Friday, May 11, 2018

2016001: Hope Creek's 1st SRV Inspection Responce To Me

Reposted from 9/30/2017

The questions I posed to the NRC to drive this article is on the NRC's docket.

May 10, 2016

SUBJECT: HOPE CREEK GENERATING STATION UNIT 1 – INTEGRATED INSPECTION REPORT 05000354/2016001

Annual Sample:  Safety Relief Valve Set Point Drift
a. Inspection Scope
The inspectors reviewed PSEG's identification, evaluation, and corrective actions associated with longstanding main steam safety relief valve (SRV) set point drift issues at HCGS.  Specifically, at HCGS, one or more SRVs have exceeded the TS allowable as-found lift set point acceptance criteria in 17 of the 19 operating cycles over the life  of the plant (See Section 4OA3.1 for a review of Licensee Event Report (LER) 05000354/2015-004-01 related to as-found test results from refueling outage 19 (RF19)).  PSEG contracted with NWS Technologies to perform SRV as-found testing, SRV pilot valve assembly inspection and repair, and SRV as-left testing at their offsite facility.
The inspectors assessed PSEG’s problem identification threshold, technical and cause analyses, operating experience (OE) and trend reviews, vendor oversight, and the prioritization and timeliness of corrective actions to evaluate whether PSEG was appropriately identifying, characterizing, and correcting problems associated with these issues and whether the planned and/or completed corrective actions were appropriate.  The inspectors compared the actions taken in accordance with the requirements of PSEG’s and NWS’ maintenance procedures, PSEG’s CAP, 10 CFR 50 Appendix B,  Hope Creek’s TSs, and the Maintenance Rule.  The inspectors interviewed Nuclear Oversight (NOS) and engineering personnel to gain an understanding of potential operational challenges, overpressure protection capability and margin management, NWS performance, planned and completed corrective actions, and SRV performance.  The inspectors also reviewed NWS pilot assembly test and inspection documentation, including quality assurance (QA) acceptance and independent verifications, to ensure that NWS performed activities in accordance with prescribed procedures and industry standards.  In addition, the inspectors performed several walkdowns of SRV related instrumentation (including the control room, the remote shutdown panel, and the alternate shutdown automatic depressurization system panel instrumentation and alarm panels) to independently assess the material condition, operating environment, SRV performance, and configuration control.  [See also NRC Inspection Report 05000354/2012004, Section 4OA2.2, NRC Inspection Report 05000354/2013005, Section 4OA2.6, and NRC Inspection Report 05000354/2015003, Section 4OA2.4 for additional NRC assessment of the Hope Creek SRV issues.]
a. Findings and Observations
No NRC or self-revealing findings were identified.  A licensee-identified violation associated with as-found set point test failures in RF19 is documented in Section 4OA7.  
The Hope Creek main steam SRVs are 6" x 10" Target Rock Model 7567F, 2-stage SRVs consisting of a pilot stage, a main stage, and an air operator for remote operation.  Hope Creek has 14 safety-related main steam SRVs that provide reactor pressure vessel overpressure protection and an automatic/manual depressurization function.  Hope Creek TS 3.4.2.1, “Safety/Relief Valves,” requires that 13 of the 14 SRVs be operable with the specified code safety valve function lift setting (+/- 3 percent).  Hope Creek TS surveillance requirement 4.4.2.2 requires that at least half of the SRV pilot stage assemblies be removed and set pressure tested in accordance with the Surveillance Frequency Control Program (currently at the refueling outage (RFO) frequency of every 18 months).  Since RF15 in April 2009, PSEG has performed as found lift tests on all 14 SRV pilot valves every outage.  PSEG conducts this surveillance testing during RFOs when the SRVs are accessible during reactor shutdown conditions.  Historically, Hope Creek has experienced numerous as-found lift pressure failures during SRV testing.  Most recently, in June 2015, PSEG identified that 10 of 14 SRVs lifted above the TS specified pressure band (see Section 4OA3.1).
The Target Rock 2-stage SRV has an industry-wide history of set point drift.  Early documentation from General Electric (GE) identified that the Target Rock 2-stage SRV design was susceptible to corrosion bonding resulting in set point drift.  The corrosion bonding failure mode occurs due to bridging oxides created between the pilot disc surface and the pilot valve body disc seating surface during service.  The corrosion bonding trend results in the valve lifting at a higher pressure, failing to meet its set point criteria during the first lift attempt, but successfully lifting during consecutive tests (after the corrosion bond is broken during the first lift).  Over the years, PSEG
