Monday, June 03, 2019

Entergy's Got a Busy Southern Fleet Of Regulated Plants

Entergy got rid of their merchant fleet of nuclear Plants, it didn't fix their nuclear plant problems.
Power Reactor Event Number: 54096
Facility: RIVER BEND
Region: 4     State: LA
Unit: [1] [] []
RX Type: [1] GE-6
NRC Notified By: ALFONSO CROEZE
HQ OPS Officer: JEFFREY WHITED
Notification Date: 06/01/2019
Notification Time: 03:15 [ET]
Event Date: 05/31/2019
Event Time: 23:45 [CDT]
Last Update Date: 06/01/2019
Emergency Class: NON EMERGENCY
10 CFR Section:
50.72(b)(2)(iv)(B) - RPS ACTUATION - CRITICAL
Person (Organization):
JASON KOZAL (R4DO)
Unit SCRAM Code RX Crit Initial PWR Initial RX Mode Current PWR Current RX Mode
1 M/R Y 30 Power Operation 0 Hot Shutdown
Event Text
MANUAL REACTOR SCRAM DUE TO LOW REACTOR WATER LEVEL

"At 2345 CDT at River Bend Station (RBS) Unit 1, a manual Reactor scram was inserted in anticipation of receiving an automatic Reactor Water Level 3 (9.7") scram due to the isolation of the 'B' Heater String with the 'A' Heater String already isolated. The 'B' heater string isolation caused loss of suction and subsequent trip of the running Feed Water Pumps 'A' and 'C'. All control rods fully inserted with no issues. Subsequently Reactor level was controlled by the Reactor Core Isolation Cooling (RCIC) system. Feed Water Pump 'C' was restored 4 minutes after the initial trip and the RCIC system secured. Currently RBS-1 is stable and is being cooled down using Turbine Bypass Valves.

"No radiological releases have occurred due to this event from the unit."

The plant is currently under a normal shutdown electrical lineup.

The licensee notified the NRC Resident Inspector.

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