Wednesday, January 09, 2019

“There’s going to be an accident,” he said. “The only question is when and where.”




Sun editorial: 

Former NRC chairman remains clearly opposed to nuclear energy
Wednesday, Jan. 9, 2019 | 2 a.m.

In a perfect world, nuclear energy would be a perfect tool for combating climate change. Nuclear power plants don’t burn fossil fuels, don’t emit greenhouse gases into the environment and don’t speed global warming.

But with the Union of Concerned Scientists and other groups reversing their former opposition to nuclear energy, former Nuclear Regulatory Commission Chairman Gregory Jaczko is going on the offensive to explain why nuclear energy is nowhere near a perfect solution to the climate crisis.

In a new book, Jaczko reiterates his longstanding criticism of the nuclear industry and his opposition to development of traditional nuclear power plants, which he says are unsafe despite technological improvements designed to make them safer.

Exhibit No. 1 in Jaczko’s argument is the Fukushima disaster. While Japan and other countries used nuclear power to limit their carbon emissions, he contends that the catastrophe at Fukushima wiped out environmental gains that Japan made by burning less fossil fuels.

“What happens after Fukushima is they shut down all of their nuclear plants over time,” Jaczko said during a phone interview with the Sun. “So then what did they do? They had to turn to polluting fossil fuels. So you wind up with this solution where it’s kind of boom or bust: You’ve got nuclear power, but once you turn it off then now what do we do? Well, we have to turn to dirty fossil fuels.”

Jaczko said the fundamental problems with development of nuclear energy included that the basic design of plants hadn’t changed and that the industry wouldn’t pay for technological improvements that would reduce the damage from accidents.

A case in point involves eliminating the kind of hydrogen gas blasts that many people likely remember seeing in footage from the Fukushima disaster.

The gas builds up when steam inside the reactor interacts with one of the metals used to contain nuclear fuel. Jaczko said new container materials have been developed that would limit the gas buildup, but the industry hasn’t adopted them because they’re prohibitively expensive.

Meanwhile, he says, the cost of generating electricity through natural gas and renewables is lower in most parts of the country than nuclear generation. Although nuclear proponents point out that renewables can’t provide continual power — turbines don’t generate when the wind doesn’t blow and solar panels don’t generate when the sun isn’t shining — Jaczko calls that argument a red herring. He points to innovations that are making power storage more affordable — not just advancements in battery design but such methods as pumped-storage hydroelectricity, in which water is pumped to a higher elevation during overnight hours when electricity demand is low and then is released to operate turbines during peak hours.

“So to me, the idea that somehow we’re going to preserve these reactors and that’s a climate solution is just wrong,” he said.

Then, of course, there’s the issue with nuclear waste — a hazard we’re familiar with in Southern Nevada. Jaczko, whose concerns about the proposed Yucca Mountain nuclear waste repository were a leading reason he was hand-picked for the commission by former Sen. Harry Reid, hasn’t grown any fonder of the waste facility since he left the commission. He continues to be alarmed about the long-term safety of the site and the prospect of transporting high-level waste from across the country to Nevada.

Jaczko’s bottom-line assessment is that despite decades of development, nuclear energy remains too hazardous and costly to be a viable source of power.

“There’s going to be an accident,” he said. “The only question is when and where.”

It’s a compelling argument, and anyone who may be warming to nuclear energy in the fight to reverse climate change should examine it. The book, “Confessions of a Rogue Nuclear Regulator,” is available now at Amazon, Barnes & Noble and other outlets.

Tuesday, January 08, 2019

NRC: Controlling Bad Behavior On Plant Employees Through One Papercut After Another