May 11 2018: The multiple failures of the coatings and new valve designs indicate massive experimentation going on in the reactor. They are suppose put these changes into a comprehensive testing regime guaranteeing there will no surprises and the changes worked as advertised before they to go into the reactor. I think all these changes are engineered to buy time for the utility, not really solve the problem. It is really fraud and corruption!!!    
personnel reviewed failure mechanisms and implemented maintenance recommendations from industry OE, GE Service Information Letters (SILs), and Boiling Water Reactor Owners Group recommendations in an unsuccessful attempt to address Target Rock pilot set point drift failures.  For example, the industry and PSEG have identified and implemented numerous mitigating strategies including: different pilot disc materials/coatings, addressing critical pilot disc and seat dimensions, correcting methods of insulation installation, and increased TS as-found set point margin (from +/- 1 percent to +/- 3 percent) in an attempt to improve Target Rock 2-stage SRV reliability.  The inspectors noted that PSEG implemented a mitigation strategy to install new pilot discs in all 14 SRV pilot valves every RFO; however, based on the continued set point drift failures, this aggressive practice has not proven effective at mitigating the corrosion bonding failure mechanism. 
During the review of Hope Creek LER 05000354/2010-002-01 in September 2011, NRC inspectors questioned whether multiple SRVs exceeding the TS allowable as-found lift set point acceptance criteria represented a significant CAQ (SCAQ).  In response, on September 13, 2011, PSEG initiated corrective action NOTF 20525076 to address the inspectors’ concern.  PSEG reviewed their CAP procedure guidance and determined that the condition was not a SCAQ; however, it warranted a root cause evaluation (RCE).  In February 2012, PSEG completed the RCE, “SRV Setpoint Drift Root Cause Evaluation” (70128407-010), to evaluate the longstanding SRV set point drift issues.  PSEG’s root cause analysis reviewed station preventative maintenance practices (rigging, storage, transportation, etc.), maintenance procedures, internal maintenance history, vendor maintenance history (including testing and inspection reports, replacement parts, and practices), industry OE, and the application of this OE at Hope Creek.  The root cause team evaluated the Target Rock SRV pilot valve design, manufacturing, and application.  The root cause team also reviewed effects of Extended Power Uprate, steam line vibration, and performance of each SRV by serial number.  In February 2012, the multi-disciplined PSEG root cause team determined that the Target Rock 2-stage SRV pilot valve design was incapable of satisfying the set point drift design requirements on a consistent basis.  PSEG’s corrective actions to prevent recurrence of the above root cause included plans to replace the currently installed Target Rock 2stage SRVs with a design that eliminates set point drift events exceeding +/-3 percent and improves SRV reliability.  Based on several engineering studies (including industry OE), PSEG’s Main Steam SRV Replacement Project (H-11-0009) recommended replacing the existing 2-stage Target Rock pilot valves with a SEBIM pilot operated design or with an upgraded Target Rock 3-stage pilot.  During the first quarter of 2014, PSEG made the decision to no longer pursue the SEBIM model replacement valve due to difficulties meeting Hope Creek specifications.  PSEG developed design change package (DCP) 80107006, “Safety Relief Valve (SRV) Replacement,” and had planned to install seven Target Rock 3-stage pilots in May 2015 (RF19).  However, in the early months of 2015 (just prior to RF19), PSEG decided to defer installing the new 3-stage Target Rock valves due to significant OE at Pilgrim Nuclear Power Station (including a Target Rock Part 21 report).  At the time of this inspection, PSEG tentatively planned to install one new 3-stage Target Rock pilot valve in the Fall 2016 RFO (RF20), contingent on the satisfactory acceptance testing results.  The inspectors noted that PSEG’s decisions that resulted in delays in replacing the existing 2-stage Target Rock pilot valves were appropriate, conservative, and aligned with the principle of not moving forward in the face of uncertainty.  From a historic perspective, leading up to RF19 in May 2015, the inspectors noted that PSEG’s aggregate actions to address SRV pilot valve set point drift issues were aligned with industry initiatives, appropriate, and commensurate with the safety significance.
On June 3, 2015, based on initial post-RF19 test reports, PSEG initiated corrective action NOTF 20692390 documenting that four SRVs failed their as-found set point tests.  Upon completion of the as-found testing on June 10, 2015, PSEG updated the NOTF documenting that 10 of 14 SRVs had failed their as-found set point tests.  On July 30, PSEG submitted a LER (LER 2015-004-00) for the SRVs set point failures. 
