Wednesday, March 18, 2015

Storm Juno LOOP and SRV Malfunction...the Special Inspection.

Works in progress...I've be adding to this in the next week. Heading towards a 2.206.

Update: March 20, 2015 
Yesterday i called the Hatch nuclear plant senior resident asking him about all their recent failures of the model 0867F SRVs. Could just leave a recording. You know you are in Siberia when the regional public relations person calls you back instead of the resident inspector.
He didn't have much information about the Hatch SRV events…but he did say something particular. There is no doubt he called region I officials and the higher level officials were coordinating the response. What the message the NRC wanted me to relay to the public:
The failed SRV at Pilgrim had 57 cycles on it while a similar Hatch SRV  has 3 to 4 cycles on it. Hatch operates their SRV's fundamentally different than Pilgrim.
I tried to probe this guy (he was a nice guy) asking him how Hatch operates their SRVs different than Pilgrim. I told him I was a license operator at Vermont Yankee. He responded back to me, Pilgrim uses their SRVs to control pressure while up at power while Hatch does not. You never know when these guys are playing dumb or are really dumb? Usually all NRC employees, no matter what the stripe, are particularly intelligent. I asked him twice what he meant by that, the response never changed. 
If I had to translate what he said, I think he was trying to say during start-ups and particularly shutdowns and hard shutdowns, Pilgrim reverts as a normal operation path, especially when the main stream lines are closed, into using their SRVs as the means of cooling the core and pressure control in the vessel. 
Is he saying all their shutdowns and hard shutdowns are causing damage to Pilgrims SRVs? Why are the SRV designs so delicate? 
Typically in the worst accident possible (DBA), they cycle the SRV valves between 300 and 500 times in one accident…
I asked region I senior public affair official to respond to this in a phone message (Mrs. Srenci)

Did the NRC release this for the public meeting tonight?


PNO

Part 21 Event Number: 50900

Only the 0867F is under investigation.
The root cause of the potential test induced defect has not yet been confirmed as of the date of this report.
One of the four installed MS-SRVs may not have fully opened.
As-found steam testing of the affected MS-SRV did not duplicate this failure; the valve opened on demand.  
We are working with all three (4) sites to identify appropriate precautions.
Rep Org: CURTISS WRIGHT FLOW CONTROL CO.
Licensee: CURTISS WRIGHT FLOW CONTROL CO.
Region: 1
City: EAST FARMINGDALE State: NY
County:
License #:
Agreement: Y
Docket:
NRC Notified By: JOHN DeBONIS
HQ OPS Officer: STEVE SANDIN Notification Date: 03/17/2015
Notification Time: 09:59 [ET]
Event Date: 03/17/2015
Event Time: [EDT]
Last Update Date: 03/17/2015
Emergency Class: NON EMERGENCY
10 CFR Section:
21.21(a)(2) - INTERIM EVAL OF DEVIATION
Person (Organization):
GLENN DENTEL (R1DO)
BINOY DESAI (R2DO)
PART 21/50.55 REACT (EMAI)
Event Text
INTERIM PART 21 REPORT - POTENTIAL TEST INDUCED DEFECT IN A 0867F MAIN STEAM SAFETY RELIEF VALVES

The following report was received from Curtiss - Wright via email:


"This letter provides interim notification of a potential test induced defect in a 0867F Series Main Steam Safety Relief Valves (MS-SRVs) manufactured and supplied by Target Rock (TR). The information required for this notification is provided below:


"(i) Name and address of the individual or individuals informing the Commission.


William Brunet

Director of Quality Assurance
James White
General Manager
Target Rock, Business Unit of Curtiss-Wright Flow Control Corporation
1966E Broadhollow Road
East Farmingdale, NY 11735

"(ii) Identification of the basic component supplied for such facility or such activity within the United States which may fail to comply or contains a potential defect.


Target Rock 0867F Series of Main Steam-Safety Relief Valves Manufactured by Target Rock. This is a 3-stage piloted valve consisting of a main valve (the 'Main') with an actuator mounted to it (the 'Topworks'). The 0867F is the latest generation of the 67F line of MS-SRVs, including the original 3-Stage and 2-Stage designs, and this product line has over 40 years of plant operational experience. Only the 0867F is under investigation. This is due to the differences between the 0867F design and the other designs.


"(iii) Identification of the firm supplying the basic component which fails to comply or contains a defect.


Target Rock, Business Unit of Curtiss-Wright Flow Control Corporation

1966E Broadhollow Road
East Farmingdale, NY 11735

"(iv) Nature of the defect or failure to comply and the safety hazard which is created or could be created by such defect or failure to comply.


As we understand it, the Pilgrim Station recently manually opened the Target Rock Main Steam Safety Relief Valves (MS-SRVs) as part of cooling down the reactor following a loss of offsite power. One of the four installed MS-SRVs may not have fully opened. As-found steam testing of the affected MS-SRV did not duplicate this failure; the valve opened on demand. However, the valve did not re-close as expected. Internal inspections found damaged parts in the main stage subassembly that could potentially affect the ability of the MS-SRV to operate as designed.


We are investigating potential root causes for this damage. However, we are still unable to determine if a specific defect exists. GE SIL-196, Supplement 17 determined Main Spring relaxation was caused by 'extreme dynamics encountered during limited flow testing . Valve dynamics under full flow conditions (i.e. discharge not gagged) are much less severe than those under limited flow conditions.' These extreme dynamics, under limited flow test conditions, are the focus of our investigation. Specific areas of investigation include;


a) Testing of materials to verify they are consistent with our material specifications,

b) evaluation of differences between the 0867F and earlier designs, and
c) evaluation of the differences between different limited flow test loop configurations and test procedures

"(v) The date on which the information of such defect or failure to comply was obtained.


The Pilgrim event occurred on January 27, 2015. As-found testing occurred on February 2, 2015.


"(vi) In the case of a basic component which contains a defect or fails to comply, the number and location of these components in use at, supplied for, being supplied for, or may be supplied for, manufactured, or being manufactured for one or more facilities or activities subject to the regulations in this part.


While we have yet to determine if a specific defect exists, the following plants were supplied 0867F MS-SRVs:


- Pilgrim (Model 09J-001) Quantity Shipped = 8

- Fitzpatrick (Model 09H-001) Quantity Shipped = 4, Quantity on order= 8
- Hatch 1 and 2 (Model 09G-001) Quantity Shipped= 24, Quantity on order= 12

The following plants will be supplied 0867F MS-SRVs:


- Hope Creek (Models 14J-001, 14J-002) Quantity on order = 7


"(vii) The corrective action which has been, is being, or will be taken; the name of the individual or organization responsible for the action; and the length of time that has been or will be taken to complete the action.


The root cause of the potential test induced defect has not yet been confirmed as of the date of this report. Therefore, no specific corrective actions have been initiated. Target Rock Problem Report 080 will document the corrective actions when they are determined and complete the 10 CFR Part 21 evaluation of the potential test induced defect. This determination will be based on further mechanical and material evaluations. TR anticipates completing these evaluations within 45 days; however, in the event the evaluations are not completed, TR will forward another interim report within 45 days.


"(viii) Any advice related to the defect or failure to comply about the facility, activity, or basic component that has been, is being, or will be given to purchasers or licensees.


We are working with all three (4) sites to identify appropriate precautions.


"(ix) In the case of an early site permit, the entities to whom an early site permit was transferred.

