toward full shutdown.

Sheehan said it was “too soon to tell if wear and tear is the cause of the slow closure time.”

“Entergy is evaluating the cause of the valve slowness and will have to develop a plan to fix the problem,” Sheehan said. “We will be closely following the company’s troubleshooting and repair efforts.”

Mary Lampert, director of Pilgrim Watch, said she could save the NRC the trouble of waiting for a cause to be found.

“Let me help them out,” she wrote in an email. ”The cause is a continuation of Entergy's record of poor maintenance — prioritizing their bottom line over public safety — and NRC allowing them to do so.”

After investigating last summer’s valve problem, Entergy concluded a faulty strut supporting the gas pressure line had allowed the line to drop onto the main steam line. After years of vibration, the gas pressure line ruptured and failed to open the valve.

“The August 2015 problem was, according to Entergy’s report, caused by an action pre-2001 that remained ‘hidden’ for over a decade until it caused the failure,” wrote David Lochbaum, director of the Nuclear Safety Project for the Union of Concerned Scientists, in an email.

The company checked the gas pressure lines on the other seven valves for signs of wear after the rupture.

“Entergy confined its fixes to only the specific thing that failed that time,” Lochbaum wrote. “It’s a good example of the difference between doing it right and doing it Entergy’s way.”

Lochbaum said one need only look at the NRC’s performance standards matrix, which ranks nuclear plants nationwide, to see Entergy is a poor performer in general.

“Only 11 reactors in the entire country are not in Column 1, where the NRC expects them to be,” Lochbaum wrote. “Poor performance has moved 11 reactors out of Column 1, and Entergy owns five of the 11 reactors, including all three of the worst performers.”

Pilgrim, along with Arkansas I and II, all Entergy-owned, are the only reactors in the NRC’s lowest performance column.

— Follow Christine Legere on Twitter: @ChrisLegereCCT.

Thursday, August 18, 2016

Heroin, Stealing Merchandise, A Mother And A PerfectThree Year Old baby boy in Keene

They are trying to protect a heroin mother and 3 year old baby. How much money did she cost us so far?

They were trying to protect the mother and child in 2015 by allowing her to plead down from theft. The courts wanted to latch onto her in 2015 and make her go to treatment? Did it work?  

Bet you she is still a active heroin user. Imagine the power of a substance that can strip a baby from a mother? How many heroin babies have been striped from mothers in NH? I live next to a similar perfect boy. There is a high probability Dakota will be dead in a year. 

Has that beautiful little boy been taken away from her yet? Does financially impaired DCYS have that little boy?

Plead down from stealing?
637:3-a Willful Concealment. –
    I. A person is guilty of willful concealment if, without authority, he or she willfully conceals the goods or merchandise of any store while still upon the premises of such store. Goods or merchandise found concealed upon the person shall be prima facie evidence of willful concealment. Notwithstanding RSA 637:11, willful concealment shall be a misdemeanor

A perfect boy born to Dakata in 2013 
2013 : "a boy, Maddox Paul Matthew, to Dakota Keller and David Wood of Drewsville"
 Three people charged during criminal patrol Wednesday
Posted: Thursday, August 18, 2016 12:00 pm
Three people charged during criminal patrol Wednesday By Sentinel Staff SentinelSource.com
Three people were arrested on warrants Wednesday during a stepped-up criminal patrol conducted through a collaboration of area law enforcement agencies.
The patrol was aimed at those involved in heroin sales, according to a news release from Keene police.
Arrested were:
* Glen Goodwin, 24, of Fitzwilliam, charged with a felony count of sale of heroin. Goodwin is accused of selling a quantity of the drug for $200 on July 11 to a person cooperating with the N.H. Drug Task Force. He was released on $10,000 personal recognizance and is scheduled to be arraigned Sept. 1 in Cheshire County Superior Court.
* Jonathan R. Poanessa, 20, of Swanzey, charged with a felony count of sale of cocaine. He is accused of selling cocaine to another person for $100 in May. Poanessa is on probation for a 2014 drug offense and was held without bail, according to police. He will be arraigned at a date to be determined in Cheshire County Superior Court.
* Dakota A. Keller, 25, of Keene, accused of violating her probation after being convicted of willful concealment in March 2015. Police don't say how Keller allegedly violated her probation. She was held for lack of $1,500 bail and is scheduled to be arraigned Sept. 18 in 8th Circuit Court District Division in Keene.
The patrol was a collaboration among the Keene Police Department, N.H. State Police, the Cheshire County Sheriff's Office and the N.H. Attorney General's Drug Task Force. Anyone with further information on these cases is asked to call Keene police at 357-9820 and ask to speak with Detective Don Lundin or Detective Jen Ramey. Information can also be provided anonymously at www.ci.keene.nh.us/departments/police/anonymous-crime-tips.


Wednesday, August 17, 2016

Keene Sentinal and Mike Mulligan Develped New Series On Locale Heroin Problems.

I initiated this Keene Sentinel set of articles about heroin in Hinsdale. I talked about Hinsdale's heroin troubles to Mr. Landen... talked about these Hinsdale sorrows reflects all the communities surrounding us.

The Sentinel suggested I disclose to Hinsdale I was working on this story with them. Locale people might want to more talk to me about heroin issue after this. Give me a call or pull me over while I am biking. I will pass on the information to the Sentinel or have Mr. Landen give you a call at home. Or just listen to you. I can take whatever you got.  

