Power Reactor Event Number: 53793 Facility: ARKANSAS NUCLEAR
Region: 4 State: AR
Unit: [1] [] []
RX Type: [1] B&W-L-LP,[2] CE
NRC Notified By: SEAN DAVIS
HQ OPS Officer: DONG HWA PARKNotification Date: 12/18/2018
Notification Time: 15:40 [ET]
Event Date: 12/18/2018
Event Time: 00:00 [CST]
Last Update Date: 12/18/2018Emergency Class: NON EMERGENCY
10 CFR Section:
50.72(b)(2)(iv)(B) - RPS ACTUATION - CRITICAL
50.72(b)(3)(iv)(A) - VALID SPECIF SYS ACTUATIONPerson (Organization):
RYAN ALEXANDER (R4DO)
Unit SCRAM Code RX Crit Initial PWR Initial RX Mode Current PWR Current RX Mode 1 A/R Y 100 Power Operation 0 Hot Standby
Event Text
AUTOMATIC REACTOR TRIP - LOSS OF NON-VITAL BUS
"On December 18, 2018 at 1126 CST, Arkansas Nuclear One, Unit 1 (ANO-1) reactor automatically tripped due to a loss of the A-1, non-vital 4160V bus. All control rods fully inserted. Loss of the A-1 bus resulted in de-energizing A-3 vital 4160V bus. Emergency Diesel Generator #1, K-4A, started automatically and is currently powering A-3 vital bus. Non-vital buses A-2, H-1, and H-2 and vital bus A-4 transferred power automatically to the Startup Transformer #1. Off-site power remains energized and available for ANO-1. The reason for loss of A-1 bus is unknown at this time. Currently, ANO-1 has stabilized in Mode 3, Hot Standby."
Decay heat is being removed by the main condenser using the turbine bypass valves. The loss of the A-1, non-vital bus, is under investigation. The licensee has notified the NRC Resident Inspector and the state.
Whistleblowing can be used as a potent creative tool to help your bureaucracy evolve towards a more enlightened organization. Phone: 1-603-209-4206 steamshovel2002@yahoo.com Note: I constantly update my articles. Comments at the bottom of the article are always welcome!!! Mike Mulligan, Hinsdale, NH
Wednesday, December 19, 2018
Junk Plant ANO Unit 1 Trips Too
See! How overloaded is Entergy with both plants tripped?
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