Wednesday, January 27, 2016

The Brooks Brother Suits Wants Budget's Slashed 30% at Nuclear Plants

Republished from 12/8/2015

Update 12/9

Another example of terrible waste:  "Indian Point's other reactor, Unit 3, is now running at 100 percent, but has been shut down for two scheduled and four unscheduled outages in 2015."

As one insider says:
"Over paid execs who are just sending gold bars to their headquarters" 
 
In other words, the NEI and electric utilities finally see themselves in a severe death spiral. It is time to begin hacking and slashing budgets in order to survive. If these guys were really fiducial professional, they would already be funding these plants without any extra financial waste or slack. It would already be going back to the stockholders.   

Did the nuclear utilities order the NEI to pressure plants to cut cost 30% across the board?

Not a worry a bit about this ultra-high capacity factor degrading safety. How are they going assure us no safety will be cut.

I got the first big cut, wind down the NEI. This is only basically a no work or easy work nuclear industry welfare.  

I am glad they are finally seeing the magnitude of their financial problems.

The NRC should send out a mandatory anonymous questionnaires to every technical employee and management in the industry. Ask them if they now are adequately resourced? Will you be able to safely operate with budget cuts of upwards to 30%?

List the 3 top weak links with severe budgets cuts?
I got another great ideal, anyone making over $150,000 a year should begin with a 30% reduction in salary and the higher paid Brooks Brother suits should take a much bigger percentage hit as a symbol of the crisis.
 
You just got to know the rank and file guys who really run the plant, the Brooks Brother suits are going to be focusing their wrath at cutting the wages and benefits at the bottom half.
When A Strike is a Possibility at a Plant
You notice how Entergy took care of their Union and strike problem at FitzPatrick...they are just going to shut them down.     
US nuclear power fleet aims to cut costs by 30%: industry official 
Washington (Platts)--8 Dec 2015 517 pm EST/2217 GMT
  • You mean the electric utilities have demanded this goal.
The US nuclear power industry has launched a wide-ranging initiative with the goal of cutting its electricity production costs by 30% by 2018, an industry official said Tuesday. 
Maria Korsnick, chief operating officer of the Nuclear Energy Institute, said during a media briefing at the National Press Club in Washington that despite record-high capacity factors achieved by US nuclear power plants in recent years, the average production cost of the electricity they generate rose significantly from 2002 to 2014. 
  • “despite record-high capacity factors” for last 12 years.  
  • "total electric generating costs at US nuclear plants have increased 28% in twelve years” despite record capacity factor. 
NEI said in a statement Tuesday announcing the initiative that "total electric generating costs at US nuclear plants have increased 28% -- to an industry average $36.27/MWh -- over the past 12 years," including fuel, capital and operation and maintenance costs. 
Since 2013, Entergy's Vermont Yankee and Dominion's Kewaunee in Wisconsin have been permanently shut "for economic reasons," and Entergy has announced it will shut its Pilgrim in Massachusetts and FitzPatrick in New York in the next two years "largely due to financial losses," NEI said. 
"We are operating in markets with a glut of natural gas at historically low prices, concurrent with low electricity demand nationally," Korsnick said in the statement. "We are seeking to redesign fundamental plant processes to significantly improve operational efficiencies and effectiveness, and in the process make nuclear energy facilities more economically viable." 
NEI said in a fact sheet provided at the briefing that "[a]n analysis at one US nuclear plant site found that supervisors spent over half their time on administrative duties and only 14% of their time supervising employees. In addition, little time was being spent on process improvement efforts or problem-solving activities." 
Other factors contributing to increased productions costs, Korsnick said during the briefing, include significant increases in regulation of nuclear plants and electricity markets that do not adequately recognize and compensate the benefits of nuclear power, such as its reliability in extreme weather, she said during the briefing. 
Industry working groups have identified initial potential savings in several areas, including improvements in corrective action programs, work management, engineering, security and regulatory efficiency, she said. 
Korsnick said the groups' recommendations are being reviewed by a steering committee of chief nuclear officers from companies that operate power reactors. 
Preliminary estimates indicate that the potential savings identified by the working groups could result in "30% cost savings across the industry," amounting to "hundreds of millions of dollars" annually, Korsnick said. Korsnick emphasized that the initiative is being closely coordinated with the US Nuclear Regulatory Commission, and "safety reviews are built into the process" of selecting and implementing the savings proposals. 
  • So what about running this across independent safety advocates and representative community. You do well with people who are skilled at communication and highly skeptical.
In fact, by encouraging operators to take a fresh and critical look at practices and procedures at nuclear plants, the initiative is expected to enhance safety, she said. 
  •  Most if not all the big events in the industry and certainly watching a plant or their management spectacular failing…all of it revolves around emerging financial priorities and budgets cuts. These guys are spectacularly stupid at budget cutting.
Korsnick said in response to a question that the initiative is considering various proposals to modify regional electricity markets to better value the benefits of nuclear power, including low-carbon portfolio standards that would provide additional compensation to carbon-free generators using funds from a surcharge on electricity sold in the state adopting the standard. Exelon, operator of the country's largest nuclear fleet, has proposed such a standard be adopted in Illinois, saying that would benefit its economically struggling nuclear plants and help assure reliable electricity supply. 
Such market reform proposals, however, are far more complex than plant-specific efficiency improvements, and so would take longer to consider and implement, Korsnick said. 
  • So it is a voluntary program plant by plant? What if going through this program they find more money needs to be spent. 
Proposals approved by the steering committee will be either offered for adoption by individual nuclear plants at their discretion or, in the case of actions that must be undertaken by the industry as a whole to be effective, submitted for a vote of NEI's Nuclear Strategic Issues Advisory Committee, a standing group of chief nuclear officers, Korsnick said. Initiatives approved by that committee are binding for the entire industry.