It snowing outside my house. Entergy has more Confirmatory Orders than all the snowflakes on the roof of my house. Entergy has more orders than anyone else in the industry. Basically obsolete equipment and not enough funding to keep all their obsolete plants in good order. Sickening and repetitive fleet wide training on ethics, tell the full truth and don't falsify documents. Well, unless it facilitates high capacity factors and make the corporate more profits. A absolution system without doing the hard work to eradicate corruption...    
Subject: Entergy Response to Confirmatory Order EA-17-132/EA-17-153, Element K
Arkansas Nuclear One, Units 1 & 2 Docket Nos. 50-313 & 50-368 License Nos. DPR-51 & NPF-6
Grand Gulf Nuclear Station, Unit 1 Docket No. 50-416 License No. NPF-29
River Bend Station, Unit 1 Docket No. 50-458 License No. NPF-47
Waterford 3 Steam Electric Station Docket No. 50-382 License No. NPF-38
Indian Point Energy Center, Units 2 & 3 Docket Nos. 50- 247 & 50-286 License Nos. DPR- 26 & DPR-64
Palisades Nuclear Plant Docket 50-255 License No. DPR-20
Pilgrim Nuclear Power Station Docket No. 50-293 Renewed License No. DPR-35
References: 1) U.S Nuclear Regulatory Commission (NRG) letter to Entergy (Entergy Nuclear Operations, Inc. and Entergy Operations, Inc.), "Confirmatory Order, NRG Inspection Report 05000416/2017014, and NRG Investigation Reports 4-2016-004 and 4-2017-021," dated March 12, 2018
2) Entergy Nuclear Operations, Inc. and Entergy Operations, Inc. letter to the NRG, "Entergy Response to Confirmatory Order EA-17-132/EA-17-153, Element J," CNR0-2018-00039, dated September 27, 2018
Communications with Site Workers
Between March 3, 2018 and April 11, 2018, communications about integrity were shared from the Chief Nuclear Officer (CNO) and senior site leaders with Entergy employees and contractors. The tool "Nuclear Talk" was used to share the message. A video with the CNO about integrity was also distributed across the fleet. These messages communicated with workers the circumstances leading to this Confirmatory Order, that willful violations will not be tolerated, and, as a result, Entergy will be undertaking efforts to confirm whether others are engaging in such conduct at any of its sites. The communications stressed the importance of procedural adherence, ensuring that documents are complete and accurate, and of potential consequences for engaging in willful violations. The messages were balanced with the recognition that people do make mistakes and when that happens, it is Entergy's expectation that its employees and contractors will identify and document issues accordingly.
Between September 21, 2018 and October 1 O, 2018, Entergy conducted the first semi-annual communications with workers in the Entergy fleet reemphasizing its intolerance of willful misconduct and updating the workforce on the status of compliance with this Confirmatory Order...

Monday, January 07, 2019

Wasterford: Another Entergy's Dog Plant Trip or Manual Shutdown

I don't yet know why they shut down. It occurred on Jan 5. I hope River Bend being at 90% is just shaping the core. Grand Gulf, it is now your turn. It seems they got junk plant Palisades and Pilgrim turned around pretty quick.   
Unit Power
Arkansas Nuclear 1 100
Arkansas Nuclear 2 100
Callaway 100
Columbia Generating Station 100
Comanche Peak 1 100
Comanche Peak 2 0
Cooper 100
Diablo Canyon 1 100
Diablo Canyon 2 100
Grand Gulf 1 100
Palo Verde 1 100
Palo Verde 2 100
Palo Verde 3 100
River Bend 1 90
South Texas 1 100
South Texas 2 100
Waterford 3 0
Wolf Creek 1 100

NRC's Staff In Trouble

We are a week into 2019 and the NRC hasn't put a 2019 link into this important page yet. Waterford tripped, probably shutdown over the weekend. I can't click the 2019 link in order to reference back a few days, to figure out when Waterford tripped?

Power Reactor Status Reports



2010s: | 2018 | 2017 | 2016 | 2015 | 2014 | 2013 | 2012 | 2011 | 2010 |

2000s: | 2009 | 2008 | 2007 | 2006 | 2005 | 2004 | 2003 | 2002 | 2001 | 2000 |

1990s: | 1999 |

Page Last Reviewed/Updated Friday, December 29, 2017

Entergy: Dog Plants Palisades and Pilgrim.

How close are we to collapse of a capacity factor accident. Remember these plants contain many millions of components. The complexity of the machines makes them a difference beast. If you ding the maintenance budget over and over, get away with really less than you need...you might not see any diffidence. There is a delay time on the decline of plant reliability. We are really getting into the realm uncertainty. If you plow a lot of money into the plant, you drastically reduce global uncertainty. Conversely, if you  get a bad unexpectant accident, you might plow a ton of money, training and new people into the plant, but it would take years of this new intensity to even change the bad curve of reliability. And believe me, tons of money into a dog plant, new training, people, the NRC up your ass, this further disrupts the mojo of the staff.