On  August 13, engineering completed two technical evaluations assessing the safety significance of the set point failures and determined that the set point drift did 
Maybe it bounded reactor vessel overpressure and other engineering design limits...but nobody talks about the reduction in that margin for the last decade. Remember an overpressure accident leading to cracking the vessel or bursting a large pipe would be a accident like no other meltdown in the western world.
not impact or challenge the ability of the SRVs to perform their function of relieving reactor vessel overpressure (see Section 4OA3.1).  On August 26, 2015, PSEG submitted a revision to the LER (LER 2015-004-01) to include the associated technical evaluations and impact on SRV operability.  Based on a review of the LERs, technical evaluations, and associated corrective action NOTF, the NRC resident inspectors identified that PSEG did not identify and/or evaluate an apparent adverse trend in as-found set point testing results (see table below).  Specifically, the resident inspectors noted that both the number and
Update May 11 2018: On the step increase of problem, the NRC says they brought it to the attention of Hope Creek. I brought it to the NRC before they knew it.    
magnitude of the RF19 failures represented a step increase compared to the previous four operating cycles (RF15 – RF18).  The resident inspectors discussed this observation with PSEG staff on several occasions and subsequently engaged PSEG senior managers and the PSEG engineering staff on a conference call on September 16, 2015.  This conference call included NRC Region I Division of Reactor Projects and Division of Reactor Safety managers and technical staff.  On November 5, 2015, following the resident inspectors’ additional engagement on the potential adverse trend, PSEG initiated two corrective action NOTFs to: (1) evaluate a possible trend in SRV set point drift magnitude and/or number of valves affected (NOTF 20709653), and (2) evaluate a potential correlation between the number of as-found set point failures and the time interval between SRV removal and SRV testing (NOTF 20709757).  Based on a review of corrective action NOTFs and NOS reports, the inspectors found no evidence that PSEG had identified and evaluated this potential trend prior to NRC engagement. 
RF15 04/09
RF16 10/10
RF17 04/12
RF18 10/13
RF19 05/15
SRV set point failures
6 6 6 5 10
Average set point drift (average of all 14 valves)
3.77% 3.64% 3.30% 2.34% 5.34%
Highest set point  pressure (psig)
1212 1199 1202 1192 1240
Number of valves above 1200 psig
2 0 1 0 5
Approximate average delay in days between SRV removal & SRV test
N/A N/A 20 25 50
Causal analysis Note: significance level  (SL)2 RCE completed in 02/12
SL3 ACE (70096933)
SL3 ACE (70115711)
SL2 WGE (70138789)
SL2 WGE (70161353)
SL4 no evaluation
On February 17, 2016, engineering completed two evaluations (70181904-010 and 70181906-010).  Engineering concluded that no definitive trend could be established based on a review of the as-found set point failures by cycle, SRV location, and set pressure group (i.e., valves set to lift at 1108 psig, 1120 psig, or 1130 psig), with one exception.  Engineering noted that the data showed that the 1108 psig set pressure group had an increasing trend in failures after cycle 14.  Engineering initiated an action item to perform a more detailed trend analysis of the 1108 psig group by specific pilot valve serial number and critical as-found dimensions (70181904-060).  In the evaluation, engineering concluded, that although the H1R19 test results show a significant increase in failures compared to H1R18, the failure rate does not represent an adverse trend and the single H1R19 data set is not sufficient to declare a trend.  The inspectors noted that engineering’s evaluation did not fully evaluate the possible trend in SRV set point drift magnitude (note from the table above that the average set point drift more than doubled when compared to the RF18 data).
Engineering reviewed the test data for RF17 through RF19 from the table above and concluded that an extended time interval between SRV removal from the plant until as found set point testing can adversely impact the results (number of set point failures).  Engineering initiated an action item to expedite SRV as-found testing in RF20 to further evaluate and assess the potential adverse trend in the RF19 failure rate (70181904-050).  The inspectors noted that the data supported engineering’s  conclusion regarding the impact of a time delay before testing.  Based on an OE review, the inspectors also noted that a Pilgrim Nuclear Power Station LER (LER 2004-001-00) attributed three 2-stage SRV pilot valve failures due to a significant delay in performing as-found testing.  The inspectors noted that the data suggests that significant delays prior to testing may result in more failures and a higher average set pressure.  However, the data also showed that the corrosion bonding phenomenon adversely impacted SRV pilot valve set pressures during the operating cycle as some valves failed even when tested within a few days of removal.  Thus, expediting the as-found testing would not eliminate corrosion bonding induced test failures; however, it may reduce the number and magnitude of the overall failures and result in as-found test results that more accurately reflect SRV pilot valve performance during the operating cycle.