Tuesday, January 26, 2016

Fitz Scram: 'The Three Little Pigs'

The Three Little Pigs 
"Little pig, little Pig, let me come in." 
"No, no, not by the hair on my chinny chin chin." 
"Then I'll huff, and I'll puff, and I'll blow your house in."

So three things took out Fitz. These plants have have millions of components in it and the bureacrocy of the plant is just as complex. This is what happens with insufficient maintenance and budgets...the plant runs away from them. This is a small scale cascade event at the plant. 
 
These guys are heading for the gallows in a year. They ain't plowing money into this invaluable plant.
Anyone watching the new X Files?

What is wrong with this picture? They were at 100% when Frazil ice didn't take them out. Then went down to 60%. It sounds like it's operator error dressed up as an act of god with frazil ice.

Somebody is lying through their teeth. This is not illegal at all.      

1) Frasil

2) So called Planned maintenence

3) And a broken switch 
Platts: FitzPatrick spokeswoman Tammy Holden said in an email Monday: "The lowering intake level indication was a result of frazil ice," which she explained "is a slushy ice condition that occurs in Lake Ontario under meteorological conditions involving water temperature, air temperature, and wind speed and direction." She said, "Frazil ice can create a blockage at the [water] intake structure." 
Sheehan on Monday said, "There was one complication during shutdown: A power transfer glitch knocked the circulating-water pumps out of service, but other systems were used for the cooldown." 
Operators early Friday had reduced the unit's output to 60% of capacity from 100% early in order to conduct unrelated "planned maintenance," Holden said that day in an email.

Monday, January 25, 2016

Calvert Cliffs Junk-Waiting For A Shocking Cascade Accident to Occure

It pretty pathetic when two separate problems takes out a plant. What else is spinning in the background broke but unseen.

Setting up for the deep cascade accident that will shake the nation...

Now what was that special inspection switchyard cable issue. It was Oconee? Junk switchyards at a increasing number of nuclear plants.  

Exelon's Calvert Cliffs-1 nuclear unit shut due to tech glitch in storm's wake

Washington (Platts)--25 Jan 2016 515 pm EST/2215 GMT 
Operators at Exelon's 890-MW Calvert Cliffs-1 units in Lusby, Maryland, shut the unit early Monday morning due to a technical issue, following a downpower to about 10% of capacity from 100% on Sunday when a main transformer cable was found to be disconnected, a US Nuclear Regulatory Commission spokesman said Monday.

Lacey Dean, a Calvert Cliffs spokeswoman, said in an email late Sunday: "Icy conditions and 60 mph winds [from the weekend blizzard] caused a high voltage line in Calvert Cliffs' switchyard to disconnect." Dean added operators "reduced power on Unit 1 and took the generator offline to allow BGE crews to repair the line safely and effectively."

The 880-MW unit 2 continues to operate at 100% of capacity, she said.

Neil Sheehan, an NRC Region I spokesman, said in an email Monday that operators shut the unit early that day "after elevated sodium levels were identified in the condenser. Plant personnel will be checking for condenser tube leakage."...

A Weekend Worth of Junk Nuclear Plants' Tripping.

Yep Calvert Cliffs was related to the storm. So Pilgrim about a year ago had switchyard problems and now Calvert Cliffs uncovered salt water leakage into the condensate through a broken switchyard cable occurring during storm Jonas.
God now is uncovering and disclosing problems at the plant not the NRC or the plant's bureaucracy.   
I see none of these related to storm Jonas. This is a severe scram rate on the national picture. It would be pretty bad if this 3 day rate stays this high. Only Fitz is winter related. This is all bad maintenance... 

