Power Reactor Status Reports
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Page Last Reviewed/Updated Friday, December 29, 2017
Whistleblowing can be used as a potent creative tool to help your bureaucracy evolve towards a more enlightened organization. Phone: 1-603-209-4206 steamshovel2002@yahoo.com Note: I constantly update my articles. Comments at the bottom of the article are always welcome!!! Mike Mulligan, Hinsdale, NH
This is getting really dangerous. That is a really bad accident if this occurs...you can certainly count on two or three known other component failures, maybe even poor training showing up, in this accident.
Power Reactor Event Number: 53813 Facility: PALISADES
Region: 3 State: MI
Unit: [1] [] []
RX Type: [1] CE
NRC Notified By: JACOB MILLIKEN
HQ OPS Officer: JEFFREY WHITEDNotification Date: 01/03/2019
Notification Time: 23:57 [ET]
Event Date: 01/03/2019
Event Time: 00:00 [EST]
Last Update Date: 01/04/2019Emergency Class: NON EMERGENCY
10 CFR Section:
50.72(b)(2)(iv)(B) - RPS ACTUATION - CRITICAL
50.72(b)(3)(iv)(A) - VALID SPECIF SYS ACTUATION
Person (Organization):
ERIC DUNCAN (R3DO)
Unit SCRAM Code RX Crit Initial PWR Initial RX Mode Current PWR Current RX Mode 1 M/R Y 85 Power Operation 0 Hot Standby Event Text
REACTOR TRIP DUE TO CYCLING OF TURBINE GOVERNOR VALVE
"At 2028 [EST] on January 3, 2019, with the reactor at 85% power, the reactor was manually tripped due to cycling of Turbine Governor Valve #4. The trip was uncomplicated with all systems responding normally following the trip. Investigation of the cause of the valve cycling is ongoing.
"All full-length control rods inserted fully. Auxiliary Feedwater System actuated as designed in response to low steam generator water levels. Operations stabilized the plant in Mode 3 (hot standby). Decay heat is being removed by atmospheric dump valves.
"This condition has no impact to the health and safety of the public.
"The licensee notified the NRC Senior Resident Inspector.
"This event is being reported pursuant to 10 CFR 50.72(b)(2)(iv)(B) and 10 CFR 50.72(b)(3)(iv)(A)."
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Power Reactor Event Number: 53815 Facility: PILGRIM
Region: 1 State: MA
Unit: [1] [] []
RX Type: [1] GE-3
NRC Notified By: PAUL GALLANT
HQ OPS Officer: DONALD NORWOODNotification Date: 01/05/2019
Notification Time: 17:30 [ET]
Event Date: 01/05/2019
Event Time: 00:00 [EST]
Last Update Date: 01/05/2019Emergency Class: NON EMERGENCY
10 CFR Section:
50.72(b)(3)(v)(A) - POT UNABLE TO SAFE SD
Person (Organization):
ANTHONY DIMITRIADIS (R1DO)
Unit SCRAM Code RX Crit Initial PWR Initial RX Mode Current PWR Current RX Mode 1 N Y 31 Power Operation 31 Power Operation Event Text
POTENTIAL LOSS OF MSIV SCRAM FUNCTION DURING MAIN STEAM LINE ISOLATION VALVE TESTING
"At approximately 1040 EST on January 5, 2019, during evaluation of test results for the 'C' Main Steam Isolation Valve (MSIV), it was determined that closure of three of four
Main Steam Lines would not necessarily have resulted in a full scram during testing due to failure of a limit switch (LS-6) associated with MSIV-1C while in the test configuration. This condition is being reported as an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(v), 'Any event or condition that could have prevented the fulfillment of the safety function of structures or systems that are needed to: (A) Shut down the reactor and maintain it in a safe shutdown condition.'
"The system was restored from the testing configuration at 1057 EST and the failed trip channel was placed in the tripped condition at 1326 EST thus restoring the design function. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified."
Pilgrim Powers Down Due to Faulty Valve
January 5, 2019
The Pilgrim Nuclear Power Station in Plymouth is yet again operating at sharply reduced capacity following as officials continue to deal with valve issues at the plant.
As of yesterday, the facility was working at 23% capacity as workers deal with the problem.
In a statement to CapeCod.com, Pilgrim spokesman Patrick O’Brien that the power reduction came as a result of prescheduled maintenance.
“Pilgrim is currently operating at reduced power due to a scheduled backwash of the main condenser,” he explained.
According to Pilgrim, backwashes are routine maintenance conducted 5-6 times annually to ensure safe and reliable operation of the main condenser by removing mussel growth.
During this power reduction officials at the plant will also be conducting other scheduled maintenance and testing, and would not indicate when they expect to return to full power.
Valves are responsible for regulating water flow into nuclear reactors, and keeping them fully operational has been a consistent issue at the Plymouth facility.
Similar valve issues have led to a number of unplanned shutdowns of the plant this year alone.
Pilgrim is set to permanently close in mid-2019.
Palisades reactor shut down Thursday night
- By ALEXANDRA NEWMAN - HP Staff Writer
COVERT — Palisades nuclear power plant operators manually shut down the reactor Thursday after fluctuations of a turbine governor valve.
“These types of valves control the flow of steam to the turbine,” Palisades spokeswoman Val Gent said.
The event happened just before midnight Thursday and was classified as a non-emergency.
Gent said all systems responded as expected during the shutdown.
The Nuclear Regulatory Commission reported that “all full-length control rods inserted fully. Auxiliary Feedwater System actuated as designed in response to low steam generator water levels.”
Gent said the plant is currently in a safe and stable condition and at no time was the health and safety of the public or plant challenged.
A detailed analysis of the cause and subsequent repair plan is underway.
Palisades returned to service Dec. 28 after a scheduled refueling and maintenance outage that began on Oct. 28. Only one more planned outage is scheduled before the plant is closed in spring of 2022.
Contact: anewman@TheHP.com, 932-0357, Twitter: @HPANewman
***More of same.
Grand Gulf nuclear power plant troubles 'happening far too often,' Mississippi official says
Jeff Amy, Associated Press Published 9:36 a.m. CT Dec. 19, 2018 | Updated 10:15 a.m. CT Dec. 19, 2018
JACKSON, Miss. — Another unplanned outage at Mississippi's Grand Gulf nuclear power plant outside Port Gibson is adding to regulators' concerns over reliability problems at the largest single-unit nuclear power plant in the United States. The move is also heightening scrutiny over whether problems at Entergy Corp.'s plant may be affecting power markets.
Operators took the southwest Mississippi plant offline last week, citing problems with a turbine bypass valve. Last Wednesday's outage came to light Tuesday when the federal Nuclear Regulatory Commission announced a special inspection.
"The reactor was safely shut down but some equipment issues occurred that the agency wants to better understand," the agency said in a statement.
It's at least the sixth unplanned decrease in output at the plant in the last 15 months, according to NRC documents. The plant has been running at reduced or zero power output for much of the time since 2016, according to an analysis published earlier this month by E&E News .
"Over recent years, Entergy's Grand Gulf Nuclear Station reliability record has not met the company's standards," spokesman Mark Sullivan wrote in an email Tuesday. He said the company has invested $265 million and hired about 200 employees seeking to improve operations.
Grand Gulf took a nearly six-month outage in 2016 and 2017 aimed at improving performance because the plant didn't, in the words of Chief Nuclear Officer Chris Bakken, "meet our standards of excellence." There was more self-scrutiny during a planned refueling outage this spring, with Entergy CEO Leo Denault promising investors in April that "we expect the reliability with the plant and its capability factor to improve going forward."
Sullivan, though, says improvement will take time.
The plant's troubles come as President Donald Trump continues to support plans to subsidize nuclear power generation for reliability purposes. Sullivan said the plant had restarted Tuesday and NRC figures showed its output was up to 18 percent.
Grand Gulf, which began generation in 1985, is 90 percent owned by Entergy and 10 percent owned by Cooperative Energy, a Mississippi group that supplies power to member-owned cooperatives. Entergy's subsidiaries in Mississippi, Arkansas, New Orleans and Louisiana have contracts to buy power from the plant.
In November, Nuclear Regulatory Commission regulators wrote Entergy a letter notifying that it was downgrading the plant's safety rating from green, the safest of four levels, to white, the second safest. The letter cited a number of equipment failures. Consequently, the commission said, it was planning a supplemental inspection to explore the root causes of the problems, to independently assess conditions and to make sure problems had been corrected and wouldn't recur.
Beyond questions of safety, the absence of Grand Gulf's 1,443-megawatt capacity can stress power supplies and may cause higher prices across Mississippi, Arkansas, Louisiana and southeastern Texas, a region that includes not only New Orleans-based Entergy's utilities, but cooperatives and private utility Cleco of Pineville, Louisiana.
In January and September, the Midcontinent Independent System Operator, which manages the region's electrical grid, ordered emergency conservation because of possible power shortages. The September and January events both happened while Grand Gulf was offline or at low power. Entergy's River Bend nuclear plant near St. Francisville, Louisiana, was also offline during the January cold snap.
"Just the scale of it, it's so big that you notice when it's missing," said Ted Thomas, chairman of the Arkansas Public Service Commission. "It doesn't take many other issues in addition to give you a problem."
The Federal Energy Regulatory Commission and the North American Electric Reliability Corp. announced in September that they were jointly investigating the January event. The Louisiana Public Service Commission is also investigating.
Mississippi Public Service Commission Brandon Presley said Tuesday he would ask the agency's independent staff to investigate the outages and determine whether the commission should open an official proceeding.
"This has been happening far too often," Presley said.
Arkansas has not launched an official inquiry, but Thomas said Grand Gulf "has our attention."
Entergy spent hundreds of millions to increase the plant's generating capacity in 2012, setting it up to be a cornerstone of low-cost generation in the region for decades, especially after winning a 20-year extension of the plant's license from the NRC through 2044. But when it's down, utilities have to buy power from other plants in the MISO region.
"We're paying to have that plant generate and when it doesn't generate, we have to substitute," Thomas said.