So Grand Gulf, Arkansas 1&2 are currently in shutdown. The only one in a legitimate scheduled outage is Arkansas 2?
Come on, they been shutdown for almost three weeks for a leak in a tiny "one" inch line??? What else did they find?
9/30/2016
Power Reactor | Event Number: 52271 |
Facility: ARKANSAS NUCLEAR
Region: 4 State: AR
Unit: [1] [ ] [ ]
RX Type: [1] B&W-L-LP,[2] CE
NRC Notified By: MARK GOHMAN
HQ OPS Officer: STEVE SANDIN | Notification Date: 09/30/2016
Notification Time: 04:01 [ET]
Event Date: 09/29/2016
Event Time: 21:00 [CDT]
Last Update Date: 09/30/2016 |
Emergency Class: NON EMERGENCY
10 CFR Section:
50.72(b)(3)(v)(B) - POT RHR INOP | Person (Organization):
WILLIAM COOK (R1DO)
CHRIS MILLER (NRR) |
Unit | SCRAM Code | RX CRIT | Initial PWR | Initial RX Mode | Current PWR | Current RX Mode |
1 | N | N | 0 | Refueling | 0 | Refueling |
Event Text
UNISOLABLE LEAK ON DECAY HEAT REMOVAL PIPING DUE TO WELD FAILURE ON A 1" COMMON PIPE
"At 2100 CDT on 09/29/16, while in Mode 6, both trains of Decay Heat (Residual Heat Removal) were declared inoperable due to a cracked weld on a 1" common pipe. The leak developed in a USAS B31.7, Class1 pipe at a weld upstream of pressure indication isolation valve DH-1037. The leak is not isolable from the common 8-inch Decay Heat piping and encompasses approximately 1/3 [one third] of the pipe circumference.
"At the time of discovery, the unit was in Lowered Inventory with both Loops of Decay Heat in service. Subsequently, one train of Decay Heat has been secured to reduce the likelihood of crack propagation. One Train of Decay Heat remains in service providing the function of removing Decay Heat and the other train is readily available. The leakage impacts redundant equipment required to fulfill a safety function. In the current condition, both trains are required to be operable to meet Technical Specification LCO 3.9.5, Decay Heat Removal (DHR) and Coolant Circulation-Low water Level.
"This condition is reportable per 10 CFR 50.72(b)(3)(v)(B) for any event or condition that results in a loss of Safety Function associated with the Decay Heat System (Residual Heat Removal System).
"The licensee has notified the NRC Resident Inspector."
The leak is approximately 0.25 gallons per minute and pipe pressure is 140 psi. Compensatory measures are in place and include an individual posted to watch the pipe in case plugging is necessary. Repairs to the pipe will be completed once pipe is able to be drained. |
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