It sounds like a coverup as they didn't save the leaking gasket...
Susquehanna Steam Electric
Station 05000-387
Unit 1
EVENT DESCRIPTION
On April 22, 2016 at
approximately 11:25, Unit 1 entered Mode 1.
On April 22, 2016 at
approximately 12:09, Technical Specification (TS) 3.5.3 was entered and the
RCIC [EllS System Identifier: BN] Quarterly Flow Surveillance was performed
with reactor pressure vessel (RPV) pressure at approximately 930 psig.
On April 22, 2016 at
approximately 14:00, a two to three drops per second leak on the 1 F212B, RCIC Turbine
Lube Oil Filter [EllS Component Identifier: FL T], was identified.
On April 22, 2016 at
approximately 16:01, the main turbine [EllS System Identifier: TA] was tripped
due to a seal oil leak on the collector end of the generator [EllS System
Identifier: TB].
On April 22, 2016 at
approximately 20:57, the reactor entered Mode 2.
On April 23, 2016 at
approximately 00:46, the reactor entered Mode 3. RPV Pressure was below 150
psig at approximately 03:00.
On April 23, 2016 at
approximately 03:55, an operability review concluded that RCIC was inoperable
since there was no guarantee that RCIC would meet its mission time with the
identified leak.
On April 23, 2016 at
approximately 06:54, the reactor entered Mode 4.
On April 30, 2016, both
filter elements and all gaskets were replaced. These
actions corrected the leak and RCIC was subsequently declared operable.
The leakage identified on
April 22, 2016 was considered sufficient to require declaring RCIC inoperable.
RCIC was also considered
to have been inoperable prior to the transition to Mode 1. As a result, the condition
was considered a violation of Technical Specification (TS) 3.0.4 and reportable
in accordance with 10 CFR 50.73(a)(2)(i)(B) as a condition prohibited by
Technical Specifications.
CAUSE OF EVENT
The two items replaced
to correct the leak were the gaskets and the filters. The filters
would not cause an oil leak in the system and no deficiencies within the
filters were identified. The gaskets were disposed of prior to the evaluation,
and were the only difference that could have potentially resulted in the oil
leak. Based on this available information, the
direct cause of the leak was determined to be an unidentified gasket issue. A manufacturing defect or
poor seating caused by pressurization are two of the potential gasket issues
that could have caused the leak; however, a
definitive apparent cause could not be determined.
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