The inspectors noted that engineering’s evaluation did not assess a potential correlation between time delays on the front end of the cycle and the failure rate (including magnitude).  Specifically, potential significant time delays between completing the required as-left +/- 1 percent testing and installing the pilot valves back into the plant and the potential impact on as-found failure rate at the end of the operating cycle.  The inspectors reviewed the data for RF18 and RF19, and concluded that there was no correlation on the front end.  
The inspectors noted that the significant step-change in SRV pilot valve as-found test results from the RF19 testing represented a CAQ.  Based on interviews and document reviews, the inspectors determined that PSEG had not identified the condition until prompted by the resident inspectors.  The inspectors determined that PSEG’s not identifying and evaluating the CAQ was a performance deficiency that was reasonably within PSEG’s ability to foresee and correct.  The inspectors evaluated this PSEG performance deficiency in accordance with IMC 0612, Appendix B, “Issue Screening,” and determined that the issue was minor.  This issue was minor because the inspectors did not identify any PSEG and/or NWS deficiency that may have contributed to an increased failure rate, nor any actions that PSEG should take to preclude recurrence prior to RF20.  
Based on a historical review of PSEG’s causal evaluations initiated to evaluate SRV set point drift failures (see table above), the inspectors concluded that PSEG had high confidence in their 2012 RCE, which may have led to not questioning the RF19 as-found test results.  Specifically, the inspectors noted that, following the RCE (completed in February 2012), PSEG initiated a significance level (SL) 2 work group evaluations (WGEs) after RF17 and after RF18, but initiated no causal evaluation after RF19.  In addition, the inspectors noted that on June 5, 2015, PSEG personnel did not provide adequate documentation supporting the CAP Management Review Committee (MRC) decision to screen NOTF 20692390 as SL4 with no associated evaluation, especially considering the number and magnitude of the as-found test failures.  The inspectors noted MRC’s decision, barring any documented justification, was not aligned with PSEG procedure LS-AA-120, “Issue Identification and Screening Process,” Attachment 2 (“Significance Level Guidance”) and Attachment 3 (“Guidance for Determining Evaluation Type”).  The inspectors determined that PSEG’s not following their CAP administrative procedure was a performance deficiency that was reasonably within PSEG’s ability to foresee and correct.  The inspectors evaluated this PSEG performance deficiency in accordance with IMC 0612, Appendix B, “Issue Screening,” and determined that the issue was minor.  Notwithstanding, the inspectors viewed the issue as another missed opportunity for PSEG to self-identify this trend.
Based on the RF19 as-found test results (all second lift tests were within 3 percent of the specified set point, with the average of 1.39 percent), engineering concluded that all ten SRV test failures were also due to the corrosion bonding phenomenon.  The inspectors noted that, based on PSEG and industry OE and RF19 test results, engineering’s conclusion was reasonable.  However, at the time of this inspection,PSEG had not performed internal inspections of any of the SRV pilots removed during RF19 to confirm their theory.  PSEG plans to perform inspections (including subsequent as-left set point testing) of all 14 SRV pilot valves commencing in June 2016 to support Hope Creek’s next RFO (RF20).  
Based on a review of as-left test documentation for all 14 SRVs pilot valves installed in RF17 and RF18 and a sample of SRV pilot assembly inspection records, the inspectors noted that NWS personnel maintained high-quality records that clearly documented the as-found condition, repairs and/or replaced components, the as-left condition, QA acceptance, and procedure compliance.
 2. The station is planning the replacement of the currently installed Target Rock two-stage SRVs with three-stage SRVs that are expected to eliminate setpoint drift events exceeding +/-3% and improve SRV reliability. The replacement is expected to begin in the next planned refueling outage, H1 R21, in the spring of 2018, pending resolution of open technical items with the valve manufacturer. The replacement will take place over several outages in order to replace all fourteen SRVs.

