Can it be more delicious with our ongoing crazy political season...the Trump Phenomena.
I think the Trump spectacle is washing out "House Of Cards".
As it stands now, I am voting for Trump...
OMG: the President Underwood been shot and needs a new liver.
Whistleblowing can be used as a potent creative tool to help your bureaucracy evolve towards a more enlightened organization. Phone: 1-603-209-4206 steamshovel2002@yahoo.com Note: I constantly update my articles. Comments at the bottom of the article are always welcome!!! Mike Mulligan, Hinsdale, NH
Friday, March 04, 2016
Thursday, March 03, 2016
Junk Plant Seabroook Had Problems Controlling Steam Generator Level
Power Reactor Event Number: 51765 Facility: SEABROOK
Region: 1 State: NH
Unit: [1] [ ] [ ]
RX Type: [1] W-4-LP
NRC Notified By: MIKE TAYLOR
HQ OPS Officer: STEVEN VITTONotification Date: 03/02/2016
Notification Time: 18:13 [ET]
Event Date: 03/02/2016
Event Time: 13:12 [EST]
Last Update Date: 03/02/2016Emergency Class: NON EMERGENCY
10 CFR Section:
50.72(b)(3)(iv)(A) - VALID SPECIF SYS ACTUATIONPerson (Organization):
WILLIAM COOK (R1DO)Event Text
Unit SCRAM Code RX CRIT Initial PWR Initial RX Mode Current PWR Current RX Mode 1 N N 0 Hot Standby 0 Hot Standby
VALID ACTUATION OF EMERGENCY FEEDWATER
"On 3/2/2016, [at] 1312 hours EST, while in the process of a plant cooldown, a valid actuation of the emergency feedwater system (EFW) occurred when B steam generator levels were reduced to 20 [percent]. The lowering level was a result of the unanticipated tripping of the start up feed pump on low condensate storage level while it was the feed source to the steam generators. The start up feed pump was restarted and feed flow had been restored when the actuation took place. The EFW flow was secured per procedure and the start up feed pump remains the feed source to the steam generators.
"This is reportable under 50.72(b)(3)(iv)(A).
"The licensee notified the NRC Resident Inspector."
Drama Queen Junk Plant River Bend Increased Power from 1% to 4% in 24 Hours?
3/8
There you go: 100%
Update 3/7
River Bend is at 84%. This is ridicules with the plant at 3% Thursday night and they are only at 84% on Monday. Can't wait for this painfully slow march to 100% power. Any bets when 100% power is reached? This guys shouldn't even be running.
Saturday 40%
Sunday 93% (more like it)
Then a big down power today to 84% power.
Update 3/4
In another 24 hours last night, River Bend power is at 3%. They have gone down 1% in 24 hours. Did it scram a second time? I wish power level was a gage I could touch, because I'd tap it on the side wondering if the needle is stuck.
Certainly what they are doing is safe, but not preparing the plant for start-up raises the question if the competent to safely operate the plant in the future.
There is massive budget cutting going on in the future. The NEI want to cut 35% from all plants. Is this behavior at River Bend going to be normalized at all USA plants. Is this our future?
So the worst plant in the nation ANO, today there are up to 100%. Did the designers of the plant consider a plant could hang at under 5 % power for days, or did was the plant designed where they could hangout at low power operations for days and weeks. I would think the safest would be to raise up from low power as fast as you can.
Humm, recently ANO 2 and River Bend started up. ANO is at about 20% in 24 hours, while River Bend is at 4% in 24 hours.
Then River Bend shutdown subsequent to the special inspection over more unreliable safety breakers and extremely poor plant engineering. We discovered this yesterday thought a NRC mistake. The NRC disclosed through a mistake, the agency released highly confidential and a competitive information. It just wasn't one plant, the agency released confidential information nuclear industry wide. I think the NRC pressured River Bend to shutdown!
There you go: 100%
Update 3/7
River Bend is at 84%. This is ridicules with the plant at 3% Thursday night and they are only at 84% on Monday. Can't wait for this painfully slow march to 100% power. Any bets when 100% power is reached? This guys shouldn't even be running.
Saturday 40%
Sunday 93% (more like it)
Then a big down power today to 84% power.
Update 3/4
In another 24 hours last night, River Bend power is at 3%. They have gone down 1% in 24 hours. Did it scram a second time? I wish power level was a gage I could touch, because I'd tap it on the side wondering if the needle is stuck.
Certainly what they are doing is safe, but not preparing the plant for start-up raises the question if the competent to safely operate the plant in the future.
There is massive budget cutting going on in the future. The NEI want to cut 35% from all plants. Is this behavior at River Bend going to be normalized at all USA plants. Is this our future?
So the worst plant in the nation ANO, today there are up to 100%. Did the designers of the plant consider a plant could hang at under 5 % power for days, or did was the plant designed where they could hangout at low power operations for days and weeks. I would think the safest would be to raise up from low power as fast as you can.
Humm, recently ANO 2 and River Bend started up. ANO is at about 20% in 24 hours, while River Bend is at 4% in 24 hours.
Recap: I initiated two special inspection at River Bend last
year. The second special inspection was over unreliable safety breakers. It
took about a year for the lump to pass through the snake. The results came out in
the last few weeks and it was damming.
Then River Bend shutdown subsequent to the special inspection over more unreliable safety breakers and extremely poor plant engineering. We discovered this yesterday thought a NRC mistake. The NRC disclosed through a mistake, the agency released highly confidential and a competitive information. It just wasn't one plant, the agency released confidential information nuclear industry wide. I think the NRC pressured River Bend to shutdown!
It was a very expensive shutdown and it lasted in excess of 10
days. Can things get worst?
At the end of 2/1, the plant was at 1%
At the end of 2/2, the plant was at 4% power.
It would be reckless for any plant to stay at these low
power levels for 24 hours.
They must have scrammed or shutdown during 2/2/2016.
Does the NRC got Entergy rattled???
Wednesday, March 02, 2016
Junk Plant River Bend Shuts Down Over Junk Safety Breakers.
See new special inspection results?
Why didn't my special inspection early last year fix River Bend? A totally ineffective NRC.
shutdown 2/17
Why didn't my special inspection early last year fix River Bend? A totally ineffective NRC.
shutdown 2/17
Junk Plant Arkansas 2 Shutdowns Over Junk Leaking Check Valves
shutdown began 2/23?
Worst nuclear facility in the USA.
Giant NRC inspections began 1/27?
Did the army of NRC inspectors on site provoke the shutdown?
Worst nuclear facility in the USA.
Giant NRC inspections began 1/27?
Did the army of NRC inspectors on site provoke the shutdown?
Junk Plant Seabrook Trips On Bum Transmission Work
Update 3/3
So Seabrook tripped yesterday and why isn't this reported on?
So it happened last night at 02:52.
Check out how sensitive our grid is to the lost of Seabrook. It tripped around 3 am. It is getting doubtful the transmission work caused the trip. NEISO electricity has been pretty inexpensive this mild winter. This has made a lot of long term contracts bankrupt?
Equipment problem shuts down nuke plant
SEABROOK — An equipment malfunction triggered the safe shutdown of NextEra Energy Seabrook nuclear power plant early yesterday morning, according to the Nuclear Regulatory Commission.
According to NRC Region I spokesman Neil Sheehan, at 2:53 a.m. Wednesday, Seabrook Station plant experienced an unplanned shutdown because a turbine tripped, or went offline.
“That triggered, as expected, a reactor shutdown,” he said. “The shutdown was uncomplicated. Turbines are considered to be the secondary, or non-nuclear, side of the facility.”
Sheehan said the NRC’s resident inspectors assigned full-time to Seabrook Station were promptly notified about the shutdown.