Several nuclear plants see unplanned outages over winter weekend

Several nuclear power plant units experienced unplanned outages during the winter weekend, according to data filed with the Nuclear Regulatory Commission on Jan. 25. 
NRC records indicate that four commercial reactors went offline during the winter weekend when much of the eastern half of the nation was experiencing the so-called “Winter Storm Jonas.” At least one of the nuclear operators has acknowledged that their outage was weather-related. 
Overall, 92 of the nation’s 100 commercial power reactors were listed as generating power early Jan. 25 by the NRC. Some were already offline for scheduled maintenance. 
The Tennessee Valley Authority Watts Bar 2 unit has not actually commenced operation yet but is counted among the 100 active domestic units because it has been licensed. 
Nuclear operators typically don’t divulge how long they expect an outage to last, citing competitive reasons. Here’s a rundown of the weekend’s unplanned outages:
  • The Calvert Cliffs 1 unit in Maryland, operated by Exelon was manually tripped from 10 percent power due to elevated condenser sodium levels. All systems responded per design, according to an event report filed with NRC. The event happened shortly after 3 a.m. on Monday, Jan. 25. Unit 2 was not affected and remains at full power, according to the report.  
  • The Dominion Millstone 3 facility in Connecticut was at 100 percent power shortly before 2 a.m. on Jan. 25 when a problem with the ‘B’ reactor coolant pump “caused a reactor trip on low coolant flow,” according to the NRC report. The issue is under investigation and the dayshift will be troubleshooting the problem, the report said. A company spokesperson described the automatic shutdown as “safe and uncomplicated.” 
  • The Entergy FitzPatrick 1 facility in Upstate New York underwent a manual scram from 89 percent power late Jan. 23 “due to a lowering intake level,” according to the report to NRC. There was no release of radioactivity and no threat to workers or the public, an Entergy spokesperson told GenerationHub. “The lowering intake level indication was a result of frazil ice. Frazil ice is a slushy ice condition that occurs in Lake Ontario under a specific set of environmental and meteorological conditions involving water temperature, air temperature, and wind speed and direction. Frazil ice can create a blockage at the intake structure,” the spokesperson said. 
  • The FirstEnergy Perry plant in Ohio experienced a reactor shutdown "due to unidentified leakage in the drywell,” according to the NRC report. Perry plant personnel are performing maintenance on a weld on a plant piping system after shutting down early Sunday, Jan. 24, said a company spokesperson. “There are no adverse impacts to workers at the plant or to the public as a result of this work,” she said.

Connecting the Dots on ANO and Recent Nuclear industry Issues

My theme is there was documented and known issues these plants were entering a abyss by the NRC...but the NRC was prevented to act by Congress. Prevented from seeing the big Picture. I really don't think the rank and file NRC inspector has the requisite education and experience to even be a NRC inspector.   

This all looks like jumping flees to me...Palisades, Vermont Yankee, ANO, Pilgrim and now River Bend and Waterford. 

So basically the function of the NRC is to stay away from a serious off site radiation event(meltdown)...their job is not to keep the industry palatable to the public and orderly. Risk perspectives does that for them. I think the demarcation of a serious accident like TMI and Fukushima is is blurry as hell to the agency and at the plant. More, the danger line is almost unquantifiable, as least through the component worth and isolated risk calculation of components and systems. Basically risk perspectives is worthless.It is grossly oversold as a protect scheme for our nation...

Why doesn't risk perspectives focus the agency to look at the right areas in the below plant events...anticipate these events. Why didn't the NRC informed by risk perspective, step in and knock heads before these events emerged from the bureaucracy of organizations. Really, the events below are seen months and years before the events occur. They are organization centric events, not components, systems and electronics centric events.

Really congress is regulating the plant inspectors and the NRC...limiting their interaction and field of view with the goings on in the plants. We strictly follow the rules, but are we really allowed to see everything and is the plants required to show everything. It more a child's peekaboo going on in the USA between a plant and the NRC.
Jan 2015 Pilgrim
March 2013 ANO
March 2012 San Onofre
June 2011 Fort Calhoun
As example, if the NRC can't anticipate and head off...being situationally aware... in the four plant events above, how do you expect them to head off a meltsown or other significant industry events.

Post findings on these plants for the events, they discovered years of known problems not openly confronted by the NRC. It is as if we got two regulatory policies, one declared and the other not seen by outsider until a big event makes transparent the agency negligence over many years. The truth is, congress never punishes the NRC for allowing a plant to operate outside regulation. The NRC is mostly on the day to day events in these plant a god unto themselves. The big problem is agency knows they are not constrained by higher levels of government. The giant electric utilities are just a too powerful political force unconstrained  political campaign contribution. Really not bounded by the ideals of our perfect constitution. The NRC acts like a totalitarian force for big business, unafraid of getting thrown out of office by the voters. Ultimately they are a power unto themselves and nobody is required to tell the complete truth.       