I know for a fact the Hinsdale Police chief and Hinsdale selectmen have been recently inundated by phone calls from the news media and request for interviews, inquiring about the troubles of our police department.     
Posted: Wednesday, August 17, 2016 12:00 pm
By XANDER LANDEN and CALLIE GINTER Sentinel Staff SentinelSource.com
The opioid epidemic that’s leading to unprecedented numbers of drug deaths in New Hampshire has given rise to grim statistics. But within the facts and figures is a more anecdotal claim that keeps getting repeated.
“Everybody in our state at least knows of someone who has a child or a student or someone they’re connected to who has a drug problem or has overdosed,” said Jennifer Horn, chairwoman of the state Republican Party, in an article published by RealClearPolitics last November.
In August, gubernatorial candidate Colin Van Ostern said much the same thing.
“We all know someone, some of us in our own families, who have fallen into the (devastating) opioid trap, who have fallen into addiction or a substance abuse disorder and we have to work together to overcome it,” said the executive councilor, a Concord Democrat, when he unveiled his strategy to tackle the opioid problem if elected.
But in the heart of a community weathering the crisis, how well does this assumption match reality?
The Sentinel conducted an informal survey to find out.
Of 50 people randomly selected and interviewed over a two-day period on Keene’s Main Street, 38 of them — 76 percent — said they know someone with an opioid addiction personally or through a mutual acquaintance. Twenty-seven said they’re touched by the opioid epidemic at a close range — through a co-worker, teacher, friend or family member — while the other 11 knew of an addict second-hand.
Three, including Anna Sullivan, 25, of Keene, said they’re addicted to or recovering from opioids themselves.
Sullivan’s a recovering heroin addict who said she’s been sober for two months. She said she knows many people addicted to opioids, mostly heroin, and the survey results don’t surprise her. They shouldn’t surprise other locals either, she noted.
“It’s always been around, and it’s always been a problem, and more people are doing it than you think,” she said.
Ray Lindsey, 29, of Surry, runs a coffee stand in Railroad Square. Roughly three weeks ago, he said, he called the police about two separate opioid overdoses he saw in the square on a single day.
Lindsey also has a personal connection to opioid addiction; he said a relative’s in recovery for heroin use, and spent time in jail on drug charges.
The Sentinel’s survey was unscientific and limited by a range of factors. The sample size was small, the respondents pulled from a single geographic area and the data likely influenced by people’s willingness to be candid, in face-to-face conversation, about a difficult, stigmatized subject.
But it offers insight into just how many people are being affected by the crisis, and was conducted at a time when Keene is seeing a spike in opioid overdoses.
From January through May this year, the Keene Fire Department, on average, used the opioid antagonist Narcan just under 12 times per month, to respond to overdoses for an average of approximately six patients. But in June and July, the department has used Narcan at a higher rate.
In June, the department used Narcan 21 times for 12 suspected opioid overdoses, according to a news release from Fire Chief Mark F. Howard. In July, the department responded to seven overdoses and administered Narcan 14 times.
Last Thursday alone, there were as many as five overdoses in Keene on the same day, three of which were confirmed to be linked to opioid use, according to Deputy Fire Chief Jeffrey Chickering. Keene firefighters responded to these overdoses and administered Narcan three times within an eight-and-a-half-hour period, Chickering said.
As of the fire department’s most recently released data, three people in the Elm City had died from opioids so far this year. Statewide, officials project 482 deaths from opioids and other drugs by the end of 2016.
Those interviewed in downtown Keene offered a glimpse not only into opioids’ grip on the city, but also their reach in the surrounding region, through the accounts of people from Alstead, Richmond, Harrisville, Peterborough, Troy, Gilsum and Jaffrey.
Kim Fallon, chief forensic investigator for the state’s chief medical examiner’s office, said that though The Sentinel survey’s sample size was small, the results aren’t surprising.
“It seems accurate. It seems that the problem is so prevalent that everyone knows somebody or knows somebody who knows somebody who is addicted,” she said.
Standing under the marquee of The Colonial Theatre, a retired emergency room doctor from the area who preferred to remain anonymous said his son has been in recovery from heroin for seven years. He said opioid addiction isn’t limited to people of only one class, race or background.
“It’s all walks of life. Children of doctors, children of anybody. No one is immune to this.”
Callie Ginter can be reached at 352-1234, extension 1409 or cginter@keenesentinel.com. Follow her on Twitter @CGinterKS. Xander Landen can be reached at 352-1234, extension 1420 or xlanden@keenesentinel.com. Follow him on Twitter @XLandenKS

Heroin In Hinsdale,NH: Is WalMart Eating up Police Department Resources

Update 8/18

OK, is Walmart property taxes properly flowing through the selectman office into the police department...such that the police department can fully support Walmart?

Again, the only way we are going to fix this is if we are data driven. Not secret agendas!!!

Update:
"More than 2.4 million Americans were addicted to synthetic pain relievers or heroin in 2014, according to the latest federal survey on drug use and health".
A heavy addicts spends about $200 to $300  a day on heroin.  Think about the crime wave needed to support this addiction. Maybe the total spending by addicts is about a $ 1billion dollars a day. Honestly, are we talking about $365 billion dollars a year heroin tab per year from the USA?
I wonder how much shoplifting at Hinsdale Walmart supports heroin addiction in our area? 
I estimate there are more than 12 million heroin users in the USA. Total of about 15 million users?  
I worked at the Hinsdale Walmart a few years back. I hated working there with how management pushed the conservative ideology. The police were always parading in and out of the store to contend with shoplifters. I got dinged for stealing time at Walmart in their camera'd store wide theft prevention and detection system. I was caught  purchasing snacks for lunch on the clock. This is strictly forbidden.  

