Mr. Mulligan,
I have attached the transcripts from the teleconferences held with you on February 17, 2012, and April 10, 2012, associated with your petition request dated January 24, 2012, regarding Peach Bottom Atomic Generating Station. Per your request during the April 10, 2012, teleconference, a copy of the transcript of that teleconference has been forwarded to the NRC Office of Inspector General.
I also wanted to inform you that the NRC staff is continuing to consider your petition request and is in the process of completing the review of Licensee Event Report (LER) 3-11-03 (ADAMS Accession No. ML11325A383) associated with the failure of the Unit 3, 71B Automatic Depressurization System Safety Relief Valve on 9/25/2011. The NRC staff anticipates that the review of LER 3-11-03 will be completed and addressed in the Peach Bottom 2nd quarter Inspection Report by September of this year, which will be publicly available in ADAMS. Once this LER evaluation is issued, the NRC staff will be able to make a final determination regarding your petition request.
I also wanted to inform you that the NRC staff is continuing to consider your petition request and is in the process of completing the review of Licensee Event Report (LER) 3-11-03 (ADAMS Accession No. ML11325A383) associated with the failure of the Unit 3, 71B Automatic Depressurization System Safety Relief Valve on 9/25/2011. The NRC staff anticipates that the review of LER 3-11-03 will be completed and addressed in the Peach Bottom 2nd quarter Inspection Report by September of this year, which will be publicly available in ADAMS. Once this LER evaluation is issued, the NRC staff will be able to make a final determination regarding your petition request.
Thank you,
John Hughey, Project Manager
NRR / Division of Operating Reactor Licensing
Phone: 301-415-3204
This was dated 2/1/2012 when I first put this on my site...
I made the NRC think and I am sure Exelon...I appreciate the NRC in this.
............
New Updated NRC Vender Issues
Exelon Fourth-Quarter Profit Misses Estimates on Costs, Weather
Jan 25, 2012 Bloomberg: Exelon is seeing profit margin shrink on electricity generated by its 17 nuclear reactors as contracts it signed when power prices were high begin to expire, said Andrew Levi, a New York-based power analyst with Caris & Co. A glut of U.S. gas supplies has cut prices for the power-plant fuel, in turn causing average electricity prices in PJM to fall 38 percent since 2008.
“Power prices in general have fallen off a cliff,” Levi said in a telephone interview before the earnings were released. “Whether it’s Exelon or some of the integrated names, they definitely have some big headwinds to fight.”
Jan 24, 2012
R. William Borchardt
Executive Director for Operations
US Nuclear Regulatory Commission
Washington, DC 20555-0001
Dear Mr. Borchardt,
Request an Emergency Peach Bottom nuclear plants 2 and 3 shutdown to replace all safety relief valves pneumatic actuators buna-n seals with nylon seals…or other high quality and durable materials designed and tested for elevated temperature.
Here are excepts from the License Event Report 05000278 2011-003-00 dated 11/18/2011.
This got to be backwards. So you had a contractor tell you in March the seals are substandard and 6 months later your LER states the apparent cause of a buna-n seal failure was thermal degradation of the thread seal material. And you don’t got the capability to immediately update the valve actuators knowing there are safety deficiencies. Is this a nuclear plant and is this the United States of America, the greatest nation on the planet?
...”There were no actual safety consequences as a result of this event.
“Subsequent review by Engineering personnel determined that the
apparent cause was thermal degradation of the thread seal material. A vendor technical evaluation report was issued in March 2011 and provides recommendations to upgrade the seal with a design that is more resistant to heat related failures.”
Here is Entergy-Vermont Yankee’s LER-02-01 dated 10/25/2010 over troubles with their SRV buna-n. I/we have been nipping at Entergy’s heels over Vermont Yankee and Palisades with many 2.206s. I am one of two 2.206’s over this. The NRC blew me off on this as they always do. Least they allow me to get it down on paper.
“During the 2010 refueling outage, the pneumatic actuators for the four main steam safety relief valves (RV), RV- 2-71 -A, B, C & D, were tested and leakage was identified through the shaft to piston thread seal on three of the four RVs. This leakage, when combined with the RV accumulator leakage, caused two of the four RVs to not meet design actuation requirements and therefore be considered inoperable. Technical Specification (TS)3.6.D requires at least three of the four RVs to be operable for overpressure
...Subsequent material testing of a seal from the same batch lot determined that the apparent cause of the thread seal condition was thermal degradation.”
The idea in a critical nuclear power plant core cooling safety system the material engineers weren’t absolutely sure of the characteristic of the buna-n and couldn’t perfect predict with certainty the life span in the worst temperatures...we are in the realm of Fukushima Daiichi stupidity.
NRC VY Problem and Resolution Inspection 2011-008
You wouldn’t believe all the troubles Entergy’s Palisades plant is having with management...following procedures, adequate process system for following maintenance and fixing problems. Most perplexing is, management showing they actually don’t care what was going on in the site, by paying attention and being intrusive. I got a pending 2.206 on that. They are right up there with being in the top five worst plants in the nation. This is another indication how systemic their problems are and the NRC didn’t care. There computer document system is upside down...
... “The Type 2 actuator has cooling slots, where as the Type 1 actuator does not. These cooling slots were not accounted for when the Type 1 actuator was replaced with the Type 2 actuator and the cooling slots were covered by insulation.”
recommendation did not conduct an appropriate equivalency review on their own. Thus when the Type 2 actuator was used at VY the valve was exposed to higher temperatures which resulted in thermal degradation and air leakage from the actuator.
2) The NRC do a special investigation or equivalent...with contrasting and explaining the similarities and differences between Vermont Yankee and Peach Bottom SRV actuators and seal problems.
3) Need a generic notice on this?
4) That Peach Bottom nuclear plant be immediately shutdown.
5) All safety relief valve seals and actuators be replaced with a design with a sufficient margin of safety before start-up.
6) Request the formation of a local public oversight panel around every plant.
7) A emergency NRC senior official oversight panel with the aims of reforming the ROP.
8) A national NRC oversight panel of outsiders to oversee and report on the agency’s activities. There should be a mixture of professional academic people and capable lay people.
9) I request that President Obama fire Chairman Jazcko and the other Four Horsemen of the Apocalypse NRC Commissioners!
Sincerely,
Mike Mulligan
Hinsdale, NH 03451
steamshovel2002@yahoo.com
1-603-336-8320