Why aren't we asking ourselves and NRC, is our NRC just as inflexible as the Japanese's Nuclear Regulatory Authority. Have we regulated the inspectors more than the plants? Is the NRC and the public only getting a very limited field of view...has Congress set up the system for that by campaign contribution. 
January 22, 2016 5:30 pm JST 
IAEA urges Japan to enhance technical competence for nuclear restarts 
TOKYO (Kyodo) -- The International Atomic Energy Agency said Friday that Japan should "strengthen its technical competence," after a team of experts of the U.N. nuclear watchdog concluded a 12-day mission the same day to assess the regulatory framework for nuclear and radiation safety in Japan. 
The country's Nuclear Regulation Authority "needs to further strengthen its technical competence in light of upcoming restarts of nuclear facilities" idled after the 2011 Fukushima nuclear disaster, the team said in its initial report. The final mission report will be released in about three months.
The latest Integrated Regulatory Review Service followed the first review in Japan in June 2007, marking the first assessment since the March 2011 earthquake and tsunami caused the Fukushima nuclear crisis. The NRA was established in 2012 to oversee stricter regulations. 
The team of 19 nuclear experts also found Japanese authorities need to amend relevant legislation to allow the NRA to conduct more effective inspections. 
"What we found is the system that is regulating or defining the framework for inspection is very complex and very rigid," Philippe Jamet, the head of the mission team, said at a joint press conference held by the team and the NRA.
"It doesn't give enough freedom for the inspectors to react immediately," Jamet said. 
Shunichi Tanaka, the chairman of the NRA, said the Japanese regulatory body will work more closely with power companies to improve its inspection operations. 
"We have to talk to operators more thoroughly to improve the inspection method," Tanaka said. 
The mission team also said the NRA should work to attract more experienced staff and strengthen staff skills through education, training and international cooperation...

 Briefing Notes for 95003 Inspection at Arkansas Nuclear One
2:00 pm EST/1:00 pm CST
January 20, 2015

Nuclear Regulatory Commission (NRC) Staff Participants:
  • Neil O’Keefe, Branch Chief and 95003 Inspection Team Leader
  • John Dixon, Assistant Team Leader
  • Brian Tindell, Senior Resident Inspector
Purpose 
To provide a current status of performance regulatory oversight and performance improvement efforts to improve safety performance at the Arkansas Nuclear One nuclear power plant.

Background 
The NRC increased regulatory oversight of Entergy’s Arkansas Nuclear One (ANO) plant in the third quarter of 2014. ANO was placed into Column 4, “Multiple/Repetitive Degraded Cornerstone,” of the NRC’s Action Matrix as a result of having two Yellow findings affecting each of the two plants. The NRC’s color coding indicates that Yellow findings have substantial safety significance. These findings were identified as a result of the events surrounding the industrial accident that occurred at the plant on March 31, 2013, which resulted in one fatality and eight injured personnel. One Yellow finding involved performance deficiencies identified from the event associated with dropping a heavy component and causing significant damage to plant equipment. The other Yellow finding involved performance deficiencies associated with inadequate flood protection of safety equipment that was exposed as a result of plant damage from the heavy component drop.

Event Description 
On March 31, 2013, during a planned Unit 1 outage, the licensee was lifting the Unit 1 main generator stator out of the turbine building when an inadequately designed temporary lifting rig failed, causing the 525 ton stator to fall approximately 30 feet into the train bay. The train bay is shared between Unit 1 and Unit 2. The impact caused substantial damage to the Unit 1 side of the turbine building and power distribution systems, and parts of the lift rig impacted the Unit 2 side of the turbine building.

Yellow Finding Associated with the Heavy Component Drop

The temporary lifting rig collapsed because there were incorrect assumptions and errors in the design such that it could not safely complete the intended lift. A test to verify the capability of the lift rig was not performed due to further errors in communication and decision making. These failures were the result of inadequate oversight of the primary contractor and a subcontractor hired to perform the operation. As a result, there was a complete loss of offsite power to Unit 1 for six days, and Unit 2 partially lost offsite power. This increased risk to the plant because alternate means of providing electrical power to key safety-related systems was not available using installed plant equipment in the event the diesels failed. The NRC determined that this constituted a violation of substantial safety significance.

Yellow Finding for Degraded Flood Protection Features

Following the flooding that occurred during the heavy component drop event, the licensee conducted a comprehensive inspection and identified over 100 deficient flood protection features, including unsealed electrical cable conduits, and degraded hatches and floor plug seals in the auxiliary and emergency diesel fuel storage buildings. NRC inspections subsequently identified additional problems, necessitating further reviews. Both Unit 1 and Unit 2 Safety Analysis Reports (SARs) require that the auxiliary building and safety-related pump rooms be watertight.

The NRC concluded that the licensee had failed to design, construct, and maintain the flood protection features in both units in accordance with the approved design requirements. The finding included multiple violation examples and was determined to have substantial safety significance. The primary contributor to the safety significance was due to the potential safety impact of the theoretical maximum rainfall event, which could lead to core damage due to equipment damage from the degraded flood protection features.