When I worked there at Walmart  they was making big bucks over shoplifters. The stores would basically fine the shoplifters. When they caught the shoplifters, they would offer them a deal. Either you pay us $500 to a $1000 dollars on the spot, sign a agreement to never come in the store,  or you are going to jail. It's very time consuming transporting these guys to county jail in Keene from Hinsdale. I image at the police station, they call the court bondsman and he offers them bail. I wonder how many a year end up going to county jail? I imagine these guys got court issues before the shoplifting and the police department is compelled to give them a ride to the Keene jail and facing the court. Is the police station even manned during off business hours? I supposed they got decent cells in the new police building.

Questions I would pose to the selectman is if Walmart is carrying their local tax rates with this police support. Hinsdale is a tiny police force and this site has a lot of customers. Usually Walmart gets locale tax reductions as part of the deal to construct the new store. I wouldn't be shocked if Walmart pays zero or little property taxes as part of the deal to get the SuperCenter into the town.

Does the poorly paid employees have a draw for heroin issues in Hinsdale? The fragile poor employees moved into Hinsdale's slum ghettoes and landlords, thereby intensifying the heroin problem.  You know darling, we need milk and tampons at Walmart, don't forget to pick up the heroin at our  Hinsdale  heroin dealer too. Most of these employees are disabled in on way or another, it a requirement they find work in order to stay on Welfare. It is a hell of a tax write off for Walmart to hire a disabled employee.

The police department would have to be data driven. I doubt this police department collects any data. So they would have to collect the information on all police involvement with Walmart and record it.

The perfect storm with the intensification of heroin addiction in Hinsdale and police needs at Walmart...
According to Walmart Stores executives, it’s all starting to work.
Police chiefs and their officers on the ground say that’s just not so. Ross likes to joke that the concentration of crime at Walmart makes his job easier. “I’ve got all my bad guys in one place,” he says, flashing a bright smile. His squad’s sergeant, Robert Rohloff, a 34-year police veteran who has to worry about staffing, budgets, and patrolling the busiest commercial district in Tulsa, says there’s nothing funny about Walmart’s impact on public safety. He can’t believe, he says, that a multibillion-dollar corporation isn’t doing more to stop crime. Instead, he says, it offloads the job to the police at taxpayers’ expense. “It’s ridiculous—we are talking about the biggest retailer in the world,” says Rohloff. “I may have half my squad there for hours.”
Walmart knows police departments are frustrated. “We absolutely understand how important this is. It is important for our associates, it is important for our customers and across the communities we serve,” says Judith McKenna, Walmart’s chief operating officer for the U.S. “We can do better.”
Questions I would posed to the selectman.

1) How much property taxes a year does Walmart pay to the town?

2) Is the property tax rate ethical and moral compared to the profits they gain in the store?

3) On average, how much money does it cost Hinsdale per shoplifting event (man hours)?

4) When the shoplifter cycles through the courts, they usually get jail time, more likely a big fine and court costs. Does Hinsdale get a proportion of court fines to cover the police cost?

5) Ask the police chief:  how much is Walmart a burden to the police department budgeting?

NYTs: To My Newspaper Buddies, The Sad Story Of Poor Women In Trouble.

Update 8/18
 OK, so you want me to give you my big picture on it all? We don't make life compelling, interesting and worthwhile for the bottom half. Not enough people think life is worthwhile... If you think this thing is money you are crazier than me. Most people think  life is nothing but a grueling journey to nowhere.  That is why we are into all these titillating superficial and temporary pleasures of money, drugs, alcohol and cigarettes, food addictions, worthless temporary thrills,  arrant agendas of no worth to fill up our lives and the grossly expensive citadels of bling. expensive cloths, cars, macmansion and artificial excitement to no ends. It like we are all putting our neurons in a  continuous haze titillation and diversion. We are the la, la, la, la generation till death. The more we build up these citadels of materialism and it doesn't, we work like slaves more, then double up on more materialism to bolster our poor self esteem and confidence. Why isn't life enough?   

How many generations of children pays the price for one mother in trouble?

How does this all play out for the heroin Mothers and children of today?
When Dolfinette Martin was convicted of shoplifting more than $700 worth of clothes in Louisiana in 2005, she had five children, no money and an addiction to cocaine.
Seven years later, in 2012, Ms. Martin became one of a growing number of impoverished women released from prisons and jails whose plight has been largely overlooked during continuing efforts to reverse mass incarceration, according to criminal justice experts.
“That cycle of poverty — not a lot of resources, not a lot of jobs, the lack of education, you kind of give up,” said Ms. Martin, 46, who now works as an administrative assistant.
*And the most common offenses that led to arrests involved drugs...

Junk plant Watts Bar 1 Power Level Jumping all Over The Place Between 84% and 95% Power

The plant and the fuel pin aren't designed for this erratic power history. These guys are designed for long term operations a 100% power.

Region 1 today has a pathetic average power history compared to the other regions. Region 1 seems to be particularly long on the maintenance tooth with all these impaired powered plants. I get it Watts Bar is in region 2.   

Tuesday, August 16, 2016

Dead Ender FitPatrick Plant: I Guess I Got The Wrong Radation leak?