Tuesday, May 08, 2018

Junk Plant River Bend's Secret Fuel Meltdown

Is this the new Trump NRC, the licensees don't have to publically discuss how they damaged fuel.

Honestly, damaged assemblies. Not a damaged assemble. More than 1000 pins in a assembly...



Pg 7

1) The inspectors evaluated a planned maintenance outage implemented to remove damaged fuel assemblies.  Inspection activities occurred from January 8, 2018, to January 31, 2018

Junk Plant Callaway Safety Analysis and Procedures

This could have turned a terrible accident into meltdown. One has no assurance there is no similar issues throughout the industry.  

This is my version of the engineers screwing the control room people. Can you believe this went unaddressed since initial startup? If the licensee can't do their jobs then it is up to the NRC to catch these flaws. Why didn't the CDBI or other special engineering inspection catch them on this years ago? Give them a big fine for not catching it.

Believe me, if you have the big one up in the control room, you are going to all be alone up in the control room. And you know it!!! The NRC and licensees set you up for failure.  
Power Reactor Event Number: 53388
Facility: CALLAWAY
Region: 4 State: MO
Unit: [1] [ ] [ ]
RX Type: [1] W-4-LP
NRC Notified By: JEREMY MORTON
HQ OPS Officer: DAN LIVERMORE
Notification Date: 05/07/2018
Notification Time: 16:31 [ET]
Event Date: 05/07/2018
Event Time: 13:35 [CDT]
Last Update Date: 05/07/2018
Emergency Class: NON EMERGENCY
10 CFR Section:
50.72(b)(3)(v)(A) - POT UNABLE TO SAFE SD
50.72(b)(3)(v)(B) - POT RHR INOP
50.72(b)(3)(v)(D) - ACCIDENT MITIGATION
Person (Organization):
MARK HAIRE (R4DO)

Unit SCRAM Code RX CRIT Initial PWR Initial RX Mode Current PWR Current RX Mode
1 N Y 100 Power Operation 100 Power Operation

Event Text

DISCOVERY OF A CONDITION THAT COULD HAVE PREVENTED FULFILLMENT OF A SAFETY FUNCTION

"On May 7, 2018, during an engineering review of mission time requirements for Technical Specification related equipment, a deficiency was discovered regarding the Emergency Operating Procedure (EOP) guidance for natural circulation cooldown with a stagnant loop. This condition could be the result of a postulated Main Steam Line Break with a loss of offsite power.