NRC Actions
  • The safe operation of the units is the NRC’s primary concern. We have three inspectors onsite that are continuously assessing day to day operation, and we are documenting our assessment that continued plant operation is acceptable in quarterly inspection reports.
  • ANO is currently receiving one of the highest levels of NRC oversight designed to ensure that the plant continues to operate safely and performance does not further decline. If safety performance declines further, the NRC will promptly identify and address the decline with regulatory actions up to and including shutting the units down.
  • Both the NRC and the licensee are in the process of evaluating the nature and extent of performance issues. We have reviewed the results of each of their evaluations and interim actions to avoid further performance decline.
  • The NRC will begin a comprehensive inspection on January 25, 2016. The inspection will involve a team of about 25 inspectors who will spend about 3,600 hours on the effort. This inspection will be an independent evaluation of the extent of the performance problems at Arkansas Nuclear One. We will also assess the licensee’s evaluation of their problems and their proposed corrective actions to ensure they lead to timely and sustained performance improvements.
  • We expect to issue an inspection report with the findings and assessments of the team in the spring of 2016. We have tentatively scheduled a public exit meeting for April 6, 201
  • April 6, 2016, and will also present the results of the NRC’s annual assessment. Victor McCree, the NRC’s Executive Director for Operations, is expected to attend this meeting.
  • The NRC will issue a Confirmatory Action Letter that documents commitments made by the licensee to implement the key corrective actions needed to improve safety performance. The NRC will then conduct inspections to verify the completion and effectiveness of those corrective actions as the actions are completed.
  • Based on past experience with plants with similar performance problems, we expect it will take ANO 2 to 3 years to complete the actions needed to demonstrate a sustained improvement in safety performance. The NRC will not reduce the level of oversight until ANO has completed those key actions designated in the Confirmatory Action Letter and the NRC inspections confirm that those actions were effective.
ANO Actions
  • ANO has been effective in running the units safely and not allowing the recovery efforts to detract from safe plant operation.
  • ANO has completed an extensive series of evaluations to identify the causes for declining safety performance, and has developed, prioritized, and scheduled corrective action to address those causes. These evaluations were performed with the help of nuclear industry experts from outside the company to assist in recognizing areas where ANO and Entergy have not been following industry practices.
  • ANO has recognized that their top issue affecting performance involves ensuring that the necessary resources are provided to accomplish station programs and processes in a safe and effective manner (for example, vendor/contractor oversight, increasing backlogs, and equipment maintenance). They have added more than 100 workers and have brought in consultants to assist with its performance improvement and recovery effort.
  • The NRC will issue a Confirmatory Action Letter that documents commitments made by the licensee to implement the key corrective actions needed to improve safety performance. The NRC will then conduct inspections to verify the completion and effectiveness of those corrective actions as the actions are completed.




Sunday, January 24, 2016

Who Wants River Bend’s Junk Capacity Factor?

Update 1/27

Is River Bend ever going to startup again? This is the big problem as far as the industry's financial problems.
 
Update 1/24

Still shutdown today? Have they made money in the last two years? 

***This shutdown must have caused a lot of damage? Eleven days and counting?  


Event Date: 01/09/2016

 

Saturday, January 23, 2016

Junk Pilgrim Prepared For Storm, Operators Say

It would take at least 4 to 6 hours to bring about a orderly shutdown and cool down.
It would be so cool for the plant to trip today and LOOP? Would this be the last shutdown in the life Pilgrim plant. :)

None of this is based on real engineering, engineering assurance it could survive Blizzard. Although I believe Entergy is worried about if Gov Baker begins to turn on them. It is all a grand NRC experiment.  
 
Who cares if Entergy is going to permanently shutdown within a year. or so.

..."the Nuclear Regulatory Commission spokesman said Friday that procedures for addressing storms have been tightened since last year."

It is interesting the grid prices spiked up this early morning. Is it a result of normal winter condition approaching the coast or has the grid anticipated losing Pilgrim:)
 
Maybe Entergy wants the NRC to shutdown the plant...blame them for permanently shutdown the plant.   
NUCLEAR SAFETY
Pilgrim prepared for storm, operators say
The protocol has been tightened in the year since a blizzard-induced shutdown at the plant, a Nuclear Regulatory Commission spokesman says.
By Christine Legere