Not applicable.

"Should you have any questions regarding this matter, please contact Michael Cinque, Director of Program Management at (631 ) 293-3800."

SRV-3B Safety Relief Valve Declared Inoperable Dueto Leakage and Setpoint Drift

Licensee Event Report 2013-002-01

Event date 01 20 2013

LER: 2013 002 01

Report Date 1 31 2014

On Sunday January 20, 2013, at 2050 hours with the reactor at 100% core thermal power (RMSS in RUN), PNPS declared SRV-3B inoperable and entered Technical Specification (TS) 3.6.D.2 requiring an orderly reactor shutdown such that reactor coolant pressure is less than 104 psig within 24 hours. On Monday January 21, 2013, at 1300 hours (16 hrs and 10 minutes) reactor coolant pressure was lowered to less than 104 psig. SRV-3B had been declared inoperable consistent with PNPS procedures that state an SRV is inoperable if the first stage pilot thermocouple temperature is 350 F below its baseline temperature. This LER Supplement provides the determination of cause for the leakage. The cause of the SRV leakage was that the natural frequency of the pilot assembly was close to a resonant frequency of the valve assembly when installed on the PNPS main steam line, that had failed to be considered in the design of the SRV. A contributing cause was wear and looseness of parts in the main stage of RV-203-3B.

The reactor was depressurized and a new pilot valve assembly was installed on SRV-3B. On January 22, 2013, at 1015 hours reactor restart was commenced. On January 24, 2013 at 0312 hours 100% core thermal power was achieved.

This LER also reports the as-found setpoint of one SRV pilot valve tested was less than the minimum pressure required by TS 3.6.D.1.

This event had no impact on the health and/or safety of the public.

BACKGROUND:

As background, the pressure relief system includes four (4) SRVs and two (2) spring safety valves (SSVs). During Refueling Outage (RFO-1 8), in April/May, 2011, the four SRVs were replaced with Target Rock Model 0867F 3-stage SRVs. The SRVs discharge through their individual discharge piping, terminating below the minimum suppression pool (torus) water level. The four SRVs are installed on the main steam piping in containment between the reactor pressure vessel and the flow restrictors.

The 3-stage SRV contains a pilot (also called the first stage), a second stage, a main stage, and an air operator.

To monitor these valves for leakage, Pilgrim installed thermocouples at the pilot (first stage), at the second stage, on the tailpipe near the valve (4.5' to 6' away), on the tailpipe far from the valve (-20' away) and at the pilot bellows. Procedure 2.2.23, "Automatic Depressurization System", provides guidance for interpreting the thermocouple data and determining valve operability based in part on testing performed by Target Rock.

Subsequent to installation in RFO-1 8 and prior to this event, Pilgrim experienced minor second stage pilot valve leakage from SRV RV-203-3C on May 18, 2011 and November 25, 2011. Also, on December 26, 2011, SRV RV- 203-3D first stage pilot valve experienced leakage while operating at full power. The SRV was declared inoperable and the plant was shutdown on December 26, 2011 in accordance with TS 3.6.D.2 and RV-203-3C was replaced entirely, and the RV-203-3D pilot assembly was replaced (LER 2011-007-00).

EVENT DESCRIPTION:

On Sunday January 20, 2013, at 2050 hours with the reactor at 100% core thermal power (RMSS in RUN), PNPS declared SRV-3B inoperable and entered Technical Specification (TS) 3.6.D.2 requiring the initiation of an orderly reactor shutdown such that reactor coolant pressure is less than 104 psig within 24 hours. On Monday January 21, 2013, at 1300 hours (16 hrs and 10 minutes) reactor coolant pressure was less than 104 psig. SRV-3B had been declared inoperable consistent with PNPS procedures that state an SRV is inoperable if the pilot stage thermocouple temperature is 350 F below its baseline temperature.

While at full power, indication of a steam leak across the first stage pilot of RV-203-3B was identified. The leakage was evaluated and in accordance with criteria specified in procedure 2.2.23, specifically, if the pilot stage thermocouple temperature is 35 degrees F below its baseline temperature (with a smaller decrease at the second stage thermocouple) and cannot be explained by a corresponding downpower, the SRV is inoperable. The safety relief valve was subsequently declared inoperable and the Limiting Condition for Operation (LCO) for Technical Specification (TS) 3.6.D.2 was entered. Per TS 3.6.D.2 the plant was shutdown and reactor coolant pressure was below 104 psig within 24 hours.

CAUSE:
The SRVs were purchased new, installed, and tested for the first time in April/May 2011 during RFO-1 8.

 Following an extensive investigation, it was determined that the cause of the SRV leakage was that the natural frequency of the pilot assembly was close to a resonant frequency of the valve assembly when installed on the PNPS main steam line. This was not considered in the Entergy specification or the Target Rock design of the

EXTENT OF CONDITION:

This condition potentially applies to all four three stage SRVs that were installed in RFO 18. During Cycle 19 operation, Pilgrim has observed leakage from RV-203-3B, 3C, and 3D. 
·         On May 18, 2011 and November 25, 2011, SRV RV 203-3C second stage pilot valve minor leakage was observed. This condition did not cause inoperability of the valve. SRV RV-203-3C was replaced during the December 26, 2011 shutdown.

·         On December 26, 2011, SRV, RV-203-3D first stage pilot valve experienced leakage that exceeded the operability criteria while operating at full power. The plant was shut down as required by TS 3.6.D.2, RV 203-3C and 3D were repaired and the plant returned to full power operation. The cause of the pilot leakage was later determined to be a combination of the natural frequency issue and weakening of the pilot bellows spring. This bellows spring had a through wall failure during testing at an offsite test facility in March 2013. This failure was the subject of a Target Rock 10 CFR, Part 21 (Reference 1).

·         On January 20, 2013, Pilgrim experienced the event described in this Licensee Event Report, first stage pilot valve leakage of SRV, RV-203-3B. The plant was shutdown as required by TS 3.6.D.2. The pilot valve was replaced with a refurbished pilot and the plant was returned to full power operation.

·         On February 3, 2013, RV-203-3B first stage pilot valve leakage was identified while at full power. Reactor power was lowered to 80% and at 1000 psig pressure, the pilot was reseated. An Operability Determination with a compensatory measure was implemented to maintain the reactor power at 80% and reactor pressure at 1000 psig. An Operations Decision Making Issue (ODMI) was implemented to monitor and take corrective actions. During the forced outage on February 8, 2013, caused by a loss of offsite power due to a major winter storm, RV-203-3B first stage pilot valve was replaced with a new pilot valve and the plant was returned to power operation. The cause of the pilot leakage was determined to be a combination of the natural frequency issue and weakening of the pilot bellows spring. This bellows spring had a through wall failure during testing at an offsite test facility in March 2013. This failure was the subject of a Target Rock 10 CFR, Part 21 (Reference 1).

The removed RV-203-3B pilot valve was sent to Wyle Laboratory for testing.
As-found test results for the SRV, RV 203-3B pilot valve were:
Pilot S/N SRV Position As-Found Deviation

23 RV-203-3B 1112 psig (-)3.8%

Technical Specification 3.6.D.1 requires the as-found setpoint to be within 1155±34.6 psig (1120.4 psig to 1189.6 psig). The as-found setpoint was less than the minimum pressure specification required by TS 3.6.D.1. This test result was entered into the corrective action program as a separate event, and is included in this LER since the condition was discovered within 60 days from the initial discovery of pilot leakage. Accordingly, this as-found value being out of Technical Specification setpoint is reported in this LER pursuant to 10 CFR 50.73(a)(2)(i)(B).