"During a natural circulation cooldown with a faulted steam generator, flow in the stagnant reactor coolant system (RCS) loop associated with the isolated faulted steam generator (SG) could stagnate and result in elevated temperatures in that loop. This becomes an issue when RCS depressurization to residual heat removal system (RHR) entry conditions is attempted. The liquid in the stagnant loop will flash to steam and prevent RCS depressurization. In this condition, the time required to complete the cooldown would be sufficiently long that the nitrogen accumulators associated with Callaway's atmospheric steam dumps and turbine driven auxiliary feedwater pump flow control valves would be exhausted. The atmospheric steam dumps and turbine driven auxiliary feedwater pump would not be capable of performing their specified safety functions of cooling the plant to entry conditions for RHR operation. This issue has been analyzed by Westinghouse in WCAP-16632-P. This WCAP determined that to prevent loop stagnation, the RCS cooldown rate in these conditions should be limited to a rate dependent on the temperature differential present in the active loops.

"The WCAP analysis was used to support a revision to the generic Emergency Response Guideline (ERG) for ES-0.2 "Natural Circulation Cooldown." Figure 1 in ES-0.2 provides a curve of the maximum allowable cooldown rate as a function of active loop temperature differential which is directly proportional to the level of core decay heat. At the time of discovery of this condition, Callaway's EOP structure did not ensure that the ES-0.2 guidance would be implemented for a natural circulation cooldown with a stagnant loop.

"Callaway has issued interim guidance to the on-shift personnel regarding this concern and is in the process of revising the applicable EOPs.

"This condition is reportable per 10 CFR 50.72(b)(3)(v) for any event or condition that at the time of discovery could have prevented the fulfillment of the safety function of structures or systems that are needed to (A) Shutdown the reactor and maintain it in a safe shutdown condition, (B) Remove residual heat, or (D) mitigate the consequences of an accident."

The licensee notified the NRC Resident Inspector of this condition.

Wednesday, April 25, 2018

Masslive/Noah Bombard-The Defective Fingerprint Scanner Problem

So I talked to him for the second time yesterday. Basically said he has a tiny news staff and he had two state police stories he is working on. So he says. I guess he has mentioned it to a state trooper and he won't talk about it. It is too weak a story based on only my testimonial. Yet, it is documented in the court documents and it states I was processed though the Russell barracks. He really wants documents about purchasing fraud or a insider information. Honestly, I don't think he has the breath of experience or skills to understand organizational issues. They want is on a silver platter and know work. Well, it was a experiment anyways. Welcome to the world of a whistleblower. The 4th estate is one of our institutions who broke and failing us all.

He told me on outing the state police payroll head's name, it took him a month of hard work. It looks like a waste of time and company resources. He is not the best newspaper manager I ever seen.

It is a weak internet news organization. He never felt trustworthy to me. He wants the high level college boy stories, not the low level trooper that could make all the troopers lives better.

If I was a whistleblower with a important story, I'd never go to these guys.

Remember, these guys probably got a relationship with the state police.

Monday, April 23, 2018

Junk Plant Watts Bar 1&2: Double Red Finding on RHR

Update May 7, 

Mark my words, all of out institutions are breaking down, most disappointingly, the democrats. I trust nothing from any one of our institutions...  

I have no confidence these computer generated safety evaluations are accurate. I am a testing guy. The only thing I would believe is a mock up of the RHR system, then put in the highest concentration of air into the system, plus some extra amount extra, then figure out when severe water hammer begins. 

At the worrying bottom of it all, these guys look so confused over a settled issue. 