Posted Jan. 22, 2016 at 5:45 PM
Updated at 9:17 AM

PLYMOUTH — Operators at Pilgrim Nuclear Power Station say they are ready for whatever the fast-traveling snowstorm heading up the East Coast this weekend, with accompanying 60 mph winds, brings their way.
“We are monitoring the storm closely and have begun preparations under our coastal storm protocol,” Entergy Corp., the plant’s owner-operator, said Friday in a statement provided by spokesman Patrick O’Brien.
One provision in the newly beefed-up storm plan calls for a pre-emptive shutdown based on the severity of the storm. “It has to do with wind speeds and the rate of snowfall,” Neil Sheehan, spokesman for the Nuclear Regulatory Commission, wrote in an email Friday.
Entergy is holding off on that decision for now. “The currently projected storm path and weather conditions do not meet the criteria for a pre-emptive shutdown of the station,” the company statement said. “We will continue to monitor the storm closely and have appropriate staff and other resources available should conditions change.”
The Pilgrim plant's 220-foot primary meteorological tower is still out of service, awaiting a part expected to be installed in February, according to Sheehan. The smaller backup tower will provide plant operators with vital information on wind velocity and direction.
That second tower had been inoperable for several years and was just recently replaced. The plant must rely on the National Weather Service in Taunton whenever a single tower goes down and lacks backup.
Representatives of the Plymouth Fire Department were at the nuclear plant earlier this week to review storm preparations, according to the town’s emergency management director, Aaron Wallace.
It has been just about a year since a blizzard tore through the Northeast, knocking out power at Pilgrim. Problems began with electrical arcing in the switchyard, where power is brought to the plant and sent from the plant to the grid. Such switchyard problems date back as long as 30 years.
Operators shut down the reactor during that January storm, but problems persisted, with the failure of a diesel-driven air compressor, a leaking safety valve used to depressurize the reactor, failure of a manually operated safety relief valve and failure of the high-pressure coolant injection system, which then leaked an inch of water onto the floor.
Sump pumps could not clear it, since all nonvital functions at the plant had been shut down.
The series of malfunctions during that storm prompted a week of federal inspections and contributed to the downgrade of the Pilgrim plant by NRC officials in September to among the three worst performers in the country.
Entergy announced in October its plan to permanently shut down the Pilgrim reactor sometime before June 2019.
Although some plant watchdogs warn there is no longer any impetus for Entergy to stay on top of plant maintenance, the Nuclear Regulatory Commission spokesman said Friday that procedures for addressing storms have been tightened since last year.
“We have a resident inspector at Pilgrim who is continuing to closely track storm preparations,” Sheehan wrote. “For instance, site walkdowns were conducted yesterday to check for any loose debris that could be tossed by strong winds and impact the switchyard or plant infrastructure.
“Also, a change put in place since last winter’s storms is the installation of heat lamps in the switchyard to prevent the kinds of electrical arcing events that have occurred in the past,” Sheehan continued. “We will be paying attention to the heat lamps’ effectiveness should they be needed during this storm.”
David Lochbaum, director of the Nuclear Safety Project for the Union of Concerned Scientists, said the switchyard is always vulnerable to winds and icing. “The backup generators are the real safety net,” he said. “If they work, they effectively cool the reactor. Because of the problems in the past, (Pilgrim operators) may be more prepared and have a longer list of backups.”

Storm Jonas 2016: Is Junk Plant Pilgrim Shutting Down?

Update The day after 1/24

The definitive answer from the NRC tonight. Lots of nuke plants had lots of trouble with weather this storm.
 

…”there have been no significant impacts at the facility”: depends on what their definition of “no significant impacts at the plant” means. I'd like them to describe all storm related impacts at the plant.    
  NRC: Update: As the Blizzard Moves Out of the Mid-Atlantic
Just North of Pilgrim.
The Weather Service recorded a wind gust of 70 miles per hour at the municipal airport in Marshfield.
So far it looks like Pilgrim stayed up at power. Course Plymouth got only grazed by storm Jonas. But...
Update, 6 p.m.
PLYMOUTH MA — Eversource crews on Saturday night restored power to all but about 100 customers after a snowstorm knocked out power to over 1,000. 
Winter Storm Jonas brought blizzard conditions that knocked out power for more than 1,000 in Plymouth Saturday afternoon. 
Boston Globe:
"Boston can expect the snowflakes to start falling between noon and 2 p.m. Temperatures will hit a high of about 30 degrees and a low of about 20 at night, said Frank Nocera, a National Weather Service meteorologist.
Nocera said the highest snow totals from the storm would be in the southeastern part of the state, where 8 to 12 inches of snow can be expected. The storm will also feature high winds that may bring down power lines and the possibility of coastal flooding, forecasters said."

Remember Pilgrim last year didn't trip after many hours of brutal blizzard conditions. It wasn't a really bad blizzard and much snow accumulation. The plant tripped right at the beginning of the blizzard.
Accuweather says Plymouth is going to get more than two hours of heavy snowfall this afternoon.
The red outlined area is the National Weather Service's "Winter Storm Warning".  Storm Jonas has intensified much more than anticipated in the models. South Shore Massachusett just a few hours ago wasn't supposed to get any snow at all.





Winter Storm Warning remains in effect until 7 AM EST Sunday.
  • Locations: Kent and Bristol counties in Rhode Island and coastal Plymouth County. Cities and towns in the warning include Plymouth, West Greenwich, Warwick. Bristol.
  • Hazard types: Heavy snow.
  • Accumulations: snow accumulation of 4 to 8 inches.
  • Timing: snow will develop around mid morning and become heavy at times in this afternoon and evening. Snowfall rates up to one inch per hour will be possible at times. Gusty winds up to 45 mph combined with the snow will result in blowing snow and poor visibilities at times. The snow will begin to taper off after midnight.
  • Impacts: hazardous travel with heavy snow and poor visibilities. Heavy snow combined with strong winds may result in isolated power outages.
  • Winds: northeast 25 to 35 mph with gusts up to 55 mph.
  • Temperatures: in the upper 20s.
  • Visibilities: one quarter mile or less at times.