Update 8/17
Basically the leak of high radiation resin into the tank room is just negligence. Usually the leak in the room comes from poor coordination between the rad waste operator and the clean up panel in the reactor building. Usually valves malfunction and leak during a backwash caused by insufficient maintenance, then overfills the tank and spills this resin onto the floor. It has occurred over and over again. If the NRC really cared about the rad dose of the
Fitz employees, they would figure out how to force management to keep up with the maintenance of the backwash system. They decades ago should have ripped out the resin back-wash system and replace it better designed new system.
Again, this indicates the NRC selectively enforces their regulation and the NRC has a inadequate tool bag of rules to protect nuclear industry employees against negligent rad doses.  Basically this leads to a sense of powerlessness to the rank and file front line employees seeing this poor professionalism and safe rad doses...it leads to a wider risk because the safety culture gets impaired effecting a wider risk of more components failing when needed.
And negligent fuel failures makes the resin hotter than a fire cracker. 
Well, I knew there was a radiation leak going on somewhere. The NRC is going


to think I was sending them a special message about a undisclosed
radiation leak. It is plausible I was trying to protect somebody.

Can’t you imagine all the steam and water leaks now in this poorly maintained plant.
Here above is another brainless guess. I produced a lot of recent articles on this dead ender plant. I think the natural gas prices will continue to drop making this newest deal bankrupt.

SCRIBA, N.Y. – The owner of FitzPatrick nuclear plant has allowed highly radioactive waste to leak into a contained area of the facility for at least four years, a safety violation that poses no risk to the public but might make it more difficult to decontaminate the site after the reactor closes.
The problem was cited in the most recent quarterly inspection report by federal safety regulators.
The U.S. Nuclear Regulatory Commission said the accumulation of spilled radioactive waste in the basement of a building at FitzPatrick is of "very low safety significance'' because it occurred in a locked, highly shielded area that is already highly radioactive.
"The bottom line is, we have been aware of this issue for some time, but it poses no immediate risks to any residents or the environment,'' said Neil Sheehan, speaking for the NRC.
Nevertheless, plant owner Entergy Corp.'s failure to address the leak is of "more than minor significance'' because the company knew about the problem for at least four years, the NRC reported.
Nuclear plant owners are required to minimize the accumulation of residual radioactive waste in their plants, which can "greatly increase the cost and complexity of future decommissioning'' after a reactor shuts down, according to the NRC.
Entergy officials today said they put off cleaning up the spill to avoid exposing workers to unnecessary radiation. They have made a robot to do the job instead, said Tammy Holden, speaking for Entergy.
"Cleanup of the area had not been conducted previously because we did not want to subject our employees to unnecessary radiation,'' Holden said. "We have fabricated a vacuum-type robot that will be used to remove the sludge. The removal is scheduled for this month.''
The NRC inspection report issued Friday did not quantify how much waste has accumulated on the floor of the FitzPatrick radwaste building, or how it might impact the plant's decommissioning costs. The waste consists of beads and powdered resins from filters that are used to clean up reactor coolant, said Sheehan, of the NRC.
Nuclear safety expert David Lochbaum, of the Union of Concerned Scientists, said he agreed with the NRC that the leak was of "minor significance.'' It's not uncommon for water spills to occur inside radwaste buildings, leaving waste behind, he wrote in an email. Entergy should have cleaned up the spill because the building floor is not designed to act as a backup storage tank, Lochbaum said.
"It'll be fixed soon now that the NRC (has) shone a spotlight on it,'' he wrote. "Which will demonstrate that it could have been fixed long ago."
The Nine Mile Point Unit 1 reactor experienced a similar long-term spill of radiation waste during the 1980s that was worse than FitzPatrick's, Lochbaum said.
The NRC also criticized Entergy for mistakes during a January 2016 outage that resulted in two plant workers being unintentionally exposed to high radiation levels. Both workers were alerted by alarms from their radiation dose monitors and moved to safety without becoming overexposed, the NRC said.
The NRC is treating both issues raised in the inspection report as "non-cited violations,'' which means FitzPatrick will not face penalties or increased oversight because of them.
Entergy has agreed to sell the 850-megawatt nuclear plant to Exelon Corp., which operates the nearby Nine Mile Point nuclear facility. Until the sale was announced last week, Entergy had planned to shut FitzPatrick permanently when it ran out of fuel in January 2017.
Anti-nuclear activists said the NRC report should raise concerns about the aging FitzPatrick plant, which started operation in 1975.
"These violations highlight the ongoing dangers posed by the upstate nuclear reactors and the lax enforcement by the Nuclear Regulatory Commission," said Tim Judson, of the Nuclear Information and Resource Service. "Entergy has known that this highly radioactive waste spill is a problem for four years, but the NRC has not imposed any fines or other penalties.''
The NRC rates FitzPatrick's general safety performance as "green'' in all 17 categories monitored, the best of four color-coded ratings.

Junk Plant Hatch Junk FirstTime Used 3-Stage SRVs

EDWIN I. HATCH NUCLEAR PLANT - NRC INTEGRATED INSPECTION REPORT 05000321/2016002 AND 05000366/2016002; AND EXERCISE OF ENFORCEMENT DISCRETION
This guys have been jumping back and forth between the two stage and three stage Safety Relief Valves like Mexican jumping beans. I believe this is the newest operational period with all three stage SRV. With the 2 stage it was corrosion bonding causing the setpoint drift, now with the 3 stage it is:  "The licensee determined that the abutment gap closed pre-maturely most likely due to manufacturing tolerances". I think all this is unreliable small parts mechanical tolerances and metallurgy tolerances. Basically the design is too delicate, you look at it the wrong way the set pressure drifts out of specs. I don't think the technicians are skilled or trained adequately to service the SRVS.