"Additional analysis has subsequently been performed and determined that a higher gas accumulation acceptance criteria does not challenge operability. 
The issue here is these problems are so complex, they can reanalyze the problem,   then come up with any conclusion they need.

Engineering Computer simulation is highly susceptible to fraud and corruption. It too complicated but for a extremely small group of highly trained and educated engineers. How can the legal system catch this kind of fraud. The only way you catch it is after a big accident and something occurs unexpected.  
!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!
Power Reactor Event Number: 53356
Facility: WATTS BAR
Region: 2 State: TN
Unit: [ ] [2] [ ]
RX Type: [1] W-4-LP,[2] W-4-LP
NRC Notified By: JUSTIN GALLAGHER
HQ OPS Officer: DAVID AIRD
Notification Date: 04/22/2018
Notification Time: 04:28 [ET]
Event Date: 04/22/2018
Event Time: 02:22 [EDT]
Last Update Date: 05/04/2018
Emergency Class: NON EMERGENCY
10 CFR Section:
50.72(b)(3)(v)(B) - POT RHR INOP
Person (Organization):
ALAN BLAMEY (R2DO)

Unit SCRAM Code RX CRIT Initial PWR Initial RX Mode Current PWR Current RX Mode
2 N Y 100 Power Operation 100 Power Operation

Event Text

BOTH TRAINS OF RESIDUAL HEAT REMOVAL INOPERABLE

"On April 22, 2018 at 0222 EDT, Watts Bar Nuclear Plant (WBN) Unit 2 entered TS [Technical Specifications] LCO [Limiting Condition for Operation] 3.0.3 due to both trains of the Residual Heat Removal System (RHRS) becoming inoperable. During surveillance testing, the gas void values on Emergency Core Cooling System (ECCS) piping common to both trains did not meet acceptance criteria. This caused both RHRS trains to become inoperable. Operations subsequently vented the RHRS to meet the acceptance criteria and exited TS LCO 3.0.3 at 0227 EDT. More frequent surveillances will be conducted to monitor gas void volumes while additional analysis is being performed to determine corrective actions."

The NRC Resident Inspector has been notified.

* * * RETRACTION FROM TONY PATE TO HOWIE CROUCH ON 5/4/18 AT 1455 EDT * * *

"This event is being retracted. The initial report was based on a conservative acceptance criteria for gas accumulation adopted on April 19, 2018 when it was determined that the previously used acceptance criteria for gas accumulation in the ECCS was non-conservative. Additional analysis has subsequently been performed and determined that a higher gas accumulation acceptance criteria does not challenge operability. With a void of less than the acceptance criteria, in the event of ECCS actuation, the system piping support loads will remain within structural limits and the piping system will remain operable. Therefore, both trains of Unit 2 RHRS were operable and the previously reported 10 CFR 50.72(b)(3)(v)(B) event is being retracted.

"The NRC Resident Inspector staff has been informed of this event retraction."

Notified R2DO (Desai) of this retraction.


Update May 1

The Nuclear Regulatory Commission has launched a special inspection into how an excess amount of gas is in the residual heat removal system used to help shut down the reactors at TVA's Watts Bar Nuclear Power Plant near Spring City, Tenn.

Two weeks ago, TVA informed the NRC that revisions to its initial calculations had reduced the acceptable size of a void due to gases in the system that helps cool down the Watts Bar reactors during their shut down. On April 21, the accumulated gas in the Unit 1 system was found to have exceeded the acceptable value, and on April 22, the same observation was made on Unit 2.


The NRC inspectors will review the sequence of events, drawings, calculations and acceptance criteria, walk down portions of the plant's systems, evaluate TVA's response and assess the adequacy of actions to address the causes of the issues. NRC spokesman Roger Hannah said the issue identified by TVA does not warrant having to shut down either of the Watts Bar units and a report on the onsite visit this week is expected by June
Absolutely no excuse for this: 
NRC GENERIC LETTER 2008-01: MANAGING GAS ACCUMULATION IN EMERGENCY CORE COOLING, DECAY HEAT REMOVAL, AND CONTAINMENT SPRAY SYSTEMS

***This is the Trump NRC remember.  

This indicates how bankrupt the NRC is. Why didn't catch this decades ago and upon first startup of unit 2? 