Thursday, January 21, 2016

Junk Safety Culture Still At Arkansas Nuclear One

This guys are bad. Can you believe the violation level from the NRC??? The risk determination system is completely broken down by political intervention. This is Flint Michigan.   
Just to be clear, ANO and Pilgrim are the worst operating nuclear power plants in the USA. There are owned by Entergy.  Where is your dignity?  
Findings  
Introduction. The inspectors reviewed a Green self-revealing non-cited violation of 10 CFR Part 50, Appendix B, Criterion V, “Instructions, Procedures, & Drawings,” for failure to follow the instructions in the chemical volume control system charging pump pulsation dampener bladder charging procedure. Specifically, the licensee used a gas cylinder containing argon, carbon dioxide, and oxygen rather than a pure nitrogen cylinder to charge the dampener. The gas leaked into the reactor coolant system and was subsequently activated by neutrons. Reactor coolant system activity significantly increased, which elevated dose rates in the auxiliary building. 
Description. The Unit 2 chemical volume control system charging pumps have suction and discharge dampeners to reduce pressure pulsations caused by these positive displacement pumps. These dampeners are an accumulator tank with a nitrogen filled bladder. Nitrogen leakage through the bladder can result in the nitrogen entrainment in the water, which is pumped into the reactor coolant system. The licensee had been aware
It's the absence of a fix it quickly philosophy. The longer you got a mechanical defect in a system with degraded safety culture the greater the chances of a bigger problem popping up.
of leakage from the dampeners and had implemented quarterly preventative maintenance tasks to check the pressure and fill the dampeners with nitrogen, if necessary. 
On July 31, 2015, a reactor coolant sample indicated a rising trend in argon-41.  argon-41 is a radioactive isotope of argon that is created when argon-40 in reactor coolant passes through the reactor and becomes irradiated. It undergoes decay, giving off a high-energy beta particle, increasing dose rates in the plant. A failure mode analysis team investigated the possible causes and identified the most likely cause to be a leaking charging pump dampener bladder filled with the incorrect gas. 
On September 3, 2015, the licensee performed gas chromatograph sampling on the 2P-36C charging pump suction and discharge dampeners. Although the test equipment cannot test for percent argon content, the test determined that the suction dampener only had a 14.4 percent nitrogen content. The discharge dampener only had a 15.4 percent nitrogen content. If the dampeners were charged with nitrogen as expected, the content would be expected to be over 90 percent nitrogen. The licensee recharged the pulsation dampener with pure nitrogen, and dose rates in the plant returned to normal. 
The addition and subsequent activation of argon caused the reactor coolant activity to increase by a factor of three over a period of two months. This increased the dose rates in the vicinity of piping associated with the chemical and volume control system, increasing dose to operators and radwaste personnel. 
The licensee performed a cause analysis and determined that a human performance error caused the wrong gas to be used. Plant maintenance mechanics had performed pulsation dampener preventative maintenance on July 28, 2015. The mechanics retrieved a pressure gauge from the hot machine shop and went to the compressed gas cylinder storage rack. The mechanics measured pressure in the cylinders and chose the first cylinder that contained sufficient gas. The mechanics then proceeded to 2P-36C charging pump dampener fill connection, connected the cylinder to the charging header, and recharged the pulsation dampeners. 
All of the gas cylinders in this storage location were the same color, and the labelling appeared similar unless read carefully. The mechanics failed to check the label on the gas cylinder to ensure that they chose a nitrogen bottle, and they incorrectly chose the single cylinder that contained a mixture of carbon dioxide, oxygen, and argon. 
The licensee revised the procedure to require independent verification of the gas prior to charging pulsation dampeners. 
Chemistry samples confirmed there was no change in oxygen content in the reactor coolant. 
Analysis. The failure to follow the pulsation dampener charging procedure, which resulted in increased reactor coolant system activity and elevated dose rates in the auxiliary building, was a performance deficiency. The performance deficiency is more than minor because it was associated with the plant facilities/equipment attribute of the Occupational Radiation Safety Cornerstone and adversely affected the cornerstone objective to ensure the adequate protection of the worker health and safety from exposure to radiation from radioactive material during routine civilian nuclear reactor operation. Specifically, charging argon into a pulsation dampener with a known bladder leak resulted in an increase in reactor coolant activity, causing elevated dose rates in several plant areas. Using NRC Inspection Manual Chapter 0609 Appendix, C, “Occupational Radiation Safety Significance Determination Process,” issued August 19, 2008, the inspectors determined that the finding was of very low safety significance (Green) because it did not involve ALARA planning or work controls, did not involve an overexposure, did not have a substantial potential to be an overexposure, and the ability to assess dose was not compromised. The inspectors determined this finding had a cross-cutting aspect in the human performance area, Avoid Complacency, because the plant maintenance mechanics failed to implement appropriate error reduction tools such as self-checking and peer-checking. [H.12] 
Enforcement. Title 10 CFR Part 50, Appendix B, Criterion V, “Instruction, Procedures, & Drawings,” states that “Activities affecting quality shall be prescribed by documented instructions, procedures, or drawings, of a type appropriate to the circumstances and shall be accomplished in accordance with these instructions, procedures, or drawings. Instructions, procedures, or drawings shall include appropriate quantitative or qualitative acceptance criteria for determining that important activities have been satisfactorily accomplished.” Contrary to the above, on July 28, 2015, the licensee failed to accomplish an activity affecting quality in accordance with the procedure. Specifically, the licensee failed to charge a charging pump pulsation dampener, an activity affecting quality, with nitrogen as required by quality Procedure OP-2411.066, “Charging Pump Dampener Bladder 2M-115A, B, C and 2M-116A, B, C Charging, Checking and Depressurization,” Revision 5, Attachment 3, Supplement 1. Step 1.3 of this procedure required that nitrogen be connected to the charging pump pulsation dampener supply valve during the charging process, but a bottle with a mix of gases including argon was used instead. The error resulted in a significant increase in reactor coolant activity, with a resulting increase in dose rates in various areas of the plant. As corrective action, the licensee recharged the dampener with pure nitrogen and degassed the reactor coolant system to reduce dose rates in the plant. This violation is being treated as a non-cited violation (NCV), consistent with Section 2.3.2.a of the Enforcement Policy because it was of very low safety significance (Green) and it was entered into the licensee’s corrective action program as Condition Report ANO-2-CR-2015-02576: NCV 05000368/2015003-01, “Failure to Follow Procedure Results in Increased Reactor Coolant Activity.”
***"On August 18, 2015, the licensee identified an adverse trend in unsecured doors, as documented in Condition Report CR-ANO-C-2015-03229. Specifically, the condition report documented that 15 condition reports had been written since May 1, 2015, for fire or high energy line break doors found open and unattended. The licensee addressed this trend by conducting a personal interface campaign at the plant entry area. As persons entered the station, managers stopped them, discussed the importance of barriers, and handed them a one page document with further information on why barriers are important to safety. In addition, departmental managers were given an action to develop a plan to verify or improve employee behaviors. Following these actions, two more condition reports identified doors that had been left open. Station management held a stand down on September 28, 2015, with all station employees to ensure that they understood the importance of door design and configuration.'
The inspectors found that the station had appropriately identified the adverse trend in regards to station behaviors, but had failed to document an adverse trend in the number of documented door deficiencies. In the past year, 31 condition reports documented deficient conditions on doors required for security, fire, high energy line break or flooding. Although the licensee failed to identify the trend, the inspectors determined that the licensee was addressing the conditions appropriately in the work management system. The licensee documented the observation in Condition Reports CR-ANO-C-2015-03972 and CR-ANO-C-2015-03973.
This whole thing is frightening as hell below. Basically defective breakers and buses interacting with a roof leak....plus the issue gets lost in the bureaucratic document system. Instead of bureaucracies and documentation systems shining a light on problems early, it digs a big hole and buries the problems.  Roof leaks are  prime evidence of a severe safety culture problem. How long was the roof leak and why didn't the NRC step in before it damaged the bus and breaker?   

