Thursday, March 30, 2017

Junk plant Browns Ferry: Reactor Protection Sytem Going Cracy On Us

Sounds like a special inspection. It is a disgrace starting up a reactor in this runaway condition.

The pre startup testing is supposed to catch this.

Back to the bad old days???

Facility: BROWNS FERRY
Region: 2 State: AL
Unit: [ ] [2] [ ]
RX Type: [1] GE-4,[2] GE-4,[3] GE-4
NRC Notified By: MARK MOEBES
HQ OPS Officer: BETHANY CECERE
Notification Date: 03/29/2017
Notification Time: 23:36 [ET]
Event Date: 03/29/2017
Event Time: 18:44 [CDT]
Last Update Date: 03/29/2017
Emergency Class: NON EMERGENCY
10 CFR Section:
50.72(b)(2)(iv)(B) - RPS ACTUATION - CRITICAL
50.72(b)(3)(iv)(A) - VALID SPECIF SYS ACTUATION
Person (Organization):
EUGENE GUTHRIE (R2DO)

UnitSCRAM CodeRX CRITInitial PWRInitial RX ModeCurrent PWRCurrent RX Mode
2M/RY1Startup0Hot Shutdown
Event Text
MANUAL SCRAM INITIATED DURING STARTUP

"At 1844 CDT on 3/29/2017, Unit 2 initiated a manual scram due to multiple rods inserting.

"At 1842 during Unit 2 start-up, Intermediate Range Monitor (IRM) 'G' drifted low. The operator adjusted the range down one position with no immediate reaction. At 1844, a spike on IRM 'G' caused a half scram on Reactor Protection System (RPS) 'A' trip system. The half scram was being reset after evaluating no trip condition was present. As the operator reset groups 2 and 3, a trip signal from IRM 'F' was received on the RPS 'B' trip system, resulting in rod insertion for groups 1 and 4. When the operator identified multiple rods inserting, the actions of procedure 2-AOI-100-1 were followed and a manual scram was inserted. Investigation is ongoing.

"All safety systems remained in standby readiness configuration. No Emergency Core Cooling System (ECCS) or Reactor Core Isolation Cooling (RCIC) reactor water level initiation set points were reached. Primary Containment Isolations Systems did not receive an actuation signal and performed as designed.

"This event is reportable within 4 hours per 10 CFR 50.72(b)(2)(iv)(B) 'any event or condition that results in actuation of the RPS when the reactor is critical except when the actuation results from and is part of a pre-planned sequence during testing or reactor operation.' It is also reportable within 8 hours per 10 CFR 50.72(b)(3)(iv)(A) 'any event or condition that results in valid actuation of systems listed in paragraph (b)(3)(iv)(B) Reactor Protection System(RPS) including reactor scram and reactor trip'. This event requires an LER within 60 days per 10 CFR 50.73(a)(2)(iv)(A).

"The NRC Resident Inspector has been notified."

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