This should be a double red finding. Remember Brown's Ferry RHR issues with a non functioning RHR injection valve. So basically the RHR was non operable for the life of the both plants. They should have gutted out all piping of the RHR and replaced them at a angle where all the air would have accumulated at the highest point in the system. This is a initial design flaw!!!



Power Reactor Event Number: 53349
Facility: WATTS BAR
Region: 2 State: TN
Unit: [1] [2] [ ]
RX Type: [1] W-4-LP,[2] W-4-LP
NRC Notified By: CHARLES BROESCHE
HQ OPS Officer: THOMAS KENDZIA
Notification Date: 04/20/2018
Notification Time: 00:55 [ET]
Event Date: 04/19/2018
Event Time: 19:44 [EDT]
Last Update Date: 04/20/2018
Emergency Class: NON EMERGENCY
10 CFR Section:
50.72(b)(3)(ii)(B) - UNANALYZED CONDITION
Person (Organization):
ALAN BLAMEY (R2DO)

Unit SCRAM Code RX CRIT Initial PWR Initial RX Mode Current PWR Current RX Mode
1 N Y 100 Power Operation 100 Power Operation
2 N Y 100 Power Operation 100 Power Operation


Event Text


UNANALYZED CONDITION RELATED TO EMERGENCY CORE COOLING GAS ACCUMULATION ACCEPTANCE CRITERIA

"On April 19, 2018 at 1944 EDT, Watts Bar Nuclear Plant (WBN) determined that a preliminary analysis shows current acceptance criteria for gas accumulation in the WBN Unit 1 and Unit 2 Safety Injection System (SIS) and Residual Heat Removal System (RHRS) discharge piping may be non-conservative. The surveillances that check void values and allow venting of the systems are to be performed utilizing conservative criteria at more frequent intervals to ensure gas void volumes remain under acceptable limits. Additional analysis is being performed to determine final actions.

"The NRC Resident Inspector has been notified."

Unit 1 BOTH TRAINS OF RESIDUAL HEAT REMOVAL INOPERABLE

"On April 21, 2018 at 2152 EDT, Watts Bar Nuclear Plant (WBN) Unit 1 entered TS [Technical Specifications] LCO [Limiting Condition for Operation] 3.0.3 due to both trains of the Residual Heat Removal System (RHRS) becoming inoperable. During surveillance testing, the gas void values on Emergency Core Cooling System (ECCS) piping common to both trains did not meet acceptance criteria. This caused both RHRS trains to become inoperable. Operations subsequently vented the RHRS to meet the acceptance criteria and exited TS LCO 3.0.3 at 2222 EDT. More frequent surveillances will be conducted to monitor gas void volumes while additional analysis is being performed to determine corrective actions."

The NRC Resident Inspector has been notified.



Unit 2 BOTH TRAINS OF RESIDUAL HEAT REMOVAL INOPERABLE

"On April 22, 2018 at 0222 EDT, Watts Bar Nuclear Plant (WBN) Unit 2 entered TS [Technical Specifications] LCO [Limiting Condition for Operation] 3.0.3 due to both trains of the Residual Heat Removal System (RHRS) becoming inoperable. During surveillance testing, the gas void values on Emergency Core Cooling System (ECCS) piping common to both trains did not meet acceptance criteria. This caused both RHRS trains to become inoperable. Operations subsequently vented the RHRS to meet the acceptance criteria and exited TS LCO 3.0.3 at 0227 EDT. More frequent surveillances will be conducted to monitor gas void volumes while additional analysis is being performed to determine corrective actions."

The NRC Resident Inspector has been notified.