·         The third pilot on RV-203-3B began leaking on February 26, 2013. Leakage was controlled by reducing power and pressure per the ODMI. This pilot was replaced during the Spring 2013 RFO. The cause of the pilot leakage was that the pilot assembly had a natural frequency that was close to a resonant frequency of the valve assembly when installed on the PNPS main steam line.

CORRECTIVE ACTIONS:

The following corrective actions were taken to address this event related to leaking RV-203-3B:

·         The SRV-3B pilot was replaced with a refurbished and tested pilot.

·         PNPS Procedure was revised to reduce reactor power and pressure to stop leakage per an ODMI as described in "Extent of Condition."

The following corrective actions are being taken to address the results of review of Extent Conditions:

·         To minimize the possibility of further pilot leaks, all currently installed pilots (and replacements if necessary until the long term corrective action can be taken) have been set at the high end of their allowed set pressure band.

·         The recommendations of the Target Rock 10 CFR, Part 21 are being followed.

·         The only PNPS pilot with a bellows spring from the same material and heat treatment certifications as the failed bellows was removed from the plant. Detailed metallurgical analysis did not identify any intergranular cracks such as those identified in the failed bellows.

·         PNPS has ordered new pilot assemblies with enhancements designed by Target Rock to raise the natural frequency of the pilot and make it more resistant to steam system vibration (References 2 and 3).

These pilots include the bellows replacement recommended by the 10 CFR, Part 21. PNPS plans to install these pilots during the spring of 2015 RFO.

SAFETY CONSEQUENCES:

The leaking SRV pilot valves and the plant shutdown to repair the SRV in accordance with Technical Specification 3.6.D.2 posed no threat to the public health and safety.

All leakage from the valve was collected in plant systems, the suppression pool (torus), and processed in accordance with normal station practices.

Pilgrim has installed temperature monitoring to provide sufficient indication of SRV leakage to ensure that timely actions can be taken to ensure that the plant is maintained in a safe condition. Procedure 2.2.23 provides the instructions and guidance for interpreting and responding to SRV temperature indications. Based on these instructions, the plant was shutdown. The SRV would have been able to respond if needed to meet its core cooling
or reactor pressure vessel over protection functions. As a result, the plant safety was maintained. The risk of operating with a leaking SRV is characterized by an increased chance of having an inadvertently opened SRV with increased chance of that valve failing to reclose.
Assuming the plant operated for 24 hours with this condition, this results in a change in core damage frequency of less than 1.OE-7. The impact of setpoint drift (0.8% below the 3% tolerance) is considered to be bounded by delta change in core damage frequency of less than 1.OE-7.

PREVIOUS EVENTS:

Prior to Cycle 19, there were no leakage or setpoint drifts occurrences with three stage safety relief valves since the new design was installed in April/May, 2011, during Refueling Outage 18 for all four safety relief valves.

During Cycle 19, Pilgrim observed minor leakage from the second stage pilot valve of RV-203-3C. Also, first stage pilot valve leakage was observed from RV-203-3D which was confirmed, plant was shutdown as required by TS 3.6.D.2, and first stage pilot valve was replaced. This event is described in LER 2011-007-00. During the outage for RV-203-3D, the entire RV 203-30 was replaced with a new valve assembly.

The industry has experienced numerous instances where SRV leakage has occurred at other plants with other Target Rock Model three stage safety relief valves.

OE33766 - Three Stage Safety Relief Valve Pilot Leakage just below Normal Operating Pressure - Plant Hatch. The plant Hatch installed the same model 3-stage SRVs in Unit 2 in April 2011. Hatch experienced numerous pilot leaks during 2011. On some occasions, leakage was reduced by power and/or pressure reductions. Hatch Unit 2 had some success through power and/or pressure reductions and operating for several months after reseating the first stage pilot valve through power and/or pressure reductions.

OE26394 & OE26892 - Planned Shutdown due to a three stage Safety Relief Valve Leak - Peach Bottom Unit 3

OE32805 - Safety Relief Valve Temperature Phenomenon – Fitzpatrick

OE34730 - Target Rock 3 Stage Main Steam SRV Bore to Seat Misalignment - Limerick 2

OE19219 - Plant Shutdown Due to Increasing Tailpipe Temperature - Duane Arnold

REFERENCES:

1. Target Rock Letter NID#13307, "10 CFR Part 21 Report, Notification of a Defect, Bellows Failure," June 17, 2013.

2. Target Rock Technical Evaluation of Replacement Items TERI 075, "Technical Evaluation of Pilot Assembly 304095-1 Replacing Pilot Assembly 303977-1 for 0867F-001," Target Rock, Revision A, January 14, 2013.

3. Target Rock Letter SRP1 3003, "Enhancements to Primary Pilot Design," Target Rock, January 21, 2013.

4. Condition Report CR-PNP-2013-0378, Safety Relief Valve RV-203-3B, Pilot Leakage.























Thursday, March 05, 2015

Pilgrim Juno Scram Linked to History of Prior Failures


Five years earlier, a nor’easter in December 2008 caused a loss of offsite power at Pilgrim, which was accompanied by switchyard flashovers and then an unplanned scram. Entergy was supposed to have determined the root cause and corrected the switchyard flashover problem back in 2008 and again in 2013. Obviously they hadn’t. Instead, in 2013 Entergy had just stored the failed insulator in a warehouse, where the NRC inspectors found it 21 months later.
OF NUCLEAR INTEREST: Pilgrim Juno scram linked to history of prior failures 