The three stage was put into the plant to fix the setpoint drift, now they got this new magical "abutment gap" setpoint drift problem in the 3 stage   problem they couldn't see in design testing.  They always find some explanation for the drift problem without fixing it right the last time.
(CLOSED) LER 05000321/2016-004-00 Safety Relief Valves As Found Setting Resulted in Not Meeting Technical Specifications
a. Inspection Scope
The inspectors reviewed this LER for potential performance deficiencies and/or violations of regulatory requirements. Additionally, discussions were held with licensee
staff members to understand the details surrounding this issue. This condition was documented in the licensee’s corrective action program as CR 10204045. 
b. Findings
Description: During the February 2016 Unit 1 refueling outage, all
eleven 3-stage safety
Inspecting and testing all eleven 3 stage in a outage is a sign of weakness. They don't have complete confidence in the design. Some plants won't trust the 3 stage design based on the Pilgrim problem.  
relief valves (SRVs) were removed and replaced. The SRVs were Target Rock model 0867F, a 3-stage valve design which was in its first use. This design was adopted as a
corrective action to address corrosion bonding experienced by 2-stage SRV model 7687F valves which were previously in use at Hatch. "As-found" test results indicated two of the eleven SRVs had experienced a setpoint drift during the previous operating cycle which resulted in their failure to meet the Technical Specification (TS) opening setpoint pressure as required by TS Surveillance Requirement (SR) 3.4.3.1. The SRV pilot valves were disassembled and inspected while investigating the reason for the drift.
For the 3-stage design, the pilot disc seating stresses should increase proportionally as reactor pressure increases to where a mechanical gap within the valve stem
mechanism, referred to as the “abutment gap,” is closed. Additional pressure increases will cause the valve stem mechanism to reduce the disc seat pressure until the valve eventually opens. The licensee determined that the abutment gap closed pre-maturely most likely due to manufacturing tolerances. The cause of the setpoint drift could not be attributed to any known preventive maintenance requirement or operating experience because of the limited operating history of this specific valve model. Additionally, there
were no symptoms available to operators or maintenance personnel to indicate the potential for the set point drift prior to post-service testing. 
Enforcement: Hatch Unit 1 TS limiting condition for operation 3.4.3, “Safety/Relief Valves,” required 10 of 11 SRVs be operable in MODES 1, 2 and 3. With two or more
SRVs inoperable, the required TS action must be taken by the applicable completion time. Contrary to the above, Unit 1 operated from the initiation of the degraded condition
until February 8, 2016, with two SRVs inoperable. The inspectors concluded that the violation would normally be characterized as a Severity Level IV violation because it was of very low safety significance (Green). However, the NRC is exercising enforcement discretion (EA-16-158) in accordance with Section 2.2.4.d of the Enforcement Policy because the violation was not associated with a licensee performance deficiency. This issue was documented in the licensee’s corrective action program as CR10204045.

Junk facility Watts Bar New Inspection Report: Site Spinning Wildly Out Of the Control Of The NRC

Not putting in the required paperwork to the NRC indicates the site is spinning out of control from the NRC.

