Friday, April 15, 2016

Junk Entergy Has Giant Ethical and Federal Falsifications Issues

How can you not say on the nuclear fleet level is not having systemic ethics and falsification issues. These are just counted from Jan 1, 2016. Entergy has had a ton of fleet ethics training mandated fleet wide over a number of confirmatory letters over falsification in the last few years. Why keep doing the same thing over and over again that never works.  

Bottom line, the NRC thinks broken ethics is just risk insignificant at any level.    
***Entergy agrees to review fire safety at reactors after probe into falsified reports at a Louisiana power plant

Daily Report Staff
April 11, 2016 
Entergy Corp. has agreed to review fire safety measures at all its nuclear reactors after an investigation by federal regulators found that workers at one plant failed to follow rules and falsified records.
Bloomberg reports contract workers at Entergy’s Waterford 3 nuclear power plant in St. Charles Parish falsified reports showing they had performed fire inspections that never occurred between July 2013 and April 2014, according to a statement issued Friday by the U.S. Nuclear Regulatory Commission.
An Entergy supervisor also failed to take action when provided with information of suspected wrongdoing, the agency says. Plant operators are required to carry out periodic inspections to ensure fire doesn’t damage the reactor’s equipment.
The commission’s findings come as Entergy faces renewed scrutiny over its safety record. Last month, nuclear regulators said that.

***Entergy avoids fine in falsified fire report case at Pilgrim Station
By: Matthew Nadler | April 12, 2016
Entergy won’t be fined following the discovery that a former employee falsified fire watch records at Pilgrim Nuclear Power Station.
Pilgrim Station Vice President John Dent, Jr was informed of the decision in a letter from Nuclear Regulatory Commission Acting Regional Administrator David Lew on Tuesday.
The company could have been fined $70,000, according to the letter. However, the NRC credited Entergy with investigating the problem after another employee had expressed concern. The safety officer who falsified the reports was fired and the company reexamined its fire watch procedures.
The security officer at Pilgrim Nuclear Power Station falsified over 200 fire watch records between June 2012 and June 2014. Fire watches are supposed to be done an hourly basis in certain areas of the plant, according to an e-mail from NRC spokesman Neil Sheehan.




***River Bend: SUBJECT: CLOSURE OF INVESTIGATION (014-2014-046)
 January 252016
Dear Mr. Mccann:
This refers to an investigation conducted by the U.S. Nuclear Regulatory Commission's (NRC) Office of Investigations regarding activities at the River Bend Station. The Office of Investigations initiated the investigation to determine whether a former nuclear security officer at Entergy Operations, Inc. 's River Bend Station, St. Francisville, Louisiana, willfully falsified training records by taking tests for other River Bend Station nuclear security officers, and if River Bend Station security supervisors and managers willfully provided answers to test questions and requested and allowed the former nuclear security officer to take tests for other nuclear security officers.
Based on the evidence developed during the investigation, the allegation that a former River Bend Station nuclear security officer willfully falsified training records by taking tests for other River Bend Station nuclear security officers was not substantiated…

Junk Plant River Bend: Unprecedented 8 LERs since Jan,1 2016

Junk Plant River Bend: Unprecedented 8 LERs since Jan,1 2016 

Junk Plant River Bend: Intentionally Starting Up With a Dead Rod

05000458

I doubt this plant is designed for finding something wrong with a rod, calling it inop, and then intentionally starting up with the dead rod until the next refueling period. Is is plainly unprofessional.\
The causal analysis for this event will be completed when the control rod can be removed for inspection during the next refueling outage. The results of that investigation will be provided in a supplement to this report.
We are getting a lot of exotic LERs out of these guys.
I doubt the NRC disclosed whats going on in their inspection report? 
They don't tell us what is wrong with the rod. They kinda make believe they don't know what caused this. I believe they know what is wrong. I wonder why they don't disclose it? The idea they don't fully know what is wrong with the rod is mind boggling. How do they know this problem won't effect different rods. 
River Bend: Operations Prohibited by Technical Specifications Due to Reactor Control Rod Drift During Core Alterations
On January 19, 2016, at 5:28 a.m. CST, while conducting core alterations, an alarm was actuated in the main control room alarm indicating that a' reactor control rod had drifted out of the fully inserted position. At the time, a fuel bundle was being raised out of the core, and the control rod in the same cell drifted out one notch with no "withdraw" command present. This condition actuated a corresponding alarm on the refueling platform, and system interlocks stopped the platform hoist with the fuel bundle partially withdrawn. When the control rod moved from the fully inserted position, the Technical Specification applicability for the intermediate range neutron monitoring system was inadvertently entered, while a certain function of those instruments was not operable. This event constituted operations prohibited by Technical Specifications, and is being reported in accordance with 10 CFR 50.73(a)(2)(i)(B). After a detailed assessment of the situation, the fuel bundle and the control rod were returned to their original positions. The drive mechanism for the control rod has been disabled, and the control rod will remain fully inserted for the remainder of the current fuel cycle. The causal analysis for this event will be completed when the control rod can be removed for inspection during the next refueling outage. The results of that investigation will be provided in a supplement to this report.

Thursday, April 14, 2016

Worst Job In USA: Newspaper Reporters

It is the only people I hate, except drug cartel leaders. Ok, I like heroin drug dealers better than newspaper reporters amd main media reportors.
Newspaper reporter named nation's worst job...again
eporters might not work with chainsaws or automatic weapons, but their job is worse than a logger or an enlisted soldier according to CareerCast.com's latest study. 
The job search and job ranking site has rated different jobs and careers through a variety of metrics since 1988. For the second straight year, newspaper reporter took the unwanted classification as the "worst job of 2016," with CareerCast citing a decline in print subscriptions and declining ad revenue leading to fewer job prospects and unfavorable pay.  
Other media jobs also made the worst list, including broadcaster at No. 3 and disc jockey at No. 4. The only thing worse than those two is logger or lumberjacks, which came in just behind reporter. Enlisted military personnel came in fifth, just behind disc jockey.

Junk Plant Plant: Permanent Shutdown May 2019

Well, at least they will be under intense scrutiny with the paper-whipping NRC.

The NRC requiring them to shutdown would give the agency instant cred? 

With the serious electricity over supply according to the NEISO ($25.25 megawatt watt-hour today)...there is no need of the plant.     
Closing date set for Pilgrim nuclear power plant

By David Abel and John R. Ellement Globe Staff 
The company that owns the Pilgrim Nuclear Power Station said Thursday that it intends to refuel the power plant next year and continue operating for three more years.
Officials at Entergy Corp. said the plant in Plymouth will close on May 31, 2019. 
The company had been weighing whether to shutter the plant next year -- as critics had hoped it would -- before it undergoes an expensive refueling process. 
The decision means that Pilgrim’s 609 employees will continue to work there until the plant closes, but activists also say it means Entergy will continue operating one of the nation’s least-safe reactors. 
“We’re pleased that we will be able to keep our team of hardworking, professional employees actively engaged in safe operations for the next three years and in a return to regular NRC and industry oversight,” said John Dent, Pilgrim’s vice president, in a statement posted on the company’s website. 
Local activists have long opposed the plant’s continued operations and said they worry that Entergy is more concerned about its finances than public safety. 
“The bottom line is that this decision is about Entergy’s pocketbook, not about public safety,” said Mary Lampert, director of Pilgrim Watch, a longtime critic of the plant. “This is an old plant, and Entergy is unwilling to spend the money to fix the problems, and the NRC is allowing them to do that. That means we’re in a heightened period of risk.” 
Last October, Pilgrim announced it would close no later than June 2019, after supplying power to more than a half-million homes and businesses for four decades. The announcement came a month after the US Nuclear Regulatory Commission designated Pilgrim one of the nation’s three least-safe reactors. 
Company officials have said they decided to close the plant because of the plummeting price of a competing fuel, natural gas, and the reluctance of federal and regional officials to provide financial incentives for nuclear power plants. 
On Monday, company officials said they decided to refuel the plant because it was the best way to fulfill their commitments to provide power to the region’s electrical grid. The plant was obliged to provide power through 2019.
“This was the most viable way for us to do that,” said Patrick O’Brien, a Pilgrim spokesman. 
The decision to continue operating for another three years means that Pilgrim will undergo its last refueling in the spring of 2017. The plant must cease operations while it refuels every other year. 
The 2015 refueling outage resulted in a $70 million investment in the plant and hundreds of contractors, Entergy officials said. 
The company said it would release a plan to decommission the plant within two years after shutting down, as required by the NRC. 
The 680-megawatt plant, which opened in 1972, generates enough electricity to power more than 600,000 homes.
David Abel can be reached at dabel@globe.com. Follow him on Twitter @davabel.

Wednesday, April 13, 2016

Junk Plant Pilgrim: Two DGs Inop

You would think they would inspect the good DG before they removed they removed the bad one. 130 drops per minute is a big leak. 

Facility: PILGRIM
Region: 1 State: MA
Unit: [1] [ ] [ ]
RX Type: [1] GE-3
NRC Notified By: MIKE MCDONNELL
HQ OPS Officer: JEFF HERRERA
Notification Date: 04/12/2016
Notification Time: 07:47 [ET]
Event Date: 04/12/2016
Event Time: 00:50 [EDT]
Last Update Date: 04/12/2016
Emergency Class: NON EMERGENCY
10 CFR Section:
50.72(b)(3)(v)(D) - ACCIDENT MITIGATION
Person (Organization):
JOHN ROGGE (R1DO)

UnitSCRAM CodeRX CRITInitial PWRInitial RX ModeCurrent PWRCurrent RX Mode
1NY100Power Operation100Power Operation
Event Text
LOSS OF BOTH EMERGENCY DIESEL GENERATORS

"On April 12, 2016, with the reactor at 100 percent power and the mode switch in RUN, Pilgrim Nuclear Power Station entered an unplanned 24-hour Limiting Condition for Operation (LCO) action statement due to both emergency diesel generators (EDG) being inoperable (Technical Specification 3.5.F.1). At 0050 [EDT] this morning, with EDG B out of service for a planned LCO maintenance window, EDG A was declared inoperable due to a 130 drop per minute leak on a line to a jacket water pressure indicator.

"Repairs to EDG A are underway at this time.

"The following plant equipment has been verified operable: both 345 Kv transmission lines; 23kV transmission line; Station Blackout EDG.

"This condition is reportable to the NRC Staff as an Event or Condition that Could Have prevented Fulfillment of a Safety Function (Mitigate the consequences of an accident) under 10 CFR 50.72(b)(3)(v)(D), and requires an 8-hour notification.

"The licensee has notified the NRC Senior Resident Inspector.

"The licensee will notify the Commonwealth of Massachusetts."

Tuesday, April 12, 2016

Junk Plant Wolf Creek: Appalling Sense of Safety with Emergency DG

Power Potential Transformer Overloading Results in Emergency Diesel Generator lnoperability

On October 6, 2014, at approximately 1326 Central Daylight Savings Time (CDT) during a scheduled 24-hour Run, the 'B' Emergency Diesel Generator (EOG) unexpectedly tripped and a fire was observed in the electrical cabinet (NE106). This resulted in an unplanned entry into a 72 hour shutdown Limiting Condition of Operation (LCO) and an ALERT emergency classification. The source of the fire was the Power Potential Transformer (PPT). On 1/28/16, a Hardware Failure Analysis concluded that the failure of the PPT was most likely due to overloading which resulted from failure of a diode in the power rectifier of the EOG excitation system. Failure of the diode mostly likely occurred during load transients on June 11, 2014. 
The station did not have the ability to assess the degradation of the PPT within the EDG's excitation system that led to the continual operation of a degraded component, resulting in significant equipment failure. Additionally, there were limited preventative maintenance, obsolescence issues that had not been addressed, limited knowledge of the exciter, and the design of the system lacked overcurrent protection/detection of the PPT. The station continued using the PPT after it was identified as degraded on June 11, 2014. When the smoking was first identified, the PPT was determined to be degraded, but could still perform its safety function due to the EDG satisfactorily performing its surveillances. 
The 'B' EOG was most likely inoperable from June 11, 2014 until October 9, 2014. During that time period, the 'A' EOG was taken out of service for maintenance on July 21, 2014, creating a condition where both trains may have been inoperable. When the 'A' and 'B' EDGs are inoperable, there are no remaining safety related on-site stand-by AC…

Sunday, April 10, 2016

Junk Presidential Candidate Clinton?

I stand by my opinion, she doesn't know now to wheel power to make America better. She and her buddy husband know how to wheel power pretty good in order to get campaigne contributions and then build ex presidential Cathedrals.
Why do I get the idea ex president Clinton hasn't grown much in the ensuing years after his presidency...he is stuck in the same old image.   


New York nuclear plant's future further divides Sanders and Clinton 

Clinton: “I want the federal government to regulate much more toughly than we have in the past,” she said on Monday. 
In 2014 Cuomo signed a law that banned fracking in New York

Junk Plant Cook: "There were a few fires"

Transformer fails, oil spills at Cook

Posted: Sunday, April 10, 2016 6:00 am

Transformer fails, oil spills at Cook By HP Staff The Herald-Palladium | 0 comments

BRIDGMAN — Crews are cleaning up oil at the Cook Nuclear Plant after 2,000 gallons overflowed a berm after a transformer failure, plant officials reported Saturday. Plant spokesman Bill Schalk said there is no impact on production, the transmission grid or customers. Unit 1 is in a scheduled refueling outage and Unit 2 is continuing to produce at full capacity.

The large transformer, which failed Friday afternoon, is stationed between two transmission switchyards and holds 30,000 gallons of cooling oil, Schalk reported. Most of the spill was contained in the berm.

Cook Environmental Manager Jon Harner stated in the news release that none of the oil reached storm drains or Lake Michigan.

“We fully expect to recapture all of the oil and fully restore the area,” he said.

The Cook Fire Brigade, Indiana & Michigan Power Co. transmission workers and local fire departments monitored the transformer overnight as cleanup began, the plant reported. The Michigan Department of Environmental Quality, the Nuclear Regulatory Commission and Berrien County Emergency Management was notified.

“There were a few fires that were quickly extinguished as the transformer drained and cooled,” plant officials stated in a news release.


What caused the transformer failure has not been determined, the plant reported.

Friday, April 08, 2016

The Elephant In The Room: With Junk plants Indian Point’s Baffle-Former Bolts.

It takes extraordinarily rare and highly highly specialized skills to completely disassemble a core to inspect and replace the baffle bolts. It is going to be a black hole looking down the core barrel anyway you look at it. Who knows what you will find in theere?  I’d like to see waiting list for these expensive services. It is outside venders they have to bring into the plant.  

The question the NRC fears most is the blow back from the powerful politicians in congress. The times and risk demand the shutdown and inspections of numerous plants. How many plants do you want on the waiting list cooling their heels shutdown and losing millions of bucks a day? That is a lot persuasion campaign contribution bucks.  
***Best strategy for the NRC: delay, delay, delay and secrecy up the ying yang…
*** What Entergy fears most is information will trickle out little by little horrendously damaging the industry and themselves. So they want to disclose the least they can and get the bad news out all at one time.

 





Unable To Compete On Price, Nuclear Power On The Decline In The U.S

Originally published on April 7, 2016 8:11 pm 
Renewable energy and new technologies that are making low-carbon power more reliable are growing rapidly in the U.S. Renewables are so cheap in some parts of the country that they're undercutting the price of older sources of electricity such as nuclear power. 
The impact has been significant on the nuclear industry, and a growing number of unprofitable reactors are shutting down. 
When the first nuclear power plants went online 60 years ago, nuclear energy seemed like the next big thing.
In many ways, it lived up to that promise. It turned out to be remarkably safe and reliable and clean. It's carbon-free and is the source of about 20 percent of the country's electricity.
 
But right from the start, people in the nuclear industry struggled with a big problem: cost. Making nuclear power cheap was the Holy Grail. 
It never panned out. Nuclear plants keep coming in over-budget. And after the Fukushima disaster in Japan in 2011 — when three nuclear reactors melted down after an earthquake and tsunami hit — companies were forced to spend millions of dollars more on safety equipment to keep older plants operating. 
"It would be very difficult for any company to make a decision to try to build a new nuclear plant," says Mike Twomey, a spokesman for Entergy Nuclear, which runs nuclear power plants. 
Entergy has already taken one unprofitable reactor offline in Vermont and plans to close two more plants that are losing money in upstate New York and Massachusetts.
In all, 19 nuclear reactors are undergoing decommissioning, of which five have been shut down in the past decade, according to the U.S. Nuclear Regulatory Commission.
 
The main reason behind the wave of closures is a new generation of cheap, gas-fired power plants that has pushed the wholesale price of electricity into the basement. 
But Mycle Schneider, a nuclear industry analyst, says nuclear also faces growing price pressure from wind and solar. Renewable energy is so cheap in some parts of the U.S. that it's even undercutting coal and natural gas.
"We are seeing really a radical shift in the competitive markets which leave nuclear power pretty much out in the rain," Schneider says.
 
Over the past decade, no new nuclear power plants have begun commercial operations in the U.S.; the last reactor to start up in the U.S. was in Tennessee in 1996 (another unit at the same plant is expected to come online sometime later this year). 
There are a handful of new nuclear reactors under construction in the South, where energy markets are still highly regulated. Big power authorities there don't face the kind of head-to-head competition that has revolutionized energy markets in other parts of the country. 
But even within the nuclear industry itself, a growing number of experts agree that the U.S. has reached a pivot point, where new nuclear power plants are just too expensive. 
"We think that the costs of new nuclear right now are not competitive with other zero-carbon technologies, renewables and storage that we see in the marketplace," says Joe Dominguez, executive vice president for governmental and regulatory affairs and public policy at Exelon, a nuclear power company that has announced plans to close one of its existing reactors in New Jersey. 
Three other plants that are losing money in Illinois and upstate New York are also being reviewed for possible closure, Dominguez says. 
"Right now we just don't have any plans on the board to build any new reactors," he says. 

Companies like Exelon and Entergy hope state governments will agree to subsidize their existing reactors, paying a premium for low-carbon nuclear power in the same way they now subsidize wind and solar.
 
The companies say the steady power generated by nuclear still pays an important role stabilizing the nation's energy grid.
But America's reactors are aging. The average is now 35 years old. With the new investment going to natural gas and increasingly to wind and solar, the old energy of the future may soon be eclipsed by the new energy of the future. 

Junk Plant River Bend: Jesus Christ, More Crappy Capacity Factor.

I been talking a lot on this blog for the past year identifying River Bend’s poor and unprofitable capacity factor.

They have gone back down 65% power today. Probably have to monitor these guys for a month as they squeak up 1% by 1% per day. It will probably take them 45 days to return to 100% power.  

Bets on if they will scam before that?
 
I am just saying, the NRC will send them another special inspection team before they get up to 100% power :) 

One good thing going on for Entergy today, at least the last standing Indian Point plant is still up at power. Going to check to see if it is still at 100% power.

Yep, still at 100% power.  


Junk Plant Grand Gulf: Crappy Capacity Factor

Just got out of outage, took forever to get up to 100% power. My bad, took forever to get up to 93% power and now down to 74% again.


Huffing and puffing to get up to the top of the 100% power mountain.  

Junk Gov Corp TVA: Soiled Underwear Of Staff At Browns Ferry

Usually this comes from long term problems of maintenence with the automated obsolete equipment that washes and reinstalled the resin in the condensate deminerizer. This contradicts anything risk perspective, as this non safety condemin malfunction triggered 1979 Three Mile Island. But you had to have a lot of maintenance problems to create core rubble at TMI. The PWR's pressure operated relief valve (PORV)are very similar valves as the BWR's SRV valves but at a lot higher water pressure. 

This is the first time I remember a notification of high radiation cause by resin intrusion. This had got to be a lot a resin in the reactor. Usually they get a lot of smaller intrusions until the big one. 


Junk condensate deminerizer filter system causes loss of feed system and scram in 2009. These are amazingly complex mechanical and electronic system for being a non safety system. That is why it bites them in the ass over and over again.   

Unit 3 also: Licensee Event Report 50-29612009-001


Reactor Shutdown as a Result of a Chemistry Excursion

On March 18, 2007, while operating at 28% power, a chemistry excursion occurred shortly after Condensate Filter Demineralizer 1T-13D was placed in service. The magnitude of the chemistry
excursion required operators to shutdown the reactor in accordance with abnormal operating procedures and plant chemistry procedures. As a result of inserting the manual scram, Primary Containment Isolation System (PCIS) groups 2, 3, and 4 isolations occurred when reactor water level dropped below 170 inches. All isolations went to completion. The reactor water level decrease is normal following a scram from 28% power due to void collapse in the reactor vessel. Reactor water level was subsequently restored to normal and the PCIS group isolations were reset.


Troubleshooting subsequently determined that the chemistry excursion was the result of resin intrusion from Condensate Filter Demineralizers into the Condensate System.


Facility: BROWNS FERRY
Region: 2 State: AL
Unit: [ ] [ ] [3]
RX Type: [1] GE-4,[2] GE-4,[3] GE-4
NRC Notified By: MATTHEW SLOUKA
HQ OPS Officer: JEFF HERRERA
Notification Date: 04/06/2016
Notification Time: 17:07 [ET]
Event Date: 04/06/2016
Event Time: 15:45 [CDT]
Last Update Date: 04/07/2016
Emergency Class: UNUSUAL EVENT
10 CFR Section:
50.72(a) (1) (i) - EMERGENCY DECLARED
50.72(b)(2)(xi) - OFFSITE NOTIFICATION
Person (Organization):
REBECCA NEASE (R2DO)
BERNARD STAPLETON (IRD)
BILL DEAN (NRR)
CATHY HANEY (R2RA)

UnitSCRAM CodeRX CRITInitial PWRInitial RX ModeCurrent PWRCurrent RX Mode
3NY100Power Operation91Power Operation
Event Text
UNUSUAL EVENT DECLARED DUE TO MAIN STEAMLINE HIGH HIGH RADIATION CONDITION

At 1545 CDT on 04/06/16 Browns Ferry Unit 3 declared and exited the declaration of an unusual event due to a main steam line high high radiation condition. Power to Unit 3 was reduced to 91 percent power. The high radiation condition alarm cleared at 1526 CDT. Browns Ferry Unit 3 reported that the high radiation conditions were due to resin intrusion from the condensate demineralizers into the reactor and hydrogen water chemistry was a potential contributor to the event. The cause is still under investigation.

The NRC Resident Inspector has been notified.

State and Local notifications were made.

Notified DHS SWO, FEMA Ops Center, NICC Watch Officer, FEMA NWC and Nuclear SSA (email).

* * * UPDATE FROM BILL BALL TO DANIEL MILLS AT 0034 EDT ON 04/07/2016 * * *

"At 1941 [CDT] BFN [Brown's Ferry] determined this notification to be potentially newsworthy due to receiving notification that counties [surrounding the plant] were alerted of this event. No plant conditions changed."

The licensee may issue a press release.

The licensee will notify the NRC Resident Inspector.

Notified R2DO (Nease).

Wednesday, April 06, 2016

Junk Presidential Candidate Clinton On Indian Point

This must be her Benghazi answer on Nuclear Power. This is why things are the way they are. Didn't she, her husband or the foundation accept huge speaking fees from Entergy. "Huge"! She should have said, if they violate any rules, we should give the NRC humongous power to inflict a terrible price to make them toe the line.
Don't forget, she is a pawn of Russian Putin's uranium trading and centrifuging business! 
Isn't that just terrible, benignly calling for oversight...not talking about the NRC massive reform. Why isn't she criticizing the NRC. She has a green light with the Gallup nuclear power public disapproval rate.

She doesn't know how to wheel power or get involved. It is anybody but Clinton in my house of woman teachers. I like Trump because he is such a system disruptor.




ALBANY — Hillary Clinton said she wants more review of the Indian Point nuclear facility but stopped short of calling for its closure. 

That’s in contrast to her presidential primary opponent, Sen. Bernie Sanders, who has called for its closure. 

“I’m glad he’s discovered Indian Point,” Clinton said Monday in an interview with "Capital Tonight’s" Liz Benjamin. “When I was a senator, I went after oversight; I went after safety.” 

Earlier Monday, Sanders had called Indian Point a “catastrophe waiting to happen," referring to the recent revelation that the plant had faulty bolts, and called for it to close.
Clinton said she had a history of calling for more oversight of Indian Point, from her time as a U.S. senator. 

Gov. Andrew Cuomo has repeatedly called for the closure of the plant because of its proximity to New York City. He has said there is no way safely to evacuate 20 million people in the greater New York City region who could be affected during a catastrophic accident. 

Clinton said Indian Point cannot easily be replaced, since it provides such a significant amount of power for New York. 

“There’s a current Nuclear Regulatory Commission study being undertaken, but we also have to be realistic and say, you get 25 percent of the electricity in the greater New York City area from Indian Point,” she said. “I don’t want middle-class taxpayers to see a huge rate increase, so this has to be done in a careful, thoughtful way.

Tuesday, April 05, 2016

Junk Plant Hatch Unit 2 2015 SRV testing report.

Hey Hatch: I know how to get you inexpensively though two or three cycles with leaking and testing failure prone SRV problems. Tell the NRC you diamond coated the pilot disc??? 
It doesn't matter you don't have the engineering evidence to prove diamond coating works? :)
Then go to coated pilot disc valves with: 
Rhodium
Ruthenium 
Iridium
It will get you to 20 years of reckless plant operation. 
If this 2 stage and 3 stage SRV thing doesn't get you confused, then something is wrong with. What was the first model SRV put in these plants when new? The 3 stage SRVs was put in new plant, the much improved design was the 2 stage model? Basically leaking and unreliability drove the industry into the much improved design with the 2 stage.   

I had a insider tell me Target Rock hasn't been making new SRVs for many decades. When a 2 or 3 stage SRV irreparably breaks, they just get old valves from the nuclear plant junk yards and get repair parts from China to refurbish them.    
LER 2-2011-002, identified multiple SRV setpoint drift for 8 of the 11 SRVs. Corrective actions included replacement of the 2-stage SRVs with 3-stage SRVs during the Unit 2 Spring 2011 refueling outage which was considered at that time to be the long term fix for this corrosion bonding issue. Subsequent to that outage the 3-stage SRVs exhibited signs of unacceptable leakage which resulted in two separate outages that involved changing out four SRVs during the first outage and the remaining seven SRVs during the subsequent outage in May 2012. The 3-stage SRVs were replaced with 2-stage SRVs containing pilot discs that had undergone the platinum surface treatment.
This is last years unit 2 SRV testing report. The problem valves today are in unit 1. 

I  talked extensively to the senior resident at Hatch. He was amazingly open to me. He is the guy in charge of collecting the operating record on the industry and Hatch SRVs for the special inspection. He told me two valves went bad on lift point setpoint accuracy and two other valves didn't fully open or close leading to the special inspection. We talked all about the finding at Pilgrim and the part 21 report. He seems to think the test stand damage before installation causing component damage at Pilgrim has been ruled out. They did all sort of pre-installation inspection especially angled for preventing the Pilgrim problem.    

It is either on one or the second SRV going outside tech specs is where Hatch needs to shutdown to fix the valves. They can't see the damage at power.
Safety Relief Valves As Found Settings Resulted in Not Meeting Tech Spec Surveillance Criteria

On May 11, 2015 at approximately 0923, Unit 2 was at 100 percent rated thermal power (RTP) when the "as-found" testing results of the 2-stage main steam safety relief valves (SRVs) were received which indicated that two of eleven of the Unit 2 SRVs had experienced a setpoint drift during the previous operating cycle which resulted in their failure to meet the Technical Specification (TS) opening setpoint of 1150 +1- 34.5 psig percent as required by TS Surveillance Requirement (SR) 3.4.3.1.

The root cause of the SRV setpoint drift is attributed to corrosion-induced bonding between the pilot disc and seating surfaces. This conclusion is based on previous root cause analyses and the repetitive nature of this condition at Hatch and within the BWR industry. All 2-stage SRVs with platinum coated pilot seats were removed from Unit 2
So here is where they put all 3 stage valves into the plant. This is crazy as hell. Five years earlier in LER 2-2011-002 Hatch experimentally put in all 3 stage relief as a solution to fix the massive setpoint inaccuracies. Before the next outage, they had massive leakages and two shutdowns over the defective 3 stage that also failed at Pilgrim. They yanked the 3 stage out of the plant and reinstalled the 2 stage. Now in 2015 they reinstalled the 3 stage in Unit 2 and unit 1 has multiple 3 stage SRV failures to operate and two having violated tech specs over setpoint inaccuracies.

Notice the below phrase below in 2011; "replaced with 3-stage SRVs with a modified pilot, 3-stage SRVs typically do not exhibit set point drift". These SRV LERs are riddle with uncontested deception and fraud. Were is the evidence this is accurate: "replaced with 3-stage SRVs with a modified pilot 3-stage SRVs typically do not exhibit set point drift".  They stuck the 3 stage in the plant for one cycle and in the 2016 SRV LER not yet put out, it is going to say their were two SRVs who didn't pass their setpoint lift accuracy. It all gaming difinision of words in order to make money.   
during the 2015 refueling outage and replaced with 3-stage SRVs with a modified pilot. 3-stage SRVs typically do not exhibit set point drift and the modified pilot reduces instances of vibration induced spurious openings and leak-by.

A 3-stage SRV with a similar modified pilot was installed on Unit 2 during the ·2013 refueling outage. Based upon "as-found" testing results, it was seen that pressure lift setpoints were maintained during plant operation.

DESCRIPTION OF EVENT

On May 11 2015, at approximately 0923, with Unit 2 at 100 percent rated thermal power (RTP), "as-found" testing of the 2-stage main steam safety relief valves (SRVs) (EllS Code RV) showed that two of the ten main steam SRVs that were tested had experienced a drift in pressure lift setpoint during the previous operating cycle such that the allowable technical specification {TS) surveillance requirement (SA) 3.4.3.1 limit of 1150 +1- 34.5 (+/- 3%) psig had been exceeded. Below is a table illustrating the as found testing results of Unit 2 SRVs that were removed from service during the Spring 2015 refueling outage and replaced with 3-stage SRVs.

MPL Pilot Serial No. Lift Pressure Percent Drift
2B21-F013B 1006 1155 0.40%
2B21-F013C 1231 1172 1.90%
2B21-F013D 303 1184 3.00%
2B21-F013E 315 1210 5.20%
2B21-F013F 1189 1179 2.50%
2B21-F013G 302 1174 2.10%
2B21-F013H 1230 1190 3.50%
2B21-F013K 1229 1164 1.20%
2B21-F013L 1228 1163 1.10%
2B21-F013M 1008 1179 2.50%

The 2-stage SRVs that were installed on Unit 2 during the previous cycle (Cycle 23) utilized platinum coated pilot discs. The 3-stage SRVs currently installed on Unit 2 have a modified pilot that helps reduce the possibility of inadvertent lift and leak by due to system vibration. The one 3-stage SRV that was installed on Unit 2 during Cycle 23 was recently successfully tested and found to be within the allowable TS SA pressure lift setpoint limit of 1150 +1- 34.5 (+/- 3%) psig.

CAUSE OF EVENT

The root cause of the SRV setpoint drift is attributed to corrosion-induced bonding between the pilot disc and its seating surface. This conclusion is based on previous root cause analyses and the repetitive nature of this condition at Plant Hatch and in the industry. In General Electric (GE) Service Information Letter (SIL) 196, Supplement 16, GE determined that condensation of steam in the pilot chamber of Target Rock 2-stage SRVs can cause oxygen and hydrogen dissolved in the steam to accumulate. As steam condenses in the relatively stagnant pilot chamber, the dissolved gases are released. In a volume such as the pilot chamber which is normally at approximately a 1000 psig pressure and a temperature of 545 degrees F, the total pressure consists primarily of water vapor partial pressure because 544.6 degrees F is the saturation temperature at 1000 psi g. This wet, hot, high-oxygen atmosphere can be very corrosive and can increase the likelihood of corrosion-induced bonding of the pilot disk to its seat. It was also noted that proper insulation minimizes the accumulation rate of non-condensable gases and the steady-state oxygen partial pressure. Despite improvements made in maintaining the integrity of insulation for the previously installed 2-stage SRVs and installing new platinum coated pilots, the corrosion-induced bonding continued to occur as evidenced by the test results from this most recent outage.

REPORTABILITY ANALYSIS AND SAFETY ASSESSMENT

This event is reportable in accordance with 10 CFR 50.73(a)(2)(i)(B) because a condition occurred that is prohibited by TS Surveillance Requirement (SR) 3.4.3.1. Specifically, an example of multiple test failures is given in NUREG-1022, Revision 3, "Event Reporting Guidelines 10 CFR 50.72 and 50.73" which describes the sequential testing of safety valves. This example notes that "Sometimes multiple valves are found to lift with set points outside of technical specification limits."

NUREG-1022 further states in the example that "discrepancies found in TS surveillance tests should be assumed to occur at the time of the test unless there is firm evidence, based on a review of relevant information (e.g., the equipment history and the cause of failure), to indicate that the discrepancy occurred earlier. However, the existence of similar discrepancies in multiple valves is an indication that the discrepancies may well have arisen over a period of time and the failure mode should be evaluated to make this determination." Based on this guidance and the fact that the development of the corrosion occurred over a period of time of plant operation, the determination was made that this "as found" condition is reportable under the reporting requirements of 10 CFR 50.73(a)(2)(i)(B).

There are eleven SRVs located on the four main steam lines within the drywell in between the reactor pressure vessel (RPV) (EllS Code RPV) and the inboard main steam isolation valves (MSIVs) (EllS Code ISV). These SRVs are required to be operable during Modes 1, 2, and 3 to limit the peak pressure in the nuclear system such that it will not exceed the applicable ASME Boiler and Pressure Vessel Code Limits for the reactor coolant pressure boundary. 

The SRVs are tested in accordance with TS surveillance requirement 3.4.3.1 in which the valves are tested as directed by the In-Service Testing Program to verify lift set points are within their specified limits to confirm they would perform their required safety function of overpressure protection. The SRVs must accommodate the most severe pressurization transient which, for the purposes of demonstrating compliance with the ASME Code Limit of 1375 psig peak vessel pressure, has been defined by an event involving the closure of all MSIVs with a failure of the direct reactor protection system trip from the MSIV position switches with the reactor ultimately shutting down as the result of a high neutron flux trip (a scenario designated as MSIVF).

The results from this MSIVF event analysis was performed by the Nuclear Fuels Department in order to bound the "as-found" results of the U2 Cycle 21 2-stage SRVs pressure setpoint drift. The results from this analysis showed a small increase in peak pressures relative to the Hatch-2 Cycle 21 reload licensing analysis (ALA) results. The higher peak pressures were due to the fact that eight of the eleven SRVs opened at pressures higher than that which was assumed in the ALA. It should be noted that in this analysis, the larger actual valve bore size was used in the calculations for nine of the valves rather than the smaller bore size which was conservatively assumed in the ALA. Therefore, higher steam flow capacities than those assumed in the ALA were used in this analysis for those nine valves.

Based on the analysis, the calculated minimum margin to the 1375 psig ASME Boiler and Pressure Vessel Code overpressure limit for peak vessel pressure would have been 27.7 psig and the minimum margin to the 1325 psig Tech Spec Safety Limit for the reactor steam dome pressure would have been 2.9 psig during an MSIVF event during Cycle 21 operation. Therefore, these test results show that in this case, where two of the eleven SRVs would have opened at pressures higher than that which was assumed in the RLA, the peak pressure at the bottom of the vessel would have remained below the ASME Boiler and Pressure Vessel code limit and the peak RPV dome pressure remained within the TS Safety limits.

Additionally, a highly reliable, though non-credited, electrical actuation system serves as a redundant, independent method to actuate the SRVs. During Cycle 23 this redundant electrical logic system was fully functional. Based on the analyses performed, the overpressure protection system would have continued to perform its required safety function if called upon in its "as found" condition. Therefore, this event had no adverse impact on nuclear safety and was of very low safety significance.

CORRECTIVE ACTIONS 

The 2-stage SRVs with platinum-coated pilot discs were removed from Unit 2 during the 2015 refueling outage and replaced with 3-stage SRVs that have a modified pilot. 3-stage SRVs typically do not exhibit set point drift due to their design. The modified pilots will help reduce spurious openings and leak-by due to system vibration.
ADDITIONAL INFORMATION
Other Systems Affected: None
Failed Components Information:
Master Parts List Number: 2B21-F013E, H
Manufacturer: Target Rock
Model Number: 7567F
Type: Relief Valve
Manufacturer Code: T020
EllS System Code: SB
Reportable to EPIX: Yes
Root Cause Code: B
EllS Component Code: RV
Commitment Information: This report does not create any licensing commitments.

PREVIOUS SIMILAR EVENTS:

LER 1-2014-003, identified multiple SRV setpoint drifts for 5 of the 11 two-stage SRVs installed on Unit 1. The two-stage SRVs with platinum-coated pilot discs were removed from Unit 1 during the 2014 refueling outage and replaced with 3-stage SRVs that have a modified pilot. The modified pilots will help reduce spurious openings and leak-by due to system vibration.

LER 1-2012-004, identified multiple SRV setpoint drift for 8 of the 11 SRVs. Corrective actions included replacement of the 2-stage SRVs with 2-stage SRVs whose pilot discs had undergone a platinum surface treatment which was considered at that time to be the long term fix for this corrosion bonding issue.
(2) The above LER was stellite with a 72% failure rate. Now they going to put in platinum
LER 2-2011-002, identified multiple SRV setpoint drift for 8 of the 11 SRVs. Corrective actions included replacement of the 2-stage SRVs with 3-stage SRVs during the Unit 2 Spring 2011 refueling outage which was considered at that time to be the long term fix for this corrosion bonding issue. Subsequent to that outage the 3-stage SRVs exhibited signs of unacceptable leakage which resulted in two separate outages that involved changing out four SRVs during the first outage and the remaining seven SRVs during the subsequent outage in May 2012. The 3-stage SRVs were replaced with 2-stage SRVs containing pilot discs that had undergone the platinum surface treatment.
Here we are in unit 2 with platinum surface treatment at the spa in LER-2-2011-02. There should be a 2013 unit 2 LER but there isn't. But in LER 2-2015-004-00 there is 2 SRV set pressure failures. Hatch explains in that LER they are replacing the platinum with the 3 stage SRVs because of 2 stage valve leaking problems and setpoint inaccuracy issues. Basically the 2 stage and 3 stage target rock SRV valves are lemons...poor design.       
LER 1-2010-001, identified multiple SRV setpoint drift for 5 of the 11 SRVs. Corrective actions included refurbishment of the pilot valves and included the replacement of the pilot discs with discs made from Satellite 21 material. Additionally, the insulation surrounding each SRV was upgraded to improve resistance to corrosion-induced bonding. These were the same actions that were taken following similar failures reported in LER 2-2009-001, since improved results had been seen to some degree in the industry for at least one operating cycle when these actions were implemented.
(1) Lets do the "similar events" in chronological order. On the above LER 1-2010-001, these guys are so riddled by engineering deception and fraud. In a nuclear plant, there should never be a ongoing experiment. So plating a surface or installing stellite disc on the scheme of things, is unbelievably inexpensive. You are suppose to before installation, put the stellite or platinum plated disc and SRV valve on a test stand modeling the plant worst coolant inviroment. Put the disc and seat through three times the worst duty as the plant. Does it stick or get glued to the seat? Then you will know how the material will stand up under the worst conditions. No surprises. We think the stellite and the platinum was just a con job over the NRC to keep the plant running based on any crack pot explanation. In one cycle with the new stellite disc on  LER 1-2012-002, they had 8 of 11 SRV teck spec setpoint lift failures with the stellite. It is a much worst failure rate than without the stellete. It is a 72% failure rate. Hatch promised the stellite would fix the tech spec violation.