By Bill Maurer and Meg Sheehan Posted Mar. 5, 2015 at 2:00 PM Updated at 4:02 PM

On Tuesday, Jan. 27, when winter storm Juno hit Entergy’s Pilgrim Nuclear Power Station (PNPS) in Plymouth, it caused an emergency “scram,” also called a “reactor trip” and more simply known as an unplanned shutdown. Unplanned shutdowns present a risk to public safety, especially when efforts to control reactor temperature and pressure during an unplanned shutdown are complicated by multiple critical equipment failures, as was the case at PNPS during Juno. Juno knocked out Pilgrim for 11 days while Entergy was making repairs to failed equipment.
Pilgrim was no sooner coming back online when winter storm Neptune hit on Valentine’s Day. This time, Entergy shut down Pilgrim as a “precautionary” measure – an explicit acknowledgement that public safety would be at risk if there was another emergency at Pilgrim. Pilgrim was offline for three days, taking an additional five days during restart to reach full power. The U.S. Nuclear Regulatory Commission (NRC) spokesman Neil Sheehan reported that during the restart Entergy was “working through some non-safety related, balance-of-plant equipment problems. These are new issues and not problems from the 1/27 storm. Such issues are not unusual following two shutdowns and start-ups in a short period of time.” 
Entergy’s Jan. 27 Pilgrim scram raised alarms not only with the public, but at the NRC too. The agency sent a six-member special inspection team to PNPS for a week to figure out what went wrong this time. Their report is due by the end of March. 
It’s no surprise that Pilgrim’s aging facilities could not handle Juno and were forced into shut down. In 2013, Pilgrim had four emergency scrams, which put it in the “degraded category” under NRC rules. In the fall of 2014, the NRC investigated the degraded conditions at Pilgrim, and one day before Juno, on Jan. 26, issued a report. The NRC found that Pilgrim failed its inspection because Entergy had not fixed all the problems that caused the four scrams in 2013. One thing the NRC found that Entergy had not addressed was how to handle severe weather events like Juno. Juno proved the NRC right – PNPS was forced to shut down.
The NRC’s Jan. 26 report also found that in 2013 Entergy had failed to deal with a recurrent switchyard performance failure called a “flashover,” which is electricity arcing between two points causing a fault. A failed insulator in the Pilgrim switchyard was identified as a contributing cause of the flashover during a storm in 2013. Five years earlier, a nor’easter in December 2008 caused a loss of offsite power at Pilgrim, which was accompanied by switchyard flashovers and then an unplanned scram. Entergy was supposed to have determined the root cause and corrected the switchyard flashover problem back in 2008 and again in 2013. Obviously they hadn’t. Instead, in 2013 Entergy had just stored the failed insulator in a warehouse, where the NRC inspectors found it 21 months later. Entergy had deferred the funding for the investigation of the failed insulator 11 times, causing the NRC to determine that Entergy “failed to investigate a deficient condition.” 
Since the Blizzard of 1978, switchyard flashovers at Pilgrim have been a recurrent equipment performance failure. Now, Pilgrim has had at least eight unplanned scrams all provoked by Nor’easters delivering blizzard conditions. Pilgrim’s switchyard equipment is located outside, totally exposed to wind-driven salt air, spray, rain, ice and snow. The Juno 2015 loss of offsite power, flashovers and unplanned scram was predictably just one more time.
The NRC’s Jan. 26 report speaks directly to the predictability of recurrent failures during nor’easters: “Inspectors determined that the inadequate guidance for pre-storm actions represented a condition adverse to quality that was reasonably within Entergy’s ability to identify and correct by execution of corrective actions identified in the RCE” (Root Cause Evaluation). Additionally the NRC said Pilgrim has “safety culture” issues and faulted Entergy for “overconfidence and complacency” in the face of safety operations. The NRC says that Entergy’s failure to correct problems is a “significant programmatic deficiency that could lead to worse errors if uncorrected.”
Entergy has had enough chances to fix the many problems that plague Pilgrim. It is time to put public safety first and stop playing Russian roulette with a nuclear reactor having a troubled history of recurrent performance failures.
Meg Sheehan is a public interest attorney and native of Plymouth. Bill Maurer is a retired construction project manager.

Tuesday, March 03, 2015

Netanyahu

I think he is a conservative and he is trying to bolster the conservatives in the USA no matter what it takes. I don’t like him, but it takes a tough bully to survive in that part of the world.
I visited Israel many years ago. I think Israel as our family and brother…do what ever it takes to assure my brother's survival and success. I think we owe that to the dead Jews for our failure before WW II, with standing by and doing nothing. I’ll die for your right of survival today!
Yep, just like us, they are not perfect.
Dam, I think Netanyahu is right. My philosophy is all war or total war, or doing nothing. Knock them out before they can damage our interest or hurt us. I think an injured mad dog running around the world is very dangerous. 
Iran killed or maimed many of servicemen in Iraq or Afghanistan...that is unforgivable!!! 
I think Netanyahu is betting on the right side; Iran is just stringing the USA along and they will never come to any agreement with the USA.

Is he setting up the president for a great fall?

So how is this going to look like in six months with everyone walking away from the negotiating table without no deal.

Netanyahu is playing Obama…

I sometimes think Israel always ends up undermining the current administration…either Bush or Obama…for the perceive greater ends of Israel in the future.
  
Maybe only as a tool for a Israeli politician to get elected.



Monday, March 02, 2015

Magic New NRC Technique Discovers RCIC Flaws At LaSalle Nuclear Plant?

These kinds of postulated shorts have been about the industry for thirty years. The agency has been discovering this often.
See, the NRC’s risk basically comes from a numerical calculation from acceptable core damage or fence line dose. I think this is chocked full with self-interested assumption. Everyone except me thinks if a licensee knows the real risk…this will push the licensee to acceptable behavior. This doesn't work. 
I think these licensees need an incentive, such as once an awhile, a bat upside the head. It will deter other licensees from making the same mistake. 
You catch how they are diluting the feedback...both plants at this site had the same flaws. But the NRC treats it as just a flaw in one plant with a “green very low safety significance”. 
If you believe the assumptions and the efficacy of the NRC’s calculated significance to change behavior…it would be 2 times a green very low safety significance. This is all snake oil…  
Bottom line, the agency doesn't create enough terror in the industry where on the emergence of this kind of accident mitigation flaw discovered, all the industry would be terrified of having the NRC finding one more.

So why did they discover this now, instead of ten or twenty years ago?  
February 27, 2015: LASALLE COUNTY STATION, UNITS 1 AND 2, TRIENNIAL FIRE PROTECTION INSPECTION REPORT 05000373/2014008; 05000374/2014008
• Green. The inspectors identified a finding of very-low safety significance (Green) and associated NCV of the LaSalle County Station Operating License for the licensee’s failure to ensure that the alternate shutdown capability was independent of the fire area. 
Specifically, in the event of a fire in the control room, the alternate shutdown capability for 16 motor operated valves (MOVs) associated with the Reactor Core Isolation Cooling (RCIC) may be affected, and may not be available due to lack of breaker fuse coordination. Fire-induced failures could result in tripping valve power supply breakers prior to tripping the control power fuses for several motor operated valves, thereby, potentially imparing the operation of RCIC from the Remote Shutdown Panel (RSP). The licensee entered this issue into their Corrective Action Program and established compensatory measures, and added steps to the safe shutdown procedures to reset the affected breakers if needed. In addition, the licensee intended to perform plant modifications to replace or revise existing breakers settings to correct the issue. 
The inspectors determined that the issue was more than minor, because fire induced circuits could impair the operation of RCIC and complicated shutdown of the plant in the event of a fire in the control room. The finding affected the Mitigating Systems Cornerstone. The finding was determined to be of very-low safety significance based on a detailed risk-evaluation. This finding was not associated with a cross-cutting aspect because the finding was not representative of the licensee’s current performance.

Friday, February 27, 2015

Palisades: Heading Back to a Yellow or Red Finding, or Worst?

You get the trend, this has repeated over and over again. The NRC attention(yellow finding) marginally drives the safety culture up for a year or two…then it goes back into steep decline.
Right, this is about holes through their titanium gonad shields and vest?  I wonder if there is boys or girls titanium gonad shields? 
It shows how ineffective the agency is.

The deal with the inaccurate dose calculations,  is they can artificially increase the efficiency of the high dose employees. The lower dose allows these employees to work more at other plants and within the radiation fields. Sometimes with big accumulated doses these employees are forced to work in non radiation fields for days, weeks and months because they are getting close to their legal dose limits.   
NRC Has Increased Oversight of Palisades Nuclear Power Plant  
The Nuclear Regulatory Commission staff issued a white finding of low-to-moderate safety significance to the Palisades nuclear power plant for the failure to accurately calculate radiation doses to workers during an activity last year. The finding will result in increased oversight by the NRC. The plant, operated by Entergy Nuclear Operations Inc., is located in Covert, Mich., five miles south of South Haven. The doses received by the workers were below the NRC’s annual radiation limit and are not expected to have any impact on their health. NRC inspectors reviewed of plant’s methodology for calculating doses to workers involved in replacing control rod drive housings during the 2014 refueling outage. They determined that the methodology did not meet NRC requirements. Specifically, the licensee failed to ensure that radiation dosimeters were placed in the highest exposed location of the body for this activity, which resulted in inaccurate dose calculations. In addition, the licensee failed to establish a procedure to ensure proper placement of dosimeters. This resulted in inaccurate calculation and assignment of dose for numerous workers. “Even though this incident did not result in harm to workers, our action underscores the importance of adhering to NRC requirements to ensure an accurate understanding and adequate monitoring of doses to workers at nuclear plants,” said NRC Region III Administrator Cynthia D.Pederson...

Profound financial problem with Entergy? 
Vt. AG pushes NRC to look into Entergy finances
By RICHIE DAVIS

Recorder Staff
Wednesday, February 25, 2015
(Published in print: Thursday, February 26, 2015)

Vermont’s attorney general has endorsed a petition filed with the Nuclear Regulatory Commission raising concerns about Entergy Nuclear’s ability to pay for decommissioning the shutdown Vermont Yankee nuclear plant, and seeking an investigation into its fiscal health in relation to the Vernon plant as well as Pilgrim Station in Plymouth and the FitzPatrick reactor in Oswego, N.Y. 
Vermont’s filing joins a similar action by Massachusetts Attorney General Martha Coakley last October and New York’s attorney general last April in the petition filed by Citizens Awareness Network in March 2013. The petition, still pending before the NRC, raises concerns about Entergy’s financial viability in anticipation of what are expected to be more than $1 billion in decommissioning costs for the plant, as well as the company’s intention to use $50 million of its decommissioning fund — now totaling about $650 million — to provide security of high-level radioactive waste stored on site. 
“The State of Vermont ... has a direct interest in ensuring that Entergy, when financing certain post-closure activities, abides by applicable NRC regulations and contractual obligations, which limit the circumstances in which Entergy can withdraw funds from its Nuclear Decommissioning Trust Fund. To determine whether Entergy — either through subsidiaries or the parent corporation — has adequate financial means without undue or unauthorized reliance on the ... fund, the NRC should fully investigate the financial qualifications of Entergy and its subsidiaries, including directing Entergy to respond to the issues raised by the Attorneys General of New York and Massachusetts,” wrote Chief Assistant Attorney General William E. Griffin. “Vermont also retains a strong interest in how Entergy intends to finance its obligations.”

CAN President Deborah Katz said, “These states are really concerned about how Entergy is going to be responsible.”
She added, “When the Memorandum of Understanding came through for Entergy to buy Vermont Yankee, the parent corporation said that it would cover expenses, and would be responsible if Entergy couldn’t come through with the money. We believe it’s really important to understand Entergy’s vulnerability, in not just an operating reactor, but for issues of safety in terms of cleanup, since they want to end the emergency planning zone and to substantially diminish what’s in the decommissioning fund.” 
Entergy Vice President Michael Twomey told members of two Vermont legislative committees last week that the company offers no guarantees it will pay to decommission the plant if the job is still not done by the end of a 60-year “SAFSTOR” period. The Associated Press reported him telling the House and Senate Natural Resources committees that he expects there would be litigation, with the state and Entergy taking different positions...




Pilgrim Stuck at 22% After Storm Neptune: Beginning To a Pull Fitzpatrick

I keyed Mary into this?

Does Pilgrim need a new Condenser? Will it come down in power 21 times in 6 months? How old is Pilgrim's condenser? 
Leaks force FitzPatrick nuclear plant to operate at reduced power

SCRIBA, N.Y. - The FitzPatrick nuclear power plant in Oswego County has been operating at reduced power since mid-June to compensate for persistent leaks in the plant's aging cooling system that have plagued the facility for the past two years.

Entergy Corp., owner of the 39-year-old nuclear plant, cut power output to about 85 percent of capacity in mid-June to try to reduce the frequency of leaks in its condenser.

The condenser, which circulates water from Lake Ontario to cool the reactor, sprouted leaks on average nearly once a week during the first six months of this year, each time forcing plant operators to reduce power until the leaks could be plugged.

Entergy officials have said they plan to replace all the condenser tubes during a refueling outage scheduled to begin next month. Crews will replace the existing brass condenser tubes with titanium tubes designed to be resistant to Lake Ontario sediments, which are abrasive and contribute to leaking, said Tammy Holden, speaking for Entergy.

Operating at reduced power cuts into what Entergy can earn from the nuclear plant, which company officials described last year as a "challenged facility'' because of its uncertain financial prospects.

The condenser is a large metal box positioned beneath the nuclear plant's generating turbine. Steam that drives the turbine then passes through the condenser, where it is cooled and returned to a liquid state by water from Lake Ontario, which circulates in thousands of small metal tubes.

The U.S. Nuclear Regulatory Commission has said the condenser leaks do not affect public safety, but the leaks have forced numerous unplanned power reductions.

During the first six months of 2014, Entergy was forced to reduce power 21 times to plug condenser leaks, according to NRC inspection reports. From April through June, the facility endured unplanned power reductions at a rate of 23 per 7,000 hours of operation, far exceeding the NRC's recommended limit of six.

NRC officials have criticized Entergy for not addressing the condenser leaks earlier. The condenser at FitzPatrick was last replaced in 1995, and the metal tubes within the condenser have an expected lifespan of 15 years, NRC officials said.

Entergy has not released the date when it plans to begin the September outage. Maintenance during the outage will employ more than 1,500 outside contractors in addition to the regular work force of 623, Holden said.
Love that Mary Lampert? 
Pilgrim’s delay in restart - tube plugs falling out 
My understanding is that the startup delay resulted from the following; please correct me if this is not accurate. 
  • Tube plugs fell out of the condensate tubes. Sea water then leaked into the fresh side of the condenser that contains the water that will go back into the reactor vessel.  
  • Because salt water would cause the stainless steel of the reactor to corrode and eventually cause a failure of the vessel and all its stainless steel pipes, the water is cleaned in the condenser demineralizer.
  • During Pilgrim’s startup, because of the loss of tube plugs, the salt water intrusion was too much for the condensate demineralizers to remove and the feedwater system and the reactor vessel were in jeopardy of massive salt water intrusion. 
  • As a result, the condensate demineralizers were shut down and the resin in the demineralizer was replaced and the tube plugs were re-installed.
Questions:
1. Were some tubes in the condenser plugged because they had failed and were leaking?
a. When did the tubes start to leak?
b. Why were they plugged and not replaced?
c. Did NRC approve that fix?
d. What is the industry history of outcomes of plugging tubes versus replacement?
2. Why did the plugs come out- sounds like poor maintenance is that correct?
a. Is there a guidance or protocol calling for inspection of plugs prior to startup?
b. Were the tube plugs inspected before the recent plant started up?
c. What is the maintenance schedule and how does it match Entergy’s performance?
d. If there was an inspection, was it done right?
e. Supposedly there is a map of the tube sheet that shows what tubes are supposed to be plugged
i. Was the map accurate?
ii. Did the maintenance crew read the map correctly?
3. Did any salt get into the reactor?
a. What tests were performed to assure that salt did not get into the reactor?
b. If any salt did get into the reactor, what protocol should, and will be, followed?
Thank you in advance,
Mary Lampert
Pilgrim Watch
148 Washington Street -Duxbury, MA 02332
Tel. 781-934-0389/Email: mary.lampert@comcast.net

From: McKinley, Raymond
Sent: Tuesday, February 24, 2015 12:58 PM
To: mary.lampert@comcast.net
The Annual Assessment Meeting will most likely occur on March 18. A public meeting notice will be forthcoming soon. We also plan to discuss the results of the 95002 Supplemental Inspection during that meeting. The Special Inspection that was launched following winter storm Juno is still in progress. That report will be issued within 45 days from the exit meeting, so we will not be in a position to discuss the findings of that inspection at the March meeting. 
We can answer some questions relative to the facts surrounding winter storms Juno and Neptune, but we will not be able to discuss any pre-decisional findings.
To your attached questions: 
Were some tubes in the condenser plugged because they had failed and were leaking? 
Yes, some tubes were previously plugged due to previously identified leaks. 
a. When did the tubes start to leak? 
The previously plugged tubes began to leak again following the planned shutdown for winter
storm Neptune. 
b. Why were they plugged and not replaced? 
Tube plugging is the most common repair used in the industry. Condensers are constructed with more tubes than needed to allow any leaking tubes to be plugged. Eventually, condenser efficiency is impacted which results in lost generation revenue for the licensee. 
At or near that point, licensees will either re-sleeve the tubes or replace the condenser water
boxes. 
c. Did NRC approve that fix? 
This is non-safety related equipment repair, and NRC approval is not required. However, as stated above, this is a normal repair used in industry. 
d. What is the industry history of outcomes of plugging tubes versus replacement? 
Plugging is very effective. However, plugs can and do fall out or become loose. The decision to repair or replace is a licensee decision. 
2. Why did the plugs come out- sounds like poor maintenance is that correct? 
Thermal and hydraulic cycling associated with shutdowns and startups were most likely the cause. There is no reason to suspect poor maintenance. 
a. Is there a guidance or protocol calling for inspection of plugs prior to startup? 
Licensees will typically inspect water boxes during a refueling outage but not for mid-cycle outages unless they perform water box work. They did not perform water box work during the Juno or Neptune outages, so there was no reason to perform a water box inspection. 
b. Were the tube plugs inspected before the recent plant started up? 
No, see previous answer. 
c. What is the maintenance schedule and how does it match Entergy’s performance? 
NRC does not regulate condenser maintenance activities. Licensee’s typically perform condenser maintenance during refueling outages or during online maintenance windows. It is in their own best interests to perform condenser maintenance to avoid unplanned down powers / outages from an economic perspective as well as to protect their capital investment. In addition, NRC does have a Performance Indicator which tracks unplanned down powers, so such issues can draw regulatory scrutiny. Pilgrim’s unplanned down power Performance Indicator is solidly in the GREEN range, so it has not been a problem to this point. 
d. If there was an inspection, was it done right? 
NRC does not inspect licensee condenser water box inspections. 
e. Supposedly there is a map of the tube sheet that shows what tubes are supposed to be plugged 
i. Was the map accurate? 
ii. Did the maintenance crew read the map correctly? 
As stated above, NRC does not inspect this activity. However, when leaks were identified
following the winter storm Neptune startup, the licensee used their tube sheet maps to make
sure plugs were still there and tight. They replaced missing plugs and tightened or replaced
any loose plugs.
3. Did any salt get into the reactor? 
The licensee monitors the condenser hotwell and condensate demineralizer discharge for conductivity and chlorides. They detected rising chlorides and conductivity in both locations during the startup which drove them to take corrective action 
a. What tests were performed to assure that salt did not get into the reactor? 
See previous answer. 
b. If any salt did get into the reactor, what protocol should, and will be, followed? 
The licensee follows Electric Power Research Institute (EPRI) guidance, and their procedures drive them to take timely and appropriate action based on the severity of the chemistry conditions. In this case, the action was to hold at reduced power until the issue was corrected. Severe chloride or conductivity excursions can require an immediate shutdown, but the chemistry levels were manageable in this case. The problem was identified and corrected and chemistry levels returned to normal. The licensee will continue to monitor reactor water chemistry and take appropriate action in accordance with the EPRI guidance and plant procedures. Our inspectors will follow up to ensure that the licensee follows their reactor water chemistry procedures. 
Sincerely,
Ray McKinley
Chief, Division of Reactor Projects Branch 5
U.S. NRC Region I
Subject: RE: Comments and questions regarding Pilgrim's delay in restart - tube plugs falling out.
Attachments: 02.23.15 QUESTIONS NRC TUBE PLUGS DELAYING RESTART.pdf
Mary,

Thursday, February 26, 2015

Bailing Out The Exelon Nuclear Plants?

My problems with this. 

1) This is going to support the Exelon structure.

2) No money is mandated into maintenance and updating plant equipment.

3) At the end of it, you still get stuck with these obsolete dogs.

Honestly, you'd be better throwing in a few more bucks for new nuclear plants.

Exelon wants $2 a month more for nuclear plants

SRINGFIELD — Electricity users would have to dip into their pockets a little more to help cover costs of Exelon's nuclear power plants under legislation unveiled Thursday that the influential corporation maintained would save jobs and keep service steady and reliable.Exelon is backing the proposal because it could prop up what it says are three money-losing nuclear plants that produce a relatively clean energy compared to other sources of power. Opponents question whether Exelon would get an unnecessary bailout when a trio of its other nuclear plants are in the black, and supporters of a separate bill prefer a broader approach that would build up renewable resources. 
Where the state ends up on the issue will play out in the months ahead as the spring session unfolds, with companies like Exelon wielding clout at the Capitol through campaign contributions to lawmakers. 
The Exelon legislation comes out of a joint report rolled out last month by multiple state agencies charged with examining the impact of closing nuclear plants and potential ways to keep them open. House Speaker Michael Madigan, D-Chicago, backed the resolution that led to the report. 
Under the Exelon-backed bill, residential customers would pay about $2 more a month, a figure Exelon calculated based on the average bills of customers of Commonwealth Edison and Ameren, which serves much of Downstate. The average residential customer's bill from ComEd, for example, was about $90 in January, the company said. 
The Citizens Utility Board questioned how Exelon, which has made billions of dollars in profit, can ask electricity users to shell out more money to help pay for money-losing plants when "consumers have already paid for those plants several times over."

David Kolata, CUB's executive director, estimated ComEd and Ameren electricity users would pay an additional $300 million a year.

Exelon executive Joseph Dominguez did not directly answer questions about how the legislation may boost Exelon's bottom line and suggested that helping to keep the plants open would benefit consumers.

"What it will help us do is not make profits but avoid losses that otherwise would be treated by retiring plants," said Dominguez, the company's senior vice president for governmental and regulatory affairs and public policy. "The right way to look at this is the consequence of losing the plants."

Under questioning, Dominguez acknowledged the legislation does not include a guarantee that Exelon would keep open the money-losing plants at Byron, the Quad Cities and Downstate Clinton. But he said the company likely would commit to keeping those plants open during the five-year life of the proposal. Such an expiration date is a common clause in Springfield, giving lawmakers a chance to gauge whether changes should be made or a law should go off the books.

The measure would require the state's independent Illinois Power Agency, which buys power on behalf of utility customers, to set up an auction beginning in 2016 to establish the lowest price for low-carbon energy credits. The new money collected from consumers would help pay for those credits, which ComEd and Ameren would purchase. The subsidy would ensure that 70 percent of the electricity the two companies deliver is low-carbon energy.  
If ComEd and Ameren paid too much for the power, based on market value, customers could get a rebate on their bills. Annual increases would be limited to about 2 percent of rates from six years ago, officials said. 
Under the proposal, Exelon would compete against other energy producers that emit little or no carbon dioxide, including wind, solar and clean-coal firms. Critics questioned whether the bill was tilted to favor Exelon.  
Dominguez said Exelon would "hope to be the lowest bidder" but would expect competition to be stiff. 
Democratic Rep. Larry Walsh, whose Will County district includes many nuclear plant workers, said the proposal probably would end up as part a compromise bill negotiated with proponents of separate legislation designed to boost clean energy use and jobs in Illinois.

Walsh, the Exelon bill's lead sponsor, maintained closing the nuclear power would hurt reliability and cost jobs." "If that power were to go away, where's it going to be made up at?" Walsh asked. 
The $31 billion company, the largest owner of nuclear power plants in the country, has been lobbying for positions that would reward it for not emitting greenhouse gases. More than half of the power produced in Illinois comes from coal and natural gas plants and renewable energy....

Simple Door Latch Sticking Problem At Millstone, Indicates A Bigger Problem?

This event reminds me of their LOOP, dual plant trip and the repeated failures of the aux turbine driven feed pump.  
LER 2014-004-00:Unlatched Dual Train Help Door Results in Potential Loss of Safety Function
On December 12, 2014, with Millstone Power Station Unit 3 (MPS3) at 100% power in operating mode 1, an operator

Honestly, why did begin to occur last Dec instead of five years ago?  It this about issues with inadequate budget; the philosophy of a half ass repair job instead of purchasing a new door and its mechanism. I think the door has come to end of life. I called the Millstone resident trying to ask him how old is the door and its mechanism.
There has been a lot of door latch problem with HELB, security and radiation barrier doors in the industry
Why didn't they bring in a door expert instead of depending on a regular maintenance without wide experience and training with doors? 
discovered a door for the MPS3 East Motor Control Center Rod Control area would not latch upon exit from the room. Upon discovery, the door was declared non-functional. Since this door is a dual train High Energy Line Break (HELB) boundary door, it affected the operability of both trains of 480 volt safety related switch gear. Plant Technical Specification (TS) 3.0.3 was entered.
Maintenance personnel repaired the lockset mechanism.

*(So they repaired the door, but nothing was ever wrong with it)
Proper operation of the door was restored within 35 minutes of being identified not functioning properly and TS 3.0.3 was exited. On January 15, 2015, with MPS3 at

Why does it take two bites of the apple? Why isn't this an excuse to rip out this door and replace it with a modern door who is alarmed when not fully latched.  

Why not purchase a heavy, heavy duty door, a high quality industrial door with security and high energy safety quality. The latching mechanism is heavy duty and high traffic quality...it doesn't matter how you open the door? Bet you the door are extremely heavy and the door hinge is worn...it is a misalignment thing.    

100% power in operating mode 1, an individual processed through the door normally and upon checking the door after passage the worker noted the door did not latch. The Control Room was promptly notified. The door was repaired and retested satisfactorily. TS 3.0.3 was

*(The the second time it was repaired, but nothing was ever broken?)
entered and exited appropriately. The door was inoperable for approximately 19 minutes. Although no definite failure mechanism was identified, there have been several occasions where a security door Iockset has been jammed due to usage of the emergency-use-only door hardware (crash bar/thumb piece). In both cases the door Iockset mechanism was manually manipulated, lubricated and then tested several times satisfactorily by maintenance personnel. Inspection of the Iockset mechanism did not find any foreign material in the lockset mechanism. Management issued a special communication to remind plant personnel that security doors not be accessed by the use of the crash bar or door thumb piece/knob/lever except for an emergency. Additional corrective actions are being taken in accordance with the station's corrective action program.
These events are being reported pursuant to 10 CFR 50.73(a)(2)(v)(D), as a condition that could have prevented the fulfillment of a safety function for systems needed to mitigate the consequences of an accident.

Yea, but they were too stupid to test it in all manners of use. 

The latching mechanism was manually manipulated and lubricated by maintenance personnel. Proper operation of the door was restored within 35 minutes of being identified not functioning properly and TS 3.0.3 was exited. This door was then tested over a dozen times without failure.
The door passage mechanism consists of a crash bar on one side of the door and a lockset thumb piece, connected to the latch mechanism in the lockset, on the other side. Utilizing the thumb piece/crash bar causes the lock-set
***I got the problem, the latch and strike or striker is not aligned properly. When you slam the door or it retracts on its own, the full force of the door closing falls on the latch against the strike. Over time this damages or bends the latch…thus it sticks in the retract position.
latch to retract into the lockset, unlocking the latch from behind the strike. When the strike is activated by the personnel security key card, the strike releases the latch. Personnel are then required to simply push the door open. Once the door is opened, the strike resets to its original locked position. The door then closes and latches. The door is now locked in the closed position preventing the door from opening. After the door is unlocked utilizing the security key card, if personnel accessing the door use the crash bar or the thumb piece to open the door, instead of simply pushing the door open, the lockset latch sometimes retracts far enough
Jammed means something is warn and broken...it has to be fixed!!!

I think this occurred a lot more frequently than documented...meaning the exposure time was a lot more.  
into the lockset to jam inside the lockset and fails to return to its normal position, behind the strike, thus leaving the door unlatched. The use of the crash bar/thumb piece is intended for emergency use only and not intended for normal passage.
Although no definite failure mechanism was identified,
*(Just saying, repaired twice and no real failure mechanism to show) 
there have been several occasions where a security door Iockset has been jammed due to usage of the emergency use only door hardware (crash bar/thumb piece).
Another one? Why does it take two bites of the apple
On November 19, 2013 while operating in MODE 1 at 100% power, a security door in the auxiliary building at Millstone Power Station Unit 3 (MPS3) was found unlatched during a door seal check. Upon discovery, the door was successfully latched and the control room notified. In addition to being a security boundary, this door is also a secondary containment boundary, specifically a supplemental leak collection release system (SLCRS) boundary. The door was previously verified properly latched on November 16, 2013. On November 20, 2013 operators determined that the unlatched door resulted in a condition that could have prevented the fulfillment of the safety function of structures or systems that are needed to control the release of radioactive material and mitigate the consequences of an accident. The direct cause of the condition was an unlatched door that did not ensure proper sealing of the credited SLCRS boundary. Upon discovery, the door was successfully latched and the control room notified. Since the door is a SLCRS boundary, it is sealed to tight tolerances and is stiff to open, close, and latch due to the sealing design. The stiffness of the door can be misleading to persons who pull/push on the door to verify it is latched. The door seals and latching mechanism were inspected with no apparent failure and received minor adjustment. Positive assurance of proper latching of doors continues to be reinforced at MPS. This condition is being reported under 10 CFR 50.73(a)(2)(v)(C) and 10 CFR 50.73(a)(2)(v)(D).
Why didn't the door alarm... 
The direct cause of the condition was an unlatched door that did not ensure proper sealing of the credited SLCRS boundary. This door is infrequently accessed and has an alarm if opened. Since the door is a SLCRS boundary, it is sealed to tight tolerances and is stiff to open, close, and latch due to the sealing design. The stiffness of the door can be misleading to persons who pull/push on the door to verify it is latched.

Monday, February 23, 2015

Questions Remain At Pilgrim Plant During the Winter of 2015

Pilgrim Nuclear Plant shutdowns leave questions unanswered for Outer Cape

By Peter J. Brown
Posted Feb. 23, 2015 at 4:12 PM

Just across the Cape Cod Canal, nestled in the hills of Manomet, Plymouth, sits the Pilgrim Nuclear Power Station. During the two blizzards — winter storms Juno and Neptune — that struck over the past couple of weeks, Pilgrim was temporarily taken off line twice. And while there was no apparent threat to the public at any time, the decisions to do so have once again raised questions about the ability of plant operators to maintain safe operations at a nuclear power plant that is over 40 years old.

“In preparation for Storm Neptune, Pilgrim Station made the decision to take the plant off line. We are following plant procedures to prepare for a potential loss of offsite power or the grid's inability to accept the power Pilgrim generates. As always, safety is our number one priority and there is no threat to the safety of plant workers or the general public,” said Meghan Leahy, spokesperson for Entergy Government Affairs on Feb. 14, in an e-mail. Entergy is the plant’s operator.

Danger signs

Keep in mind that even former Nuclear Regulatory Commission chair Gregory Jaczko placed Pilgrim on his list of nuclear power plants that needed to be closed down permanently — the sooner the better.

“[Jaczko] has stated his concern publicly about the safety of these aged Mark 1 GE boiler reactors and recommended that they be decommissioned. The Pilgrim plant has the same containment structure that failed to contain hydrogen gas explosions in the Fukushima plant,” stated Rich Delaney, director of Center for Coastal Studies and chair of the Cape Cod National Seashore Advisory Commission in a letter to Gov. Charlie Baker dated Jan. 22.

“As you now know it remained shut down for several days [after Juno struck] and then reconnected to the grid on Feb. 7. It powered down again on Feb. 14,” said Maureen Burgess, a Truro selectman who serves as that town’s representative to the Seashore Advisory Commission, where she chairs the subcommittee on Pilgrim Safety Concerns.

While the shutdown during Neptune was performed proactively, the events during Juno cascaded along in such a way as to invite scrutiny at many levels. It started with partial loss of off-site power, followed by failure of a condensate pump motor associated with the plant's high-pressure coolant injection system. Then came the malfunctioning of one of the plant's four safety relief valves, and a loss of instrument air resulting in a loss of water level indicators in the seawater intake bays.

Whether these events during Juno spurred plant operators to prudently cease operations during Neptune remains unknown.

“Pilgrim was relicensed for 20 years in 2012 in spite of a sea of protest and concerns about what could be the worst economic and ecological disaster for Massachusetts and make the surrounding areas uninhabitable for generations and poison Cape Cod Bay,” said Burgess. “These areas might include Boston and Cape Cod, depending upon wind direction. Systems are old and subject to deterioration. What appliances do you have in your home that are 40 years old? How old is your car?”

“Entergy has not followed the advice of the NRC's own experts who came up with suggested safety improvements after the catastrophe at the Fukushima Daichi power station in Japan. At Fukushima, all three nuclear reactor cores melted down and exploded within three days,” added Burgess. “The project was called ‘Fukushima Lessons Learned.’ Entergy has not improved the hardened vents on the plant to reduce a release of radiation in the event of a meltdown and explosion, as suggested by the experts.”

No evacuation plan

While other concerns, including the susceptibility of Pilgrim to a seismic event, are raised time and time again, the most troubling dimension of any discussion of the plant’s safety is the fact that there are no evacuation plans for the Outer Cape, or the entire Cape for that matter.

In his letter to the Governor, Delaney said that the advisory commission supported legislation that would expand the radiological Plume Exposure Emergency Planning Zone around Pilgrim, an approximately 10-mile-radius area, to include all of Barnstable, Dukes and Nantucket counties.

“This commission is unanimous in its ongoing concern about the myriad of issues related to [Pilgrim]. The communities on the Outer/Lower Cape and the National Seashore are located only 20 miles downwind from the plant. We continue to be frustrated that the concerns of the citizens on the Cape are not taken seriously by the plant owners or the [NRC], especially in this post-Fukushima era,” wrote Delaney. “One of the principal concerns is the lack of responsible emergency planning for communities on the Cape which would have to be addressed if the emergency planning zone was to be expanded.”

His letter also pointed out that last November, 74 percent of voters in the Cape & Islands Senatorial District voted yes to a ballot question authorizing the state senator to vote in favor of legislation expanding the emergency planning zone.

Mary-Jo Avellar, who represents Provincetown on the advisory commission, is adamant about shutting down Pilgrim and clearly uncomfortable with the fact that the Outer Cape lies so close to, and directly downwind of, the nuclear plant.

“They need to close it down,” said Avellar. “It is unsafe. And it’s terrifying that here we sit in harm’s way and there is no way out for us. We are stuck.”

She commended Burgess for her hard work on the issue. “Maureen has really done yeoman’s work on this. She has been amazing.”

According to Burgess, in the event of a worse-case scenario at the plant, the plans drawn by the Mass. Emergency Management Agency call for all traffic to be stopped at Exit 4 in Sandwich with the ultimate goal of having everyone on the Cape “shelter in place.”

If everyone, including those tourists who are part of the four million people who visit the Cape Cod National Seashore per year, had to be relocated, “where to remains unknown to us. It is possible that we may be unable to return for days, months, years, perhaps never,” said Burgess.

“We have no designated shelters on the Cape, and certainly none that would offer adequate protection. The basement of a typical house would offer 10 to 40 percent protection for a few hours.”

“Our vulnerability has been acknowledged by the industry because our local health departments have been provided with potassium iodide (KI) pills to prevent our thyroid glands from taking up radioiodine. It is unknown how many citizens have availed themselves of these KI pills. So in a sense we have been given a Band-Aid to stop a hemorrhage,” Burgess added. “My concern is that people will see this measure as all they need to do to protect themselves. There are many other radioisotopes that we would not have protection from, e.g., strontium which is absorbed by our bones.”

Public ‘oblivious’

Burgess is most concerned that so many citizens “seem to be oblivious to the danger that lies across the bay. She credits state Rep. Sarah Peake and state Sen. Dan Wolf for putting forth bills “to address the threat to public safety that Pilgrim poses.”

“Now we need Gov. Baker to step up to his charge of ensuring public safety and take on the NRC which licenses Pilgrim. I urge people to let our governor and state and federal representatives know their concerns in this matter,” Burgess said. “An accident is something unexpected and unplanned for. If there is a major radiological event at Pilgrim, we will not be able to call it an accident because too many of us have been anticipating the possible consequences of such an event. It will not be an accident. It will be sheer neglect.”

While Sen. Wolf is mindful of the safety-conscious dimension of a decision to shut down a nuclear plant in advance of a major storm, he is uncomfortable with it at the same time.

“How much confidence does it give us if they have to shut down a nuclear power plant before a storm?” asked Wolf. “What is troubling to me is that each incident there involves its own peculiar set of circumstances. As it ages, it is becoming more unpredictable and inconsistent — two things we don’t want to see with any nuclear plant. And it just gets stranger and stranger.”

“How many warning signs does that plant need to send us?” Wolf asked rhetorically.