“The senior resident inspector responded to the plant, reviewed the sequence of events, performed visual inspections, and discussed the shutdown with key plant personnel.” Sheehan said. “The inspectors will continue to follow up on the company’s assessments of what occurred, (as well as) any repairs and planning for the restart of the unit.”
The NRC monitors all happenings at the nation’s nuclear power plants, even when they are not related to the nuclear side of the plant.
“We care about a turbine trip because it initiated the reactor trip,” Sheehan said. “And any time that occurs, you’re putting unnecessary stress on the (power plant’s) operators.”
NextEra Energy Seabrook spokesman Alan Griffith confirmed the plant’s shutdown. Griffith said the plant is designed to shut down when such issues occur to ensure safety, and it functioned appropriately Wednesday morning.
As of yesterday afternoon, Griffith said, the exact cause of the equipment issue that triggered the shutdown had not yet been determined.
“As safety is our highest priority,” Griffith said, “a complete and thorough analysis is being conducted on the exact cause of the shutdown. While there is no timetable, the plant will be returned to full power once repairs are completed.”
Sheehan said along with plant personnel, the NRC’s resident inspectors will be involved in all aspects of the assessment.
So Seabrook tripped yesterday and why isn't this reported on?
So it happened last night at 02:52.
Check out how sensitive our grid is to the lost of Seabrook. It tripped around 3 am. It is getting doubtful the transmission work caused the trip. NEISO electricity has been pretty inexpensive this mild winter. This has made a lot of long term contracts bankrupt?
Power Reactor Event Number: 51762 Facility: SEABROOK
Region: 1 State: NH
Unit: [1] [ ] [ ]
RX Type: [1] W-4-LP
NRC Notified By: ANDY CARAMIHALIS
HQ OPS Officer: MARK ABRAMOVITZNotification Date: 03/02/2016
Notification Time: 04:27 [ET]
Event Date: 03/02/2016
Event Time: 02:53 [EST]
Last Update Date: 03/02/2016Emergency Class: NON EMERGENCY
10 CFR Section:
50.72(b)(2)(iv)(B) - RPS ACTUATION - CRITICAL
50.72(b)(3)(iv)(A) - VALID SPECIF SYS ACTUATIONPerson (Organization):
WILLIAM COOK (R1DO)
Event Text
Unit SCRAM Code RX CRIT Initial PWR Initial RX Mode Current PWR Current RX Mode 1 A/R Y 100 Power Operation 0 Hot Standby
TURBINE TRIP CAUSING A REACTOR TRIP
"The turbine tripped for an unknown cause followed by a reactor trip. All systems are functioning as designed. Operators have transitioned out of the EOP [Emergency Operating Procedure] network into normal operating procedures. The plant is stable in mode 3."
All control rods fully inserted during the trip and no safety or relief valves lifted. The plant is in its normal shutdown electrical lineup. Emergency Feedwater actuation occurred to restore steam generator levels. The plant expects to make a press release.
The licensee notified the NRC Resident Inspector.
NRC Makes Huge Mistake Publishing Comments in Power Reactor Status Report
(Bet you the leap year was implicated with this???)The NRC made a rare mistake yesterday. The published the comments on the power reactor status report. Or did they do this on purpose. They usually wait 30 to 60 days for competitive reason to publish the comments.
My comments about this:
Indian Point 2: The coast down to refueling for the past month has been highly erratic.
Seabrook: Did the maintenence on the 345 line or its downpower cause the scram?
Pilgrim: they explain the computer upgrade has caused its downpower to 98%.
Fermi 2 junk: runback on junk heater drain parts.
Arkansan 2 shutdown: junk check valve parts.
*Grand Gulf: my bad, in refueling outage?
Junk Plant River Bend: problems with breakers. Did the NRC shut them down?
Power Reactor Status Report for March 1, 2016
Unit Power Down Reason or Comment Change in report (*) Number of Scrams (#) Beaver Valley 1 100 * Beaver Valley 2 100 * Calvert Cliffs 1 0 02/15/2016 REFUELING OUTAGE * Calvert Cliffs 2 100 * FitzPatrick 100 Ginna 100 Hope Creek 1 100 * Indian Point 2 81 COASTDOWN TO REFUELING OUTAGE * Indian Point 3 100 Limerick 1 94 COASTDOWN TO REFUELING OUTAGE * Limerick 2 100 Millstone 2 100 Millstone 3 100 Nine Mile Point 1 100 Nine Mile Point 2 100 Oyster Creek 100 Peach Bottom 2 100 100 MVAR RESTRICTION DUE TO TURBINE BEARING VIBRATIONS Peach Bottom 3 100 Pilgrim 1 98 HOLDING POWER FOR PROCESS COMPUTER UPGRADE * Salem 1 100 * Salem 2 100 * Seabrook 1 100 DOWNPOWER CONTINGENCY DURING 345 kV LINE MAINTENANCE Susquehanna 1 89 COASTDOWN TO REFUELING OUTAGE * Susquehanna 2 100 * Three Mile Island 1 100 * Region 2
Unit Power Down Reason or Comment Change in report (*) Number of Scrams (#) Browns Ferry 1 100 Browns Ferry 2 100 Browns Ferry 3 0 02/19/2016 REFUELING OUTAGE Brunswick 1 0 02/26/2016 REFUELING OUTAGE * Brunswick 2 100 Catawba 1 100 Catawba 2 100 Farley 1 100 Farley 2 100 Harris 1 100 Hatch 1 0 02/07/2016 REFUELING OUTAGE Hatch 2 100 McGuire 1 100 McGuire 2 100 North Anna 1 100 North Anna 2 89 COASTDOWN TO REFUELING OUTAGE Oconee 1 100 Oconee 2 100 Oconee 3 100 Robinson 2 100 Saint Lucie 1 100 Saint Lucie 2 100 Sequoyah 1 100 Sequoyah 2 100 Summer 100 Surry 1 100 Surry 2 100 Turkey Point 3 100 Turkey Point 4 100 Vogtle 1 100 Vogtle 2 100 Watts Bar 1 100 Watts Bar 2 0 Region 3
Unit Power Down Reason or Comment Change in report (*) Number of Scrams (#) Braidwood 1 100 Braidwood 2 100 Byron 1 100 Byron 2 100 Clinton 99 100% ELECTRICAL CAPABILITY D.C. Cook 1 100 * D.C. Cook 2 100 * Davis-Besse 85 COASTDOWN TO REFUELING OUTAGE * Dresden 2 100 Dresden 3 100 Duane Arnold 100 Fermi 2 58 RECEIVED POWER RUNBACK FROM LOSS OF HEATER DRAIN FLOW * La Salle 1 0 02/14/2016 REFUELING OUTAGE La Salle 2 100 Monticello 100 Palisades 100 Perry 1 100 * Point Beach 1 100 Point Beach 2 100 Prairie Island 1 100 Prairie Island 2 100 Quad Cities 1 100 * Quad Cities 2 91 COASTDOWN TO REFUELING OUTAGE * Region 4
Unit Power Down Reason or Comment Change in report (*) Number of Scrams (#) Arkansas Nuclear 1 100 Arkansas Nuclear 2 0 02/23/2016 MAINTENANCE OUTAGE TO REPAIR CHECK VALVE LEAKAGE Callaway 100 Columbia Generating Station 100 Comanche Peak 1 100 Comanche Peak 2 100 Cooper 100 Diablo Canyon 1 100 Diablo Canyon 2 100 Fort Calhoun 100 Grand Gulf 1 0 02/19/2016 REFUELING OUTAGE Palo Verde 1 100 Palo Verde 2 100 Palo Verde 3 100 River Bend 1 0 02/17/2016 FORCED OUTAGE - BREAKER MAINTENANCE South Texas 1 100 South Texas 2 100 Waterford 3 100 Wolf Creek 1 100
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