This is not the normal new plant start-up process in Unit 2...it indicates widespread poor quality issues with all the components.
wildly
IR 05000390/2016-002; 05000391/2016-002; April 1, 2016 – June 30, 2016; Watts Bar, Units 1 and 2; Triennial Fire Protection Inspection, Operability Evaluations, Surveillance Testing, Problem Identification and Resolution, Event Follow-up. 
Summary of Plant Status 
Unit 1 started the reporting period at 100 percent rated thermal power and remained there until March 22, 2016, when the reactor tripped due to a main turbine trip caused by a governor valve circuit card failure. Unit 1 returned to 100 percent rated thermal power on March 28, 2016, and remained there until June 11, 2016, when power reductions were necessary to maintain main low pressure turbine #3 back pressure limits during warmer weather. Unit 1 operated between
89 and 97 percent power, as necessary to maintain main turbine backpressure limits, until June 25, 2016, when power was reduced due to turbine building sump overflowing, resulting from turbine building sump pump failures. The rising water level approached the running unit 1 #3 high pressure heater drain tank pumps. The licensee decided to secure the #3 high pressure heater drain pumps and, as a result, lowered unit 1 power. Power reduction continued to 60 percent on June 27, 2016, then increased over the next three days to 79 percent by the end of the reporting period.
Unit 2 started the reporting period in mode 3 and remained there until April 2, 2016, when it entered mode 4 for repairs to leaking safety injection check valves. The unit re-entered mode 3 on April 8, 2016, where it remained until April 17, 2016, when it re-entered mode 4 due to failure of the turbine-driven auxiliary feedwater pump (TDAFW) to meet mode 3 operability requirements. The unit re-entered mode 3 on May 1, 2016, where it remained until May 18, 2016, when it re-entered mode 4 for repairs to the solid state protection system. The unit reentered mode 3 on May 20, 2016. The unit then entered mode 2 on May 23, 2016, and mode 1 on May 25, 2016, where it remained until May 28, 2016, when it re-entered mode 3 due to abnormal indications of foreign material in the main turbine when it was rolled at low speed for the first time. The unit re-entered mode 2 and mode 1 on May 31, 2016. The unit remained in mode 1 until June 5, 2016, when the #1 turbine governor valve failed full open, causing an automatic reactor trip and safety injection. The unit re-entered mode 2 and mode 1 on June 8, 2016. The unit remained in mode 1 until an automatic reactor trip caused by steam generator low level occurred on June 20, 2016. The reactor trip was the result of a secondary transient caused by the loss of the running main feedwater pump. The unit re-entered mode 2 on June 23, 2016, and re-entered mode 1 on June 24, 2016. The unit re-entered mode 2 on June 26, 2016, due to a high pressure steam leak and subsequent lifting of two main steam safety valves
on the #4 steam generator. The unit re-entered mode 3 on June 26, 2016, to repair the steam leak and the safety valves. The unit remained in mode 3 through the end of the reporting period. 
*The report covered a three-month period of inspection by the resident and regional inspectors. Ten NRC-identified and self-revealed findings were identified. 
NRC-Identified Findings and Self-Revealed Findings 
SL IV. The NRC identified a Severity Level (SL) IV non-cited violation (NCV) of 10 Code of Federal Regulations (CFR) 50.73(a)(2)(i)(B) for the licensee's failure to notify the NRC that the technical specification (TS) limiting condition for operation (LCO) 3.5.2 required action and completion time were not met when the 1B-B centrifugal charging pump (CCP) was inoperable due to an inoperable room cooler. Subsequently, the licensee submitted LER 2016-006-00 for this event on June 30, 2016. This issue was placed in the licensee’s corrective action program (CAP) as CR 1165380.
Since the failure to submit an event report within the time requirements may impact the ability of the NRC to perform its regulatory oversight function, this performance deficiency was dispositioned under traditional enforcement and the violation was assessed using Section 2.2.4 of the NRC’s Enforcement Policy. Using the example listed in Section 6.9.d.9, “A licensee fails to make report required by 10 CFR 50.73,” the issue was determined to be a SL IV violation. In accordance with IMC 0612, “Power Reactor Inspection Reports,” dated May 6, 2016, traditional enforcement violations are not assessed for cross-cutting aspects. (Section 1R15)
SL IV: The NRC identified a SL IV NCV of 10 CFR 50.73(a)(2)(i)(B) for the licensee's failure notify the NRC that the TS LCO 3.1.8 required action and completion time were not met when the analog rod position indication (ARPI) and the demand position indication system were not operable. Subsequently, the licensee submitted LER 2016-007-00 for this issue on June 20, 2016. This violation was placed in the licensee’s corrective action program as CR 1163150.
Since the failure to submit an event report within the time requirements may impact the ability of the NRC to perform its regulatory oversight function, this performance deficiency was dispositioned under traditional enforcement and the violation was assessed using Section 2.2.4 of the NRC’s Enforcement Policy. Using the example listed in Section 6.9.d.9, “A licensee fails to make report required by 10 CFR 50.73,” the issue was determined to be a SL IV violation. In accordance with IMC 0612, “Power Reactor Inspection Reports,” dated May 6, 2016, traditional enforcement violations are not assessed for cross-cutting aspects. (Section 4OA3.6)
SL IV. The NRC identified a SL IV NCV of 10 CFR 50.73(a)(2)(i)(B) for the licensee's failure notify the NRC that the TS LCO 3.6.3 required action and completion time were not met for an inoperable emergency raw cooling water (ERCW) containment isolation valve. Subsequently, the licensee submitted LER 2016-009-00 for this issue on July 15, 2016. This issue was placed in the licensee’s corrective action program as CR 1174000.
Since the failure to submit an event report within the time requirements may impact the ability of the NRC to perform its regulatory oversight function, this performance deficiency was dispositioned under traditional enforcement and the violation was assessed using Section 2.2.4 of the NRC’s Enforcement Policy. Using the example listed in Section 6.9.d.9, “A licensee fails to make report required by 10 CFR 50.73,” the issue was determined to be a SL IV violation. In accordance with IMC 0612, “Power Reactor Inspection Reports,” dated May 6, 2016, traditional enforcement violations are not assessed for cross-cutting aspects. (Section 4OA2.3)
SL IV. The NRC identified a SL IV NCV of 10 CFR 50.73(a)(2)(i)(B) for the
licensee's failure to report, within 60 days of discovery, a condition which was
prohibited by the plant’s TS associated with recent performances of TS surveillance requirement (SR) 3.5.2.3 for verification that emergency core cooling system (ECCS) piping is full of water. Subsequently, the licensee submitted LER 2016-003-00 for this issue on May 10, 2016. This violation was placed in the licensee’s corrective action program as CR 1166564.
Since the failure to submit an event report within the time requirements may impact the ability of the NRC to perform its regulatory oversight function, this performance deficiency was dispositioned under traditional enforcement and the violation was assessed using Section 2.2.4 of the NRC’s Enforcement Policy. Using the examplelisted in Section 6.9.d.9, “A licensee fails to make report required by 10 CFR 50.73,” the issue was determined to be a SL IV violation. In accordance with IMC 0612, “Power Reactor Inspection Reports,” dated May 6, 2016, traditional enforcement violations are not assessed for cross-cutting aspects. (4OA3.4)
SL IV. The NRC identified a SL IV NCV of 10 CFR 50, Appendix B, Criterion V,
“Instructions, Procedures, and Drawings,” at Watts Bar Unit 2 for the licensee’s
failure to follow procedure OPDP-8, Operability Determination Process and Limiting Condition for Operation Tracking, Revision 22. Specifically, the 2A-A motor-driven auxiliary feedwater pump (MDAFW) was potentially inoperable in mode 3 due to inadequate compensatory measures that were being controlled outside of the operability process. The issue was corrected and the pump returned to operable status on April 19, 2016. The issue was entered into the licensee’s corrective action program as CR 1163431.
The performance deficiency was more than minor because it represented an
improper or uncontrolled work practice that could impact quality or safety, involving safety-related SSCs. Specifically, failure to appropriately use the operability process when measures must be established to compensate for degraded or nonconforming conditions can lead to SSC inoperability. As described in IMC 2517, the significance of this issue was determined using traditional enforcement, because the cornerstone associated with this finding was not being assessed by the reactor oversight process (ROP). The inspectors determined this finding to be of very low safety significance, SL IV because it represented a failure to meet a regulatory requirement, specifically a quality assurance (QA) criteria to follow quality-related procedures, which had
more than minor safety significance. The finding was assigned a cross-cutting
aspect of Work Management in the Human Performance area because the minor
maintenance work order created to compensate for the oil loss from the 2A-A
MDAFW pump was never reviewed by operations, which could have identified the out of process error. [H.5]. (Section 1R15)
SL IV. The NRC identified a SL IV NCV of 10 CFR 50, Appendix B, Criterion V,
“Instructions, Procedures, and Drawings,” at Watts Bar Unit 2 for the licensee’s
failure to follow the surveillance test program procedure by making adjustments to the turbine-driven auxiliary feedwater (TDAFW) pump control system during the performance of a surveillance instruction. The licensee reperformed the surveillance instruction with satisfactory results. The issue was entered into the licensee’s corrective action program as CR 1167102.
The performance deficiency was more than minor because making adjustments to the TDAFW pump control system during the performance of a surveillance
instruction could invalidate the test and result in the TDAFW pump being
inappropriately declared operable. As described in IMC 2517, the significance of this issue was determined using traditional enforcement, because the cornerstone associated with this finding was not being assessed by the reactor oversight process (ROP). The inspectors determined this finding to be of very low safety significance, SL IV, because it represented a failure to meet a regulatory requirement, specifically a QA criteria to follow quality-related procedures, which had more than minor safety significance. The finding was assigned a cross-cutting aspect of Conservative Bias in the Human Performance area because numerous individuals were aware the speed adjustment had been made while completing the surveillance instruction but did not question the appropriateness of that adjustment until prompted by NRC inspectors. [H.14] (Section 1R22)
SL IV. A self-revealed Severity Level (SL) IV non-cited violation (NCV) of 10 Code of Federal Regulations (CFR) 50, Appendix B, Criterion V, “Instructions, Procedures, and Drawings,” was identified at Watts Bar Unit 2 for the licensee’s failure to follow procedure 0-MI-1.003, Disassembly, Inspection, and Reassembly of Auxiliary Feedwater Pump Turbine. Specifically, the valve stem spring coil gap was not set in accordance with procedure, causing the turbine-driven auxiliary feedwater (TDAFW) pump to trip on electrical overspeed when the level control valves (LCVs) were closed. This issue was corrected on May 30, 2016, when the proper spring coil gap was set and verified and the post maintenance test was performed satisfactorily. The issue was entered into the licensee’s corrective action program as CR 1175968. 
The performance deficiency was more than minor because it represented an
improper or uncontrolled work practice that could impact quality or safety involving safety-related structures, systems, and components (SSCs). The finding was a SL IV violation because it represented a failure to meet a regulatory requirement, specifically a quality assurance (QA) criteria to follow quality-related procedures, which had more than minor safety significance. The finding was assigned a crosscutting aspect of resources in the Human Performance area because the licensee failed to ensure that personnel, equipment, procedures, and other resources are available and adequate to support nuclear safety. Specifically, the procedure that set the coil spring gap lacked sufficient detail and rigor to ensure that the coil gap would be set appropriately by the technicians. [H.1] (4OA3.1)

Junk Plant Pilgrim: Ocean Temp too Hot Now (Again)

update 8/17

So the Ocean hot water will intensify and wane during the tide cycle, but slowly trend up. Pilgrim has seen the ocean temperature slowly trend up for weeks and they would have predicted it would lead to a shutdown or down power. The ocean temps will continue to trend up until the middle of September. I suspect we will see them in repeated shutdowns and down powers for another month or more. It will beat the hell out of the plant. This environment is rich with screw-ups and breaking equipment, it is highly likely they will get a plant trip or other accident.

Update:
Even with 80 degrees service water temp update, still think Millstone might have to come down in power. So there has been a tremendous drought this summer. All the fresh water going into the Sound has been drastically reduced through the drought. How will this effect the Sound's temps? 
Why won't Seabrook have this problem? They grab their cooling seawater through a under ocean tunnel many miles out to sea. 
I thought they upped their service water temperature high limit in a License Amendment Request (LAR). This seems to be a really strong high temperature event.  They are sitting at 50% last night, are they back washing the circ water system.

When did it last happen. This happens in the later half of Aug...


This has occured in Aug 2015 and July 2013.

Facility: PILGRIM
Region: 1 State: MA
Unit: [1] [ ] [ ]
RX Type: [1] GE-3
NRC Notified By: KENNETH GOODALL
HQ OPS Officer: VINCE KLCO
Notification Date: 08/15/2016
Notification Time: 17:48 [ET]
Event Date: 08/15/2016
Event Time: 15:52 [EDT]
Last Update Date: 08/15/2016
Emergency Class: NON EMERGENCY
10 CFR Section:
50.72(b)(3)(v)(B) - POT RHR INOP
50.72(b)(3)(v)(D) - ACCIDENT MITIGATION
Person (Organization):
DON JACKSON (R1DO)

UnitSCRAM CodeRX CRITInitial PWRInitial RX ModeCurrent PWRCurrent RX Mode
1NY70Power Operation62Power Operation
Event Text
SALT SERVICE WATER SYSTEM DECLARED INOPERABLE

"On Monday, August 15, 2016 at 1552 [EDT], with the reactor at [about] 70 percent core thermal power (CTP), Pilgrim Nuclear Power Station (PNPS) entered a 24-hour shutdown Limiting Condition for Operation Action Statement (LCO-AS) for Salt Service Water (SSW) inlet temperature exceeding the Technical Specification (TS) limit in TS 3.5.B.4. The LCO-AS was subsequently exited at 1651 hours when the temperature of SSW trended to below the TS limit.