I expect to see a accident the industry never seen before based on financially throttling maintenance, old age and obsolesce, widespread staff disillusionment and the neutered NRC. It is awful seeing the respected officials above you talking utter nonsense with the condition of the plant, the crazy new plant upkeep philosophy. You know these people are better than that. But you got to tow the party line.          
Power Reactor Event Number: 53813
Facility: PALISADES
Region: 3     State: MI
Unit: [1] [] []
RX Type: [1] CE
NRC Notified By: JACOB MILLIKEN
HQ OPS Officer: JEFFREY WHITED
Notification Date: 01/03/2019
Notification Time: 23:57 [ET]
Event Date: 01/03/2019
Event Time: 00:00 [EST]
Last Update Date: 01/04/2019
Emergency Class: NON EMERGENCY
10 CFR Section:
50.72(b)(2)(iv)(B) - RPS ACTUATION - CRITICAL
50.72(b)(3)(iv)(A) - VALID SPECIF SYS ACTUATION

Person (Organization):
ERIC DUNCAN (R3DO)
Unit SCRAM Code RX Crit Initial PWR Initial RX Mode Current PWR Current RX Mode
1 M/R Y 85 Power Operation 0 Hot Standby
Event Text
REACTOR TRIP DUE TO CYCLING OF TURBINE GOVERNOR VALVE

"At 2028 [EST] on January 3, 2019, with the reactor at 85% power, the reactor was manually tripped due to cycling of Turbine Governor Valve #4. The trip was uncomplicated with all systems responding normally following the trip. Investigation of the cause of the valve cycling is ongoing.

"All full-length control rods inserted fully. Auxiliary Feedwater System actuated as designed in response to low steam generator water levels. Operations stabilized the plant in Mode 3 (hot standby). Decay heat is being removed by atmospheric dump valves.

"This condition has no impact to the health and safety of the public.

"The licensee notified the NRC Senior Resident Inspector.

"This event is being reported pursuant to 10 CFR 50.72(b)(2)(iv)(B) and 10 CFR 50.72(b)(3)(iv)(A)."

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Power Reactor Event Number: 53815
Facility: PILGRIM
Region: 1     State: MA
Unit: [1] [] []
RX Type: [1] GE-3
NRC Notified By: PAUL GALLANT
HQ OPS Officer: DONALD NORWOOD
Notification Date: 01/05/2019
Notification Time: 17:30 [ET]
Event Date: 01/05/2019
Event Time: 00:00 [EST]
Last Update Date: 01/05/2019
Emergency Class: NON EMERGENCY
10 CFR Section:
50.72(b)(3)(v)(A) - POT UNABLE TO SAFE SD

Person (Organization):
ANTHONY DIMITRIADIS (R1DO)
Unit SCRAM Code RX Crit Initial PWR Initial RX Mode Current PWR Current RX Mode
1 N Y 31 Power Operation 31 Power Operation
Event Text
POTENTIAL LOSS OF MSIV SCRAM FUNCTION DURING MAIN STEAM LINE ISOLATION VALVE TESTING

"At approximately 1040 EST on January 5, 2019, during evaluation of test results for the 'C' Main Steam Isolation Valve (MSIV), it was determined that closure of three of four
This is getting really dangerous. That is a really bad accident if this occurs...you can certainly count on two or three known other component failures, maybe even poor training showing up, in this accident. 
Main Steam Lines would not necessarily have resulted in a full scram during testing due to failure of a limit switch (LS-6) associated with MSIV-1C while in the test configuration. This condition is being reported as an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(v), 'Any event or condition that could have prevented the fulfillment of the safety function of structures or systems that are needed to: (A) Shut down the reactor and maintain it in a safe shutdown condition.'

"The system was restored from the testing configuration at 1057 EST and the failed trip channel was placed in the tripped condition at 1326 EST thus restoring the design function. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified."