Thursday, August 06, 2015

Salem Nuke Plant Is Heading For A Big Event Because Of Maintenance Budget Cutbacks?

Updated Aug 8:
LOWER ALLOWAYS CREEK TWP. — The Salem 2 nuclear reactor has returned to service after a brief shutdown, a company official said. 
According to Joe Delmar, spokesman for the plant's operator, PSEG Nuclear, the unit began sending electricity back out over the regional power grid at 7:39 a.m. Sunday.
Salem 2 automatically shut down at 3:39 p.m. Wednesday because of an electrical circuit failure on one of the four reactor coolant pumps. 
When any of those four pumps — which circulate cooling water around the reactor vessel — fails, it automatically causes the reactor to trip off-line. 
Workers traced that pump circuit failure to an electrical issue with a drain pump which removes condensed water off of the turbine on the non-nuclear side of the plant.
The drain pump tripped and a relay switch did not function properly causing the electrical circuit failure on the one reactor coolant pump...
Updated on Aug 6:

Is it a electrical problem, detector or a frozen reactor coolant pump or motor? 
***Salem reactor shut down by electrical problem
How come the NRC never discloses why the licencees reduced the maintenance?


This facility has two plants three plants(Hope Creek and 2 Salem plants)...these guys could have upwards of 10 30 million components and parts. A small change in maintenance philosophy can and does lead to a runaway component breakdown uncontrollable by the licencees. It demoralizes the staff.

Why didn't the NRC pickup this change in maintenance frequency and write up a NRC report on it before the breaker failure? Why isn't the NRC anticipatory instead of reactionary?

Just saying, on my River Bend special inspection, there has been a widespread breakdown in GE Magne-Blast breaker reliability over maintenance issues. I am sure is is not limited to breaker (Salem), but a global maintenance financial issue across the whole plant and across whole fleets of plants.

Just as the NRC expressed it in the finding concerning broad "Equipment Reliability" and entry into LCOs...an increasing trend in equipment failures outside the breaker failure. How bad is this going to get?
Broken bolts found in all of PSEG Nuclear's Salem 2 reactor cooling pumps LOWER ALLOWAYS CREEK TWP.  
PSEG Nuclear has now found broken-off bolt pieces inside all four of the huge pumps which help cool the nuclear reactor at its Salem 2 plant, officials said.

Errant bolt heads have been found in the bottom of the reactor coolant pumps and even at the bottom of the reactor core itself, settled under the nuclear fuel rods.

And some of the bolt heads that have broken off have not yet been accounted for, federal regulators confirmed Tuesday.

The bolts secure parts known as turning vanes on the inside of the pump. The vanes direct water out of the pump into the reactor where it circulates to cool the core.
We seen this a last year with their poor maintenance on the Reactor coolant pumps with nut/bolts breaking off and entering the coolant. It cost them a tremendous amount of money with the plant staying off the line. I am just saying with penny pinching, it takes a delay time for the equipment failure to show up. Then when the plant is reflooded with monies for the proper maintenance, it takes a long time to fix the degraded parts and do all the proper maintenance with equipment failures still occurring. 

This kind of licencee behavior puts the community at risk...
July 28, 2015

SUBJECT: SALEM NUCLEAR GENERATING STATION, UNIT NOS. 1 AND 2 –INTEGRATED INSPECTION REPORT 05000272/2015002 AND 05000311/2015002


*Equipment Reliability

The inspectors identified that an increasing trend of equipment failures was having an apparent impact on the ability of PSEG to meet station CAP goals. Specifically, the inspectors noted that there has been a steady increase in the number of unplanned LCOs (that exceeded station goals) and CAP evaluation products, as well as CAP evaluation products and actions that fell below station goals for quality and timeliness.

PSEG has identified an adverse trend in equipment deficiencies, as evident by the following notifications captured in CAP, dating back to September of 2014.

*Annual Sample: 12 Safety Injection Pump Breaker Failure to Close

a. Inspection Scope

The inspectors performed an in-depth review of PSEG’s evaluations and corrective actions associated with notification 20660365 and ACE 70168725 for an August 27, 2014 failure of the 12 SI pump breaker to close on demand while attempting to refill the 14 SI accumulator. The limiting conditions for operations could not be met as provided in the associated action requirements, because the system had no operable SI pumps available due to the 11 SI pump being out of service for routine maintenance. PSEG realigned, tested, and returned the 11 SI pump into service, then transitioned into TS

LCO 3.5.2.b for meeting the action statement of having one SI pump available. PSEG performed an ACE and determined the most probable cause of the failure was due to the lack of lubrication inside the breaker close latch roller. The apparent cause was determined to be not proactively addressing timely overhauls of the breakers.

The inspectors assessed PSEG’s problem identification threshold, problem analysis, extent of condition reviews, compensatory actions, and the prioritization and timeliness of PSEG's corrective actions to determine whether PSEG was appropriately identifying,

characterizing, and correcting problems associated with this issue and whether the planned or completed corrective actions were appropriate. The inspectors compared the actions taken to the requirements of PSEG's corrective action program and 10 CFR 50, Appendix B, Criterion XVI, “Corrective Action” and 10 CFR 50, Appendix B, Criterion V, “Instructions, Procedures, and Drawings.”

Findings and Observations

The inspectors concluded that PSEG took appropriate actions to identify the cause of the August 27, 2014, 12 SI pump breaker failure. The inspectors determined that the breaker failure was due to inadequate overhaul intervals of the 4kV breakers.

During review of the 12 SI pump breaker trip event, the inspectors noted that the breaker’s recent operating history had, in effect, changed its classification under PSEG’s ER-AA-1001, “Component Classification,” Revision 2. Specifically, the breaker had originally been classified as a critical, low duty cycle, mild environment component. However, inspectors noted that a high duty cycle was defined, in part, as one where the component is cycled frequently (i.e. greater than two times per week). From late 2014, the 14 accumulator had been experiencing leakage. From that time through the first half of 2015, the frequency at which the 12 SI pump was started to refill the accumulator steadily rose. In the few months leading up the failure, the number of accumulator fills with the 12 SI pump increased until its usage was three times a week for the two weeks prior to the failure. Essentially, PSEG had changed the breaker’s classification by changing its operational frequency to compensate for accumulator leakage. A review

of PSEG’s maintenance template for the same breaker as a high duty cycle component was the same as that for a low cycle breaker. Therefore, the inspectors concluded that this issue was minor. However, they also concluded that PSEG missed this as an opportunity to identify a change in the circumstances surrounding the breaker’s operation. PSEG captured this in their CAP as notification 20664925.

Introduction. A self-revealing Green NCV of 10 CFR 50, Appendix B, Criterion V, “Instruction, Procedures, and Drawings,” was identified because PSEG did not establish an appropriate interval to overhaul 4kV GE Magne-Blast breakers. As a result, the safety-related breakers for the 12 safety injection pump and 11 CCW pump were operated beyond the industry recommended overhaul interval and subsequently failed.

Analysis. The performance deficiency associated with this finding was that PSEG did not establish an appropriate interval to overhaul the 4kV GE Magne-Blast breakers. This finding is more than minor because it is associated with the equipment performance attribute of the Mitigating Systems cornerstone and adversely affected the cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, PSEG did not consider industry recommendations nor develop a basis when establishing 4kV GE Magne-Blast breaker overhaul intervals, which resulted in failure of the 12 SI pump and 11 CCW pump breakers. In accordance with IMC 0609.04, “Initial Characterization of Findings,” and Exhibit 2 of IMC 0609, Appendix A,

Tuesday, August 04, 2015

Entergy Missed Earnings Estimates By A Wide Margin ( down 4%)

Entergy's CEO: 
"...Average Northeast power prices for the second quarter were more than 40% below last year’s levels. Moreover, forward power prices continue their decline following an average of more than 6% for our plants in the Northeast since the end of March this year. These low prices are coupled with the market structure that does not reflect the value of nuclear power. Congress continues to indicate its concern about the specific market structure challenges. On July 8, the Chairs of the Senate and House committees and subcommittees responsible for energy and power Senator Murkowski and congressmen Upton and Whitefield communicated this concern in a letter to the Federal Energy Regulatory Commission Chairman, Norman Bay. In the letter, the committee chairs raised concerns about organized wholesale electricity markets, including the impacts certain market rules were having on reliable base load plants, including nuclear plants and ultimately on consumers. Entergy shares these concerns and we are encouraged by FERC’s willingness to consider these issues. We are also hopeful that FERC will take subsequent action as soon as it can..."
So not having Vermont Yankee running has cost Entergy a lot of money this quarter? 
"The decline was due to lower wholesale power prices and less of nuclear generation. Closure of the Vermont Yankee Nuclear Power Station last year also played a role in pulling down this segment’s results."
Stock price down by over 4% at 2:30 pm today? 
By Zacks Equity Research 2 hours ago 
Entergy Corporation ETR reported second-quarter 2015 operational earnings of 83 cents per share, widely missing the Zacks Consensus Estimate of $1.13 by 26.5%.

The reported number also declined 25.2% from $1.11 per share in the year-ago period. The downside was due to bleak performance at all its three segments. 
Revenues

Entergy’s second-quarter operating revenues of $2,713.2 million also fell short of the Zacks Consensus Estimate by 7.9%. Revenues declined 9.5% from $2,996.7 million in the prior year.

Operational Results

Entergy’s total operating expenses declined 8.1% year over year to $2,335.8 million primarily due to lower input costs.

Operating income for the second quarter also dropped nearly 17% to $377.4 million.

Entergy recorded $159.8 million of interest expenses in the quarter compared with $155.8 million incurred last year.

Segment Results

Utility: The segment’s quarterly operating revenues were $2,273.9 million compared with $2,409.4 million in second-quarter 2014. The downside was due to a 0.2% and 1.5% respective decline in commercial and industrial sales.

Entergy Wholesale Commodities (EWC): Entergy Wholesale Commodities' operating revenues were $439.3 million for the second quarter. In the corresponding quarter last year, revenues were $587.3 million. The decline was due to lower wholesale power prices and less of nuclear generation. Closure of the Vermont Yankee Nuclear Power Station last year also played a role in pulling down this segment’s results.

Financial Condition

As of Jun 30, 2015, cash and cash equivalents were $910.4 million compared with $1,422 million as of Dec 31, 2014.

Long-term debt as of Jun 30, 2015 was $12.1 billion compared with $12.5 billion as of Dec 31, 2014.

In the second quarter of 2015, cash from operating activates was $727.4 million, down from $761.4 million in the year-ago quarter.

Guidance

Entergy affirmed its 2015 earnings guidance in the range of $5.10–$5.90 per share on an operational basis.

Saturday, August 01, 2015

Judiciary Panel Indicts Former Tepco Executives

Judiciary panel indicts former Tepco executives Kana Inagaki in Tokyo
FILE - In this March 30, 2011 file photo, Tokyo Electric Power Co. Chairman Tsunehisa Katsumata, right, speaks during a news conference at the company's head office in Tokyo. A Japanese judicial committee has decided that three former utility executives should face criminal charges and stand trial for their alleged negligence in the Fukushima nuclear disaster. A document released Friday, July 31, 2015 showed the committee voted in favor of indicting Katsumata, who was chairman of TEPCO. at the time of the crisis, along with two other former executives. (AP Photo/Itsuo Inouye, File)©AP

A Japanese civilian judiciary panel has forced prosecutors to indict three former executives of Tokyo Electric Power, in what would be the first criminal charges brought against officials in relation to the Fukushima nuclear disaster.

In a statement, an independent review panel of 11 lay people accused the former Tepco officials for failing to take any “effective measures” and “turning a blind eye” to the possibility of an earthquake triggering a serious nuclear accident.

Citizens’ groups welcomed the decision after prosecutors twice decided not to indict the three former Tepco officials. The review panel overruled the prosecutor’s decision on Friday.

“We feel like we’ve finally gotten this far,” said Ruiko Muto, an anti-nuclear activist who represents a group of about 15,000 residents and citizens who had filed criminal complaints with prosecutors against senior Tepco officials.

“We hope that the criminal trial will uncover the truth behind the accident and that justice will be delivered,” Ms Muto said.

The Fukushima Daiichi nuclear plant in northeastern Japan suffered a number of explosions and partial meltdown following an earthquake and tsunami hit the country in March 2011. It was the worst nuclear incident since Chernobyl in 1986. Tens of thousands of people have yet to be allowed home.

The three senior managers who will stand trial are former chairman Tsunehisa Katsumata, 75, and former executives Sakae Muto, 65, and Ichiro Takekuro, 69.

In the statement, the panel accused the officials of prioritising on economic arguments over safety, saying they “had a responsibility to prepare for the remote possibility of an accident occurring from a tsunami.”

“If proper action had been taken, it would have been sufficiently possible to prevent this critical and brutal accident from occurring,” it concluded.

Tepco declined to comment on the judiciary panel’s decision. But the utility said it would continue to make efforts to strengthen the safety of its nuclear plants.

While it is rare for a civilian judiciary panel to overrule decisions made by prosecutors, legal experts say it is unlikely a trial would lead to a guilty verdict.

In 2010, a review panel of 11 lay people selected by lottery similarly overruled the prosecutor’s decision not to indict Japanese politician Ichiro Ozawa in a political funding scandal. But two year later, a Tokyo court found Mr Ozawa not guilty, clearing him of charges due to lack of sufficient evidence.

Wednesday, July 29, 2015

NEISO: Low Wholesale Electric Prices In June?


So far this summer the wholesale electric prices spikes have remained rather mild. Price spikes have been amazingly docile this summer...

Why, because the politicians are breathing down their throats? 

Wholesale electricity prices and demand in New England


Wholesale power and natural gas prices set new records in June, dropping to lowest monthly levels in 12 years

Mild weather, low demand, and the lowest average natural gas price since 2003 brought June’s wholesale power price to under $20 per megawatt-hour, by far the lowest monthly price in the 12 years New England has had competitive power markets in their current form. June’s average real-time electric energy price of $19.61/MWh was nearly half the June 2014 average price of $37.92/MWh and nearly 23% lower than the previous record-low average monthly price of $25.39/MWh, recorded during March 2012.

Matthew White, chief economist at ISO New England, said the explanation for such low power prices is simple. “It’s supply and demand. With June’s mild weather, demand for natural gas and electricity were both low, and the pipeline capacity was available to deliver a plentiful supply of exceptionally low-priced natural gas to generators in New England. Seasonal demand for natural gas has abated, and New England is able to access that low-cost supply because we aren’t seeing winter’s recurring pipeline constraints.

“But the swing in prices over just five months, going from the third-highest power price during February to the lowest in June, underscores the price volatility attributable to pipeline infrastructure constraints,” White added. “During February’s record cold, demand for natural gas was so high that the pipelines into New England—which haven’t expanded at the same pace as natural gas demand growth—were running at or near capacity. When natural gas demand is so high and the supply available to generators is limited, the price for natural gas delivered to New England rises dramatically—and so does the price for the electricity made from it.”

During February, the average wholesale price of power was $126.70/MWh, while the average price of natural gas was $17.27 per million British thermal units (MMBtu) **, the fourth-highest monthly level since 2003.
The US Energy Information Administration noted in its July 9, 2015, Natural Gas Weekly Update, entitled “Northeastern trading points set record low prices”, that natural gas prices at the Algonquin delivery point in Boston fell to an historic daily low of $1.19/MMBtu on June 5 before breaking that record with new daily low of 82 cents on July 2.
June highlights:
  • Lowest average wholesale electric energy price since March 2003
    • June 2015: $19.61 per megawatt-hour (MWh)*
    • March 2012: $25.39/MWh
    • April 2012: $25.41/MWh
    • April 2015: $25.88/MWh
    • May 2015: $26.12/MWh
  • Lowest average monthly natural gas price since March 2003
    • June 2015: $1.68/MMBtu
    • May 2015: $1.85/MMBtu
    • April 2012: $2.39/MMBtu
    • May 2012: $2.63/MMBtu
    • August 2014: $2.64/MMBtu
  • Second-lowest energy consumption during any June since 2003
    • June 2009: 9,960 gigawatt-hours (GWh)
    • June 2015: 10,146 GWh
    • June 2002: 10,317 GWh
  • Third-lowest average June temperature since 2003
    • June 2009: 63.1° Fahrenheit
    • June 2003: 65.1° F
    • June 2015: 65.2° F
Drivers of Wholesale Electricity Prices

In general, the two main drivers of wholesale electricity prices in New England are the cost of fuel used to produce electricity and consumer demand.

Power Plant Fuel: Fuel is typically one of the major input costs in producing electricity. Natural gas is the predominant fuel in New England, used to generate nearly half of the power produced in the region, and natural gas-fired power plants usually set the price of wholesale electricity in the region. As a result, average wholesale electricity prices are closely linked to natural gas prices.

The average natural gas price during June dropped to $1.68/MMBtu at the Algonquin pipeline delivery point in Massachusetts, a decline of nearly 60% from the $4.07/MMBtu natural gas average price during June a year ago. The June 2015 price was also nearly 10% lower than the May 2015 average price of $1.85/MMBtu, which briefly held the record for the lowest monthly average natural gas price in New England since 2003.

Electricity Demand: Demand is driven primarily by weather as well as economic factors. The average temperature was 65.2° Fahrenheit in New England, the third-lowest June temperature recorded region-wide since 2003, while the dewpoint, a measure of humidity, came in at 54.2°, about the same as the 54.5° in June 2014. The mild weather and the effects of energy-efficiency measures dropped energy usage to 10,146 GWh, the third-lowest level of energy consumption during any June since 2003, and about 2.5% lower  than consumption during June 2014 when the average temperature was about 67.8°F. The impact of weather is reflected in heating and cooling degree days***. During June, the region saw 26.2 cooling degree days (CDD), a slight decline from  the 27.5 CDD recorded during June 2014.

Peak demand for the month hit 20,895 MW on June 23 during the hour from 3 to 4 p.m.,  when the average temperature in New England was 84°F and the dewpoint was 69°. The June 2015 peak was down 1.7% from the June 2014 peak of 21,263 MW, set during the hour from 4 to 5 p.m. on June 30 when the temperature was 85°F and the dewpoint was 61°. The all-time peak demand in New England was 28,130 MW, recorded during an August 2006 heat wave, when the temperature was 94°F and the dewpoint was 74°. Peak demand is driven by weather, which drives the use of heating and air conditioning equipment. Air conditioning use is far more widespread than electric heating in New England, so weather tends to have a relatively greater impact on the summer peak than the winter peak.

Fuel Mix: The mix of resources used in any given time period depends on price and availability, as well as unit commitments made to ensure system stability. Natural gas-fired and nuclear power plants produced most of the 9,176 GWh of electric energy generated within New England during June, at 47% and 31%, respectively. Hydroelectric resources in New England generated 10%. Renewable resources generated 8% of the energy produced within New England, including 5.6% from wood and refuse, 1.4% from wind and 0.5% from solar resources. Coal units generated 0.05% and oil-fired resources produced 0.02% of the energy generated within New England. Dual-fuel units, which generally are capable of burning natural gas or oil and typically use the less expensive fuel, generated about 4%. The region also received net imports of about 1,124 GWh of electricity from neighboring regions.



June 2015 and Percent Change from June 2014 and May 2015June 2015 Change from June 2014Change from May 2015
Average Real-Time
Electricity Price
($/megawatt-hour**)
$19.61-48.3%-24.9%
Average Natural Gas Price
($/MMBtu***)
$1.68-58.7%-9.4%
Peak Demand20,895 MW-1.7%+7.1%
Total Electricity Use10,146 GWh-2.46%+4.5%
Weather-Normalized Use****10,456 GWh-2.7%+9.9%
  * One megawatt (MW) of electricity can serve about 1,000 average homes in New England. A megawatt-hour (MWh) of electricity can serve about 1,000 homes for one hour. One gigawatt-hour (GWh) can serve about 1 million homes for one hour. ** A British thermal unit (Btu) is used to describe the heat value of fuels, providing a uniform standard for comparing different fuels. One million British thermal units are shown as MMBtu. *** A degree day is a measure of heating or cooling. A zero degree day occurs when no heating or cooling is required; as temperatures drop, more heating days are recorded, when temperatures rise, more cooling days are recorded. The base point for measuring degree days is 65 degrees; each degree of a day’s mean temperature that is above 65 degrees is counted as one cooling degree day. A day’s mean temperature of 90 degrees equals 25 cooling degree days.  **** Weather-normalized demand indicates how much electricity would have been consumed if the weather had been the same as the average weather over the last 20 years









River Bend Talking Points to Region IV Alligations

RIVER BEND STATION – NRC SPECIAL INSPECTION REPORT 05000458/2015009; PRELIMINARY WHITE FIND

http://steamshovel2002.blogspot.com/2015/07/river-bend-talking-points-to-region-iv.html


River Bend Talking Points to Region IV Allegations

Reactor high level: Issues of not putting corrective action program. Hiding issues from NRC.  A fleet wide tactic with Entergy.
Request a reset of River Bends simulator and simulator fidelity of all Entergy simulator?
“During power ascension following startup, RFP B did not start. The licensee re-racked its associated circuit breaker and successfully started RFP B.”

“The team identified an apparent violation of 10 CFR 55.46(c)(1), “Plant-Referenced Simulators,” for the licensee’s failure to maintain the simulator so it would demonstrate expected plant response to operator input and to normal, transient, and accident conditions to which the simulator has been designed to respond.”

Pilgrim simulator problems and River Bend within a months of each other only discovered in a troublesome plant trip?

Another work around tripping MFP to control level because of leaking FRVs…

*“On several occasions, the team noted that the licensee chose the expedient solution rather than complete an evaluation to determine that corrective actions resolved the deficient condition.”

“Other examples included the licensee’s choice to have operations personnel rack in and out breakers (MFP), and have maintenance personnel manually operate a limit switch, on the makeup and start logic for the RFP C minimum flow valve, when the RFP did not start.”

NRC widely allow a plant to spin out of control in a complex system, eventually leads to a ANO event (dropped stator and flooding problems).

“Only four minutes elapsed from the time of the scram until the time the Level 8 (high) reactor water level isolation signal was reached. Consequently, operations personnel did not have sufficient time to gain control and stabilize reactor vessel level in the required band.”

“However, operations personnel stated that the plant did not respond in a manner consistent with their simulator training.”

*However, operations personnel stated that the plant did not respond in a manner consistent with their simulator training.”

*It looks like operations works for everyone else instead of everyone else working for operations.” Engineering centric instead of operations centric.”  

HB Robinson breaker event:  “The team identified that the licensee’s maintenance programs for Division I, II, III, and non-safety 4160 V and 13.8 kV breakers installed in the plant may not meet the standards recommended by the vendor, corporate, or Electric Power Research Institute (EPRI) guidelines.”

Why so many issues with faulty cards: SFRV in manual and RPS?

The operations staff is amazingly adaptive with not approved work-arounds and degraded components.

If looks to me the staff went to the SFRV because the FRVs were grossly leaking…

“In reviewing the feedwater system data from the December 24, 2014, scram, the licensee estimated 500,000 lbm/hr leaked past the closed FRVs. This represents approximately 3 percent of the full-power feedwater flow and significantly exceeds the design specification for leakage of 135,000-150,000 lbm/hr.

The licensee identified excessive leakage past the FRVs during testing in 1986. At the time of inspection, the licensee could not produce any corrective actions taken to identify or correct leakage past the FRVs. Further, the licensee had not quantified the amount of leakage past the FRVs prior to the December 24, 2014, event and NRC Special Inspection.”

So why isn’t this A COVER-UP: “The team reviewed the history of Level 8 (high) RFP trips and noted that similar issues of concern were raised by the NRC in 2012. Specifically, a Supplemental Inspection, performed in 2012, for a White performance indicator associated with reactor scrams with complications documented the failure to recognize a Level 8 (high) trip as an adverse condition and enter it into the corrective action program. This non-cited violation was documented in NRC Inspection Report 05000458/2012012.”

“The team identified an apparent violation of 10 CFR 55.46(c)(1), “Plant- Referenced Simulators,” for the licensee’s failure to maintain the simulator so it would demonstrate expected plant response to operator input and to normal, transient, and accident conditions to which the simulator has been designed to respond. As of January 30, 2015, the licensee failed to maintain the simulator consistent with actual plant response for normal and transient conditions related to feedwater flows, alarm response, and behavior of the SFRV controller. As a result, operations personnel were challenged in their control of the plant during a reactor scram that occurred on

December 25, 2014.”

“During an investigation into the report at the OSRC (Onsite Safety Review Committee) for the SCRAM on December 25, 2014, that feed regulating valve leakage (FRV) contributed to the Level 8 received reactor vessel, it was determined by analysis that there is sufficient evidence that leakage by the Feedwater Regulating Valves presents a significant challenge to Operations during a scram event.”

Is a single issue, or is it really an intentional or a inability to keep the simulator accurate?  

Work arounds:

Work Order WO-RBS-00404323: RFP B supply breaker repetitive failures to close potentially reduces the number of feedwater pumps available to operations personnel during a transient following reactor pressure vessel water Level 8 (high). Operations personnel would rack out and then rack the breaker back in until the breaker would function properly. This work order was initiated on February 3, 2015, following discussions with the NRC inspection team.

how long did this go on?

Work Order WO-RBS-00396449: RFP C minimum flow valve does not stroke fully open which prevents starting the C feed pump. Maintenance personnel would manually operate a limit switch on the valve to make up the start logic for the RFP. This work order was initiated on October 10, 2014.

Work Order WO-RBS-00346642: leakage past FRVs when closed complicated post-scram reactor water level control. Operations personnel proceduralized the closure of the main feedwater isolation valves to stop the effect of the leakage.

This work order was initiated on March 27, 2013.

Monday, July 27, 2015

Very Influential Exelon Ex Offical Says: Dump The Six Dog Nuclear Plants

Former Exelon CEO Rowe: Shutting down struggling nukes is 'the proper market-driven answer'

Those worthless egg sucking economic dog nuclear plants...

Energy Wire: Why are certain nuclear plants having trouble competing right now?
Rowe: And in a world that's driven by unfriendly market prices and unfriendly public policy, you shut them down.
Rowe: If I were there, I think I'd have shut the New Jersey plant [Oyster Creek] down first

The six plants facing the preverbal electric chair...
Clinton one plant

Quad Cities two plants

Byron two Plants

Oyster Creek one plant
I think there will be an intensification of lower energy prices here is the USA...Iran jump starting their petroleum industry (good) and issues with growth in china and their stock market problems.

We are getting ready to lose Texas.

What the hell going to go on when American fracting comes to the Iranian oil fields. 


EnergyWire: Monday, July 27, 2015


Energywire: So, what's the right policy solution to keep existing nuclear viable, such as the three Exelon plants in Illinois that are said to be losing money?

EnergyWire: Why are certain nuclear plants having trouble competing right now? Is it just natural gas and wind?

Rowe: Yeah, wind and gas and energy efficiency. The combination of the recession and energy efficiency -- and no one knows the percentages -- has caused demand for electricity to stay below '07 levels through today and probably for another seven or eight years in the Northeast. In a supply-and-demand market, reduced demand hurts. That's the first factor. The second factor is much of the time a nuclear plant is competing against natural gas in the market, so cheap gas really hurts. The third factor is the subsidized wind -- which you really pay for, and it runs whether it's economic or not -- that hurts. The wind really annoys utility people because it runs at night. At night, you have more than enough electricity, and wind just ruins the price.

EW: It has been said that preserving existing nuclear plants is key to helping the U.S. achieve climate goals. So, what's the right policy solution to keep existing nuclear viable, such as the three Exelon plants in Illinois that are said to be losing money?

Rowe: I'm living in a fairy world because I don't have the numbers and I'm not responsible for them anymore. But in my opinion, you shut those three plants down. You say they have become uneconomic just like some old coal plants are uneconomic. And in a world that's driven by unfriendly market prices and unfriendly public policy, you shut them down. That's what I think the answer is, which is a setback for our low-carbon goals and a setback for the high-paying industrial jobs that people want to keep. But it is the proper market-driven answer.

EW: That would be unpopular with your former colleagues.

Rowe: I don't know. I can ask, but I don't want to ask. They have to figure this out for themselves. I love nuclear power plants. For [current Exelon CEO] Chris Crane, it's his life. He would probably go further to keep a plant running than I would go. I don't believe there's anything divine about markets, but I believe they're pretty important. Chris has only seen the sour side of the markets. I don't believe you can run a good utility letting public policy push you toward something but not pay you for it.

In some ways, I believe the only way a utility has credibility in saying that something isn't making any money is if it's actually willing to shut it down. If I were there, I think I'd have shut the New Jersey plant [Oyster Creek] down first. It's the oldest, it's the smallest, and it would have given credibility to what Exelon is saying about the other four. Nuclear power plants have been shut down before around the country. Am I saying that's the desirable answer? No, I'm not. What I'm saying is if the real reason to keep them running is a public policy reason, then the public has to help bear the cost of doing that…

Thursday, July 23, 2015

Callaway Plume In Contaiment: Is This How the Nucler Industry Ends in the USA?

Everyone thinks it will end with mass radiation causalities...I say it will more end in a event like this?

Power ReactorEvent Number: 51253
Facility: CALLAWAY
Region: 4 State: MO
Unit: [1] [ ] [ ]
RX Type: [1] W-4-LP
NRC Notified By: WALTER GRUER
HQ OPS Officer: JEFF HERRERA
Notification Date: 07/23/2015
Notification Time: 04:21 [ET]
Event Date: 07/23/2015
Event Time: 01:15 [CDT]
Last Update Date: 07/23/2015
Emergency Class: NON EMERGENCY
10 CFR Section:
50.72(b)(2)(i) - PLANT S/D REQD BY TS
Person (Organization):
HEATHER GEPFORD (R4DO)
SCOTT MORRIS (NRR)
JEFFERY GRANT (IRD)

UnitSCRAM CodeRX CRITInitial PWRInitial RX ModeCurrent PWRCurrent RX Mode
1NY100Power Operation0Cold Shutdown
Event Text
INITIATION OF PLANT SHUTDOWN DUE TO RCS LEAKAGE

"On July 23, 2015 at 0115 [CDT], Callaway Plant initiated a shutdown required by Technical Specifications (TS). At 2139 [CDT] on July 22, 2015, TS 3.4.13 Condition A was entered due to unidentified RCS leakage being in excess of the 1 gpm TS limit. The leak was indicated by an increase in containment radiation readings, increasing sump levels, and decreasing levels in the Volume Control tank (VCT).

"A containment entry identified a steam plume; due to personnel safety the exact location of the leak inside the containment building could not be determined.

"At this time radiation levels inside [the] containment are stable and slightly above normal. There have been no releases from the plant above normal levels.

"The [NRC] Senior Resident Inspector was notified."

Callaway nuclear plant shut down after 'non-emergency' leak


The Ameren Corp. nuclear power plant in central Missouri was shut down for the second time in eight months Thursday after a "non-emergency" leak was found in the reaction control system.
The shutdown occurred at 1:15 a.m. at the plant near Fulton. Jeff Trammel, a spokesman for St. Louis-based Ameren, called it a "minor steam leak." He said no one was hurt and there was no risk to the public.
Ameren officials are investigating the cause. Trammel said it was unclear when the plant would restart.
The U.S. Nuclear Regulatory Commission was advised of the leak and inspectors are at the plant, spokeswoman Lara Uselding said.
"The plant is in a safe shutdown condition and there is no risk to public health and safety or the environment," Uselding said.
The Callaway plant also shut down in December, due to an electrical equipment failure. That shutdown was the first in more than two years. No one was hurt and the public was not threatened in that leak, Ameren said.
An NRC report on the latest incident classified it as a "non-emergency." The report said the shutdown was initiated after a reaction control system leak was detected at the plant that sits about 100 miles west of St. Louis.
"A containment entry identified a steam plume; due to personnel safety the exact location of the leak inside the containment building could not be determined," the NRC report said.
The NRC report said radiation levels were "slightly above normal," but stable inside the containment building, and there were no releases from the plant "above normal levels."
Ed Smith of the Missouri Coalition for the Environment said the shutdown raises concerns for the plant, which turned 30 last year.
"As the Callaway nuclear reactor ages, I think we're going to see more incidents like this," Smith said.
Ameren, based in St. Louis, provides electrical power to customers in Missouri and Illinois. Trammel said customers will see no impact from the shutdown. The Callaway plant generates about 20 percent of electricity for Ameren's 1.2 million Missouri customers.
Earlier coverage:
Ameren Missouri's Callaway Nuclear plant was shut down today by a "minor steam leak."
The company said the incident occurred in the plant's containment area, and "poses no threats to the health and safety of the public or Callaway employees."
Company officials are trying to determine the cause of the problem, which they said "has been contained."
No "return to service date" has been set, but service to customers "has not been affected."
Ameren provides electricity to more than 1 million customers in Central and Eastern Missouri







Tuesday, July 21, 2015

Why Are Nuclear Plants Having So Many Safety Related HVAC Problem?

July 23

Is excessive HVAC NRC reporting a symptom of too large plant work back log???

July 22:

Bet you most of the HVAC systems were rushed add on systems during troublesome construction and post TMI...

I think the NRC and industry would come back and say...this is where prescriptive regulations got it wrong. There is a insignificant chance these HVAC problems would lead to core damage and a offsite release.
I would say this is where this perspective incentivizes broadly setting up and tolerating safety component degradation and obsolesces.

If we broadly tolerate component degradations in these amazingly complex machines and organizations...then we become much closer to the day when one of these plants runs away from us.
Is there such a thing as boiling frog with priorities metaphor...normalization of deviance?

Is risk perspective numbing us to threats and real risk...

 

The truth is, if the NRC demanded just a few of this plants to shut down over HVAC problems, the industry would update all their problematic HVAC systems. It is common for these guys to fix these problems in a isolated way…instead of thinking holistic it is more efficient with our resources just to buy a new car or buy a new HAVC system.   
The question is if this is an essential safety system, then why is there only one and doing maintenance on it makes it inop.
If this is essential for accident mitigation, why is it taken off line at 100% full power operation, unless the plant has carefully schedule a DBA not to occur while the essential HVAC system is down for repair?"
 July 21:

All 2015 events.
Is it my VY leaking roofs deal…didn’t realize the system had come to end-of-life.
I bet you HVAC problems would be at the bottom of the barrel of maintenance and budgets priority systems.
What do you make big picture and why this is happening...are the issues trending up?
Would having four HVAC systems powered from two independent buses fix it...

Not a complete list: 
###Power Reactor    Event Number: 51103
Facility: CATAWBA
Region: 2 State: SC
Unit: [1] [2] [ ]
RX Type: [1] W-4-LP,[2] W-4-LP
NRC Notified By: THOMAS GARRISON
HQ OPS Officer: JOHN SHOEMAKER    Notification Date: 05/29/2015
Notification Time: 20:17 [ET]
Event Date: 05/29/2015
Event Time: 12:30 [EDT]
Last Update Date: 06/12/2015
Emergency Class: NON EMERGENCY
10 CFR Section:
50.72(b)(3)(xiii) - LOSS COMM/ASMT/RESPONSE
Person (Organization):
KATHLEEN O'DONOHUE (R2DO)

Unit    SCRAM Code    RX CRIT    Initial PWR    Initial RX Mode    Current PWR    Current RX Mode
1    N    Y    100    Power Operation    100    Power Operation
2    N    Y    100    Power Operation    100    Power Operation
Event Text
TECHNICAL SUPPORT CENTER VENTILATION SYSTEM OUT OF SERVICE DUE TO DISCOVERED CONDITION

"This is non-emergency eight hour notification for a loss of Emergency Assessment Capability.

"This event is reportable in accordance with 10 CFR 50.72(b)(3)(xiii) as the discovered condition affects the functionality of an emergency response facility.

"A condition impacting functionality of the TSC [Technical Support Center] Ventilation system was discovered on 05/29/2015 at 1230 [EDT]. The issue involves a loss of cooling capability of the TSC ventilation system due to a failed relay. Maintenance will begin repairs at 0700 [EDT] on 05/30/2015. Estimated time to repair is unknown at this time.

"If an emergency is declared requiring TSC activation during this period, the TSC will be staffed and activated using existing emergency planning procedures unless the TSC becomes uninhabitable due to ambient temperature, radiological, or other conditions. If relocation of the TSC becomes necessary, the Emergency Coordinator will relocate the TSC staff to an alternate location in accordance with applicable site procedures. The Emergency Response Organization team will be notified of the condition and the possible need to relocate during an emergency. This condition does not affect the health and safety of the public or station employees. An update will be provided once the TSC ventilation has been restored to normal operation. The NRC Resident Inspector will be notified."

* * * UPDATE FROM AARON MICHALSKI TO DANIEL MILLS AT 1557 EDT ON 6/12/15 * *

The TSC ventilation system has been returned to service. The licensee will notify the NRC Resident Inspector.

Notified R2DO (Guthrie).




###Power Reactor    Event Number: 51154
Facility: BRAIDWOOD
Region: 3 State: IL
Unit: [1] [2] [ ]
RX Type: [1] W-4-LP,[2] W-4-LP
NRC Notified By: BLAKE BAXTER
HQ OPS Officer: DANIEL MILLS    Notification Date: 06/15/2015
Notification Time: 17:42 [ET]
Event Date: 06/16/2015
Event Time: 07:00 [CDT]
Last Update Date: 06/15/2015
Emergency Class: NON EMERGENCY
10 CFR Section:
50.72(b)(3)(xiii) - LOSS COMM/ASMT/RESPONSE
Person (Organization):
PATTY PELKE (R3DO)

Unit    SCRAM Code    RX CRIT    Initial PWR    Initial RX Mode    Current PWR    Current RX Mode
1    N    Y    100    Power Operation    100    Power Operation
2    N    Y    100    Power Operation    100    Power Operation
Event Text
TSC VENTILATION TO BE REMOVED FROM SERVICE FOR PLANNED MAINTENANCE

"On 6/16/2015, planned preventive maintenance activities [will be] performed on the Braidwood Generating Station Technical Support Center (TSC), Ventilation System. The work will be completed within approximately 48 hours. This activity includes preventative maintenance that requires the TSC ventilation system to be out of service which will render the TSC ventilation system non-functional.

"If an emergency is declared requiring TSC activation during this period, the TSC will be staffed and activated using existing emergency planning procedures unless the TSC becomes uninhabitable due to ambient temperature or other conditions. If relocation of the TSC becomes necessary, the Emergency Director will relocate the TSC staff as necessary.

"This event is reportable per 10 CFR 50.72(b)(3)(xiii) for 'any event that results in a major loss of emergency assessment capability.' The planned maintenance will not be able to restore the TSC condensing unit or ventilation system to service within the facility activation time specified in the emergency plan (1 hour) in the event of an accident. The Emergency Response Organization team has been notified of the maintenance and the possible need to relocate during an emergency.

"The licensee has notified the NRC Resident Inspector."




###Power Reactor    Event Number: 51164
Facility: LASALLE
Region: 3 State: IL
Unit: [1] [2] [ ]
RX Type: [1] GE-5,[2] GE-5
NRC Notified By: TODD CASAGRANDE
HQ OPS Officer: JEFF HERRERA    Notification Date: 06/17/2015
Notification Time: 23:39 [ET]
Event Date: 06/17/2015
Event Time: 18:41 [CDT]
Last Update Date: 06/18/2015
Emergency Class: NON EMERGENCY
10 CFR Section:
50.72(b)(3)(xiii) - LOSS COMM/ASMT/RESPONSE
Person (Organization):
PATTY PELKE (R3DO)

Unit    SCRAM Code    RX CRIT    Initial PWR    Initial RX Mode    Current PWR    Current RX Mode
1    N    Y    100    Power Operation    100    Power Operation
2    N    Y    100    Power Operation    100    Power Operation
Event Text
TECHNICAL SUPPORT CENTER VENTILATION SYSTEM RETURN DAMPER FAILED CLOSED

"On June 17th, 2015 at 1841 CDT, it was determined that the onsite Technical Support Center (TSC) Ventilation System return damper 0VS119Y was failed closed, the failed closed damper affects the TSC Emergency Makeup Train filtration efficiency. There is currently no emergency event in progress requiring TSC staffing. If an emergency is declared and the TSC ERO [Emergency Response Organization] activation is required, the TSC will be staffed and activated unless the TSC becomes uninhabitable due to ambient temperatures, radiological, or other conditions. If relocation of the TSC staff becomes necessary, the Station Emergency Director will relocate the staff to an alternate TSC location in accordance with applicable site procedures.

"The licensee has notified the [NRC] Senior Resident Inspector of the issue."

* * * UPDATE AT 1700 EDT ON 06/18/15 FROM TODD CASAGRANDE TO S. SANDIN * * *

"After repairs were completed, the TSC Ventilation was restored to service at 1650 EDT on 06/18/2015.

"The licensee has notified the NRC Resident Inspector."

Notified R3DO (Pelke).




###Power Reactor    Event Number: 51154
Facility: BRAIDWOOD
Region: 3 State: IL
Unit: [1] [2] [ ]
RX Type: [1] W-4-LP,[2] W-4-LP
NRC Notified By: BLAKE BAXTER
HQ OPS Officer: DANIEL MILLS    Notification Date: 06/15/2015
Notification Time: 17:42 [ET]
Event Date: 06/15/2015
Event Time: 07:00 [CDT]
Last Update Date: 06/18/2015
Emergency Class: NON EMERGENCY
10 CFR Section:
50.72(b)(3)(xiii) - LOSS COMM/ASMT/RESPONSE
Person (Organization):
PATTY PELKE (R3DO)

Unit    SCRAM Code    RX CRIT    Initial PWR    Initial RX Mode    Current PWR    Current RX Mode
1    N    Y    100    Power Operation    100    Power Operation
2    N    Y    100    Power Operation    100    Power Operation
Event Text
TSC VENTILATION TO BE REMOVED FROM SERVICE FOR PLANNED MAINTENANCE

"On 6/16/2015, planned preventive maintenance activities [will be] performed on the Braidwood Generating Station Technical Support Center (TSC), Ventilation System. The work will be completed within approximately 48 hours. This activity includes preventative maintenance that requires the TSC ventilation system to be out of service which will render the TSC ventilation system non-functional.

"If an emergency is declared requiring TSC activation during this period, the TSC will be staffed and activated using existing emergency planning procedures unless the TSC becomes uninhabitable due to ambient temperature or other conditions. If relocation of the TSC becomes necessary, the Emergency Director will relocate the TSC staff as necessary.

"This event is reportable per 10 CFR 50.72(b)(3)(xiii) for 'any event that results in a major loss of emergency assessment capability.' The planned maintenance will not be able to restore the TSC condensing unit or ventilation system to service within the facility activation time specified in the emergency plan (1 hour) in the event of an accident. The Emergency Response Organization team has been notified of the maintenance and the possible need to relocate during an emergency.

"The licensee has notified the NRC Resident Inspector."

* * * UPDATE AT 1102 EDT ON 6/18/15 FROM DAVID KORTGE TO JEFF HERRERA * * *

"Braidwood Generating Station TSC ventilation was restored to available status at 0700 CDT on June 18, 2015.

"The previously reported system preventative maintenance has been completed."

The licensee notified the NRC Resident Inspector.

Notified the R3DO (Pelke).




###Power Reactor    Event Number: 51212
Facility: HARRIS
Region: 2 State: NC
Unit: [1] [ ] [ ]
RX Type: [1] W-3-LP
NRC Notified By: RAYMOND MOORE
HQ OPS Officer: MARK ABRAMOVITZ    Notification Date: 07/08/2015
Notification Time: 17:43 [ET]
Event Date: 07/07/2015
Event Time: 11:05 [EDT]
Last Update Date: 07/08/2015
Emergency Class: NON EMERGENCY
10 CFR Section:
50.72(b)(3)(xiii) - LOSS COMM/ASMT/RESPONSE
Person (Organization):
GERALD MCCOY (R2DO)

Unit    SCRAM Code    RX CRIT    Initial PWR    Initial RX Mode    Current PWR    Current RX Mode
1    N    Y    100    Power Operation    100    Power Operation
Event Text
TECHNICAL SUPPORT CENTER VENTILATION OUT OF SERVICE

"This is a non-emergency eight hour notification for a loss of Emergency Assessment Capability. This event is reportable in accordance with 10 CFR 50.72(b)(3)(xiii) as the discovered condition affects the functionality of an emergency response facility.

"A condition impacting functionality of the TSC Ventilation system was discovered on July 7, 2015 at 11:05 EDT. The issue involved a loss of cooling capability of the TSC Ventilation system due to failed ventilation system components. Maintenance started repairs immediately following the discovery of the component failures and completed repairs to restore functionality of the TSC Ventilation system on July 8, 2015 at 17:07 EDT. On July 8, 2015, at approximately 15:30 EDT, further review of the impact of this equipment failure determined that this condition was reportable as a loss of emergency assessment capability.

"If an emergency were declared requiring TSC activation during the non-functional period, the TSC would have been staffed and activated using existing emergency planning procedures unless the TSC became uninhabitable due to ambient temperature, radiological, or other conditions. If relocation of the TSC became necessary, the Emergency Director would have relocated the TSC staff to an alternate location in accordance with applicable site procedures. The Emergency Response Organization team was notified of the maintenance and the possible need to relocate during an emergency. This condition did not affect the health and safety of the public or station employees. The NRC Resident Inspector has been notified."



###Power Reactor    Event Number: 51213
Facility: LASALLE
Region: 3 State: IL
Unit: [1] [2] [ ]
RX Type: [1] GE-5,[2] GE-5
NRC Notified By: BRADLEY BRUMUND
HQ OPS Officer: VINCE KLCO    Notification Date: 07/08/2015
Notification Time: 21:53 [ET]
Event Date: 07/08/2015
Event Time: 18:37 [CDT]
Last Update Date: 07/08/2015
Emergency Class: NON EMERGENCY
10 CFR Section:
50.72(b)(3)(xiii) - LOSS COMM/ASMT/RESPONSE
Person (Organization):
ANN MARIE STONE (R3DO)

Unit    SCRAM Code    RX CRIT    Initial PWR    Initial RX Mode    Current PWR    Current RX Mode
1    N    Y    100    Power Operation    100    Power Operation
2    N    Y    100    Power Operation    100    Power Operation
Event Text
TECHNICAL SUPPORT CENTER VENTILATION OUT OF SERVICE

"This telephone notification is provided in accordance with Exelon Reportability manual SAF 1.10, 'Major Loss of Emergency Preparedness Capabilities', and 10CFR50.72(b)(3)(xiii).

"On July 8th 2015 at 1837 [CDT], it was determined that the onsite Technical Support Center (TSC) Ventilation System Supply Fan belts had failed, resulting in loss of ventilation for the facility. Repairs were not completed within the time required had the TSC needed to be staffed. There is currently no emergency event in progress requiring TSC staffing. If an emergency is declared and the TSC ERO [Emergency Response Organization] activation is required, the TSC will be staffed and activated unless the TSC becomes uninhabitable due to ambient temperatures, radiological, or other conditions. If relocation of the TSC staff becomes necessary, the Station Emergency Director will relocate the staff to an alternate TSC location in accordance with applicable site procedures.

"The licensee has notified the [NRC] Senior Resident Inspector of the issue."




###Power Reactor    Event Number: 51213
Facility: LASALLE
Region: 3 State: IL
Unit: [1] [2] [ ]
RX Type: [1] GE-5,[2] GE-5
NRC Notified By: BRADLEY BRUMUND
HQ OPS Officer: VINCE KLCO    Notification Date: 07/08/2015
Notification Time: 21:53 [ET]
Event Date: 07/08/2015
Event Time: 18:37 [CDT]
Last Update Date: 07/11/2015
Emergency Class: NON EMERGENCY
10 CFR Section:
50.72(b)(3)(xiii) - LOSS COMM/ASMT/RESPONSE
Person (Organization):
ANN MARIE STONE (R3DO)

Unit    SCRAM Code    RX CRIT    Initial PWR    Initial RX Mode    Current PWR    Current RX Mode
1    N    Y    100    Power Operation    100    Power Operation
2    N    Y    100    Power Operation    100    Power Operation
Event Text
TECHNICAL SUPPORT CENTER VENTILATION OUT OF SERVICE

"This telephone notification is provided in accordance with Exelon Reportability manual SAF 1.10, 'Major Loss of Emergency Preparedness Capabilities', and 10CFR50.72(b)(3)(xiii).

"On July 8th 2015 at 1837 [CDT], it was determined that the onsite Technical Support Center (TSC) Ventilation System Supply Fan belts had failed, resulting in loss of ventilation for the facility. Repairs were not completed within the time required had the TSC needed to be staffed. There is currently no emergency event in progress requiring TSC staffing. If an emergency is declared and the TSC ERO [Emergency Response Organization] activation is required, the TSC will be staffed and activated unless the TSC becomes uninhabitable due to ambient temperatures, radiological, or other conditions. If relocation of the TSC staff becomes necessary, the Station Emergency Director will relocate the staff to an alternate TSC location in accordance with applicable site procedures.

"The licensee has notified the [NRC] Senior Resident Inspector of the issue."

* * * UPDATE FROM TODD CASAGRANDE TO DANIEL MILLS AT 1510 EDT ON 7/11/15 * * *

"After repairs were completed, the TSC Ventilation was restarted on 7/9/15 at 0625 EDT for a maintenance run, the TSC Ventilation was restored to operable status at 1500 EDT on 07/11/2015.

"The licensee has notified the NRC Resident Inspector."

Notified R3DO (Stone).




###Power Reactor    Event Number: 51232
Facility: DRESDEN
Region: 3 State: IL
Unit: [ ] [2] [3]
RX Type: [1] GE-1,[2] GE-3,[3] GE-3
NRC Notified By: PATRICK HAARHOSS
HQ OPS Officer: VINCE KLCO    Notification Date: 07/15/2015
Notification Time: 01:04 [ET]
Event Date: 07/15/2015
Event Time: 00:04 [CDT]
Last Update Date: 07/17/2015
Emergency Class: NON EMERGENCY
10 CFR Section: 
50.72(b)(3)(xiii) - LOSS COMM/ASMT/RESPONSE
Person (Organization): 
STEVE ORTH (R3DO)

Unit    SCRAM Code    RX CRIT    Initial PWR    Initial RX Mode    Current PWR    Current RX Mode
2    N    Y    100    Power Operation    100    Power Operation
3    N    Y    100    Power Operation    100    Power Operation
Event Text
TECHNICAL SUPPORT CENTER OUT OF SERVICE DUE TO PLANNED MAINTENANCE 

"At 0004 [CDT] on Wednesday, July 15, 2015, the Dresden Nuclear Power Station (DNPS) Technical Support Center (TSC) emergency ventilation system will be removed from service for planned maintenance activities. During the maintenance, the TSC Ventilation will be shut down. The TSC air filtration fan and dampers will be non-functional, rendering the TSC HVAC accident mode non-functional. This maintenance is scheduled to minimize out of service time. The planned TSC ventilation outage is scheduled to be completed in approximately 24 hours. 

"Contingency plans are in place so that if an emergency is declared requiring TSC activation during this period, the TSC will be staffed and activated using existing Emergency Planning (EP) procedures and checklists. If radiological or environmental conditions require TSC facility evacuation during ventilation system restoration; the Station Emergency Director will relocate the TSC staff in accordance with station procedures." 

"The NRC Resident Inspector has been notified." 

* * * UPDATE FROM TRAVIS PRELLWITZ TO DONALD NORWOOD AT 1733 EDT ON 7/17/2015 * * * 

"At 1347 CDT on July 17, 2015, Dresden TSC Ventilation was restored. The Dresden TSC Ventilation is Functional at this time. 

"The NRC Resident Inspector has been notified." 

Notified R3DO (Orth).