Another non sited violation to their buddies ...
***Introduction. The inspectors reviewed a self-revealing violation of 10 CFR Part 50, Appendix B, Criterion XVI, “Corrective Action,” for the failure to promptly identify and correct conditions adverse to quality. Specifically, the licensee failed to promptly replace short bus stabs with longer bus stabs in six safety-related motor control centers (MCCs) following a 2007 motor control center fault.
Description.
On April 21, 2015, non-safety MCC 2B-35 experienced a fault which melted bus bars and caused the feeder breaker to the MCC to open to isolate the fault, de-energizing multiple non-vital loads in the turbine building. Subsequent inspection and analysis determined that the fault was caused by a high resistance connection between the breaker for turbine building recirculation fan and the associated bus bars. Contributing to this condition, the licensee observed indications that water had dripped onto the bus bars from above from turbine building roof leaks. This event led the licensee to review a previous similar event and to assess the corrective actions for that event.
In October 2007, a fault had occurred in a Unit 2 motor control center when starting a charging pump, which tripped the motor control center feeder breaker and secured power to all the loads supplied by that motor control center. The licensee documented in Condition Report CR-ANO-2-2007-01512 that the cause of the fault was “limited physical stab engagement on bus”. The limited contact area between the breaker stabs and the bus bars was determined to be marginal for the current needed to run the charging






Wednesday, January 20, 2016

Seabrook at 60% and ISO Prices

Update1/22

Good job Seabrook with getting back to 100% yesterday. The NEISO is at around $39 per megawatt hour. The price is shockingly low for such a cold spell. When is the businesses and ratepayer going to get a break?

***So Seabrook has been at 60% for three days. What is up?

I continue to be amazed by how docile the price of electricity has been throughout the mild winter and now in a deep winter cold spell. It is amazingly cheap. No big spikes in prices as has been the last winters...

It is amazing how much media and print time is devoted to solar and wind. It is such a small percentage of net generation...

EIA_WholesalePowerPrice


Wholesale electricity prices and demand in New England

Year-over-year natural gas and wholesale power prices dropped in December on milder weather, lower demand

December’s average natural gas and wholesale power prices in New England were about half as much as the average monthly prices recorded during December 2013, due largely to milder weather that dampened demand. During December 2013, colder weather increased consumers’ use of natural gas for heating, resulting in natural pipeline constraints that drove natural gas prices higher. Those high fuel prices, in turn, pushed up wholesale power prices.
This past December, the average real-time price of wholesale power, at $42.47 per megawatt-hour (MWh)*, fell about 57% from the December 2013 average of $98.53/MWh. It was down by about 5% from November’s price of $44.86/MWh...