"Under certain design conditions, the SSW system is required to provide cooling water to various heat exchangers such as the Reactor Building Closed Cooling Water (RBCCW) and Turbine Building Closed Cooling Water (TBCCW) systems. When the inlet temperature to these supplied loads exceeds the 75 degrees F limit established in the TS, the SSW system is conservatively declared inoperable until the temperature trends below this value. This condition existed for approximately 60 minutes.

"The SSW temperature is being closely monitored and trended on a continuous basis.

"This event has no impact on the health and safety of the public.

"The licensee has notified the NRC Senior Resident Inspector.

"This notification is being made in accordance with 10 CFR 50.72(b)(3)(v)(B) and 10 CFR 50.72(b)(3)(v)(D) due to an event or condition that could have prevented fulfillment of a safety function.

"The licensee will be notifying the Commonwealth of Massachusetts Emergency Management Agency."

Monday, August 15, 2016

Junk Nuke Company Entergy: 86% of Stocks Owned By Institutional Investers

Is this a sign of weakness or strength?
Entergy Corporation (NYSE:ETR)’s stock has been a favorite of “smart money” aka institutions, as of late.  Institutions are currently holders of 86.20% of the shares.  On the other hand, company insiders are holding 0.10%.  Entergy Corporation’s stock price currently sits at $79.25.

Junk Plant Watts Bar 1 With Sequoyah's LP Turbine UP To 95% Power

Highest power all summer?

Watts Bar 195
Watts Bar 20

Junk Plant Watts Bar 1 Pre-Operation Testing


Power ReactorEvent Number: 52177
Facility: WATTS BAR
Region: 2 State: TN
Unit: [ ] [2] [ ]
RX Type: [1] W-4-LP,[2] W-4-LP
NRC Notified By: MATTHEW MILLER
HQ OPS Officer: DONALD NORWOOD
Notification Date: 08/13/2016
Notification Time: 08:51 [ET]
Event Date: 08/13/2016
Event Time: 03:36 [EDT]
Last Update Date: 08/13/2016
Emergency Class: NON EMERGENCY
10 CFR Section:
50.72(b)(3)(iv)(A) - VALID SPECIF SYS ACTUATION
Person (Organization):
SCOTT SHAEFFER (R2DO)

UnitSCRAM CodeRX CRITInitial PWRInitial RX ModeCurrent PWRCurrent RX Mode
2NN0Hot Standby0Hot Standby
Event Text
AUTOMATIC START OF TURBINE DRIVEN AUXILIARY FEED WATER PUMP

"On August 13, 2016 at 0330 EDT, Watts Bar Nuclear Plant Unit 2 (WBN2) was being stabilized following a pre-planned reactor trip. Both motor driven auxiliary feed water pumps and the turbine driven auxiliary feed water pump (TDAFW pump) were in operation maintaining steam generator water level 6 - 50 percent in accordance with the Reactor Trip Response Procedure.

"At 0333 EDT the TDAFW pump was secured by procedure and steam generator water level lowered to the Low Low Alarm setpoint (17 percent). The trip time delay
Testing the TDAFW pump.
at 0 percent power is three (3) minutes. At 0336 EDT, the TDAFW pump automatically started with steam generator water levels less than the Low Low alarm setpoint (lowest level reached was 15 percent).

"Steam generator water level was restored to the normal shutdown control band (38 percent).

"Unit 1 remains in Mode 1 at 85 percent.

"Unit 2 is stable in Mode 3 with normal shutdown power alignment. The reactor coolant system is being cooled down to 400 degrees F for a planned maintenance period, with decay heat removal via the Main Condenser Steam dumps and the AFW system.

"This event is being reported pursuant to 10 CFR 50.72(b)(3)(iv)(A).

"TVA has notified the NRC Resident Inspector."

Friday, August 12, 2016

Junk Watts Bar 1 Hasn’t Exceeded 90% Power Since End Of May 2016

Update according to the NRC
Watts Bar has troubles with their low pressure turbine. Bet you it was blading erosion. So they swapped out their LP turbine with Sequoyah's LP turbine. I asked if it had a LAR on it. Resident said its not safety related...I'd disagreed with him. Basically the Sequoyah LP turbine is poorly designed for the Watts Bar Unit 1 duty. The Sequoyah LP turbine doesn't draw sufficient energy out of the steam...too much core energy (thru the SG) is overloading the main condensers. Basically not enough circ water leading to the high condenser back pressure. The plant now has a very poor mile per gallon rate.  
He wondered how I came upon the information. Told him I got it from the daily power history. The NRC queried me concerning this wondering if a employee got me to pose the question to the NRC.
The top 10% power is the gravy money. These guys definitely hasn’t been profitable since May 2016.
Having condenser back pressure issues is code words for the plant isn’t designed for the climate. It usually means the heat sink- the stream or pond- is too hot for the condenser and plant design.
If they having problems keeping unit 1 up at 100% then I have little hope of they getting unit 2 into production.
These are the guys that intimidate their employees from making safety concerns.  
Hmm, the unit didn't have these issue last year. It seems like component problems...