Wednesday, April 29, 2015

Jan 2014 Messages to Senator Shaheen about Seabrook


Jan 2014 Messages to Senator Shaheen about Seabrook

Bottom line, they only replaced a small percentage of the defective service water piping.  
Apr 28 2015
Service Water Piping Replacement for the Diesel Generator and Primary Component 
Cooling Water Heat Exchangers 
a. Inspection Scope The team reviewed EC 274172 which replaced degraded Plastisol-lined service water (SW) piping on the supply and return of the ‘A’ and ‘B’ emergency diesel generator (EDG) heat exchangers and degraded cement-lined SW piping on the supply side of the ‘A’ primary component cooling water (PCCW) heat exchanger. NextEra performed the modification to replace degraded SW piping with a corrosion resistant material to ensure long-term system pressure boundary integrity. NextEra replaced the carbon steel lined piping with AL-6XN, an austenitic stainless steel material, suitable for seawater service without the need for internal lining or protective coating.

I give Senator Shaheen a B+ on this. She got it all on the record. But she never had any active involvement or follow-up. The office never stayed on top of it. The NRC read her like a book..felt she would be happy just getting this on record. 
Writing to Senator Shaheen office and on the NRC docket
Remsburg, KristyFrom: Holmes, Sarah (Shaheen) [mailto:Sarah Holmes@shaheen.senate.gov]
Sent: Tuesday, January 07, 2014 10:09 AM
To: Dacus, Eugene
 Subject: FW: Seabrook issues
 Gene, Happy New Year- I hope you and your family had a nice holiday and are staying warm. Please see the note below from the Senator's constituent Mike Mulligan . He is very concerned about issues with deteriorating plumbing around the plant at Seabrook. could you please provide us with a formal reply to his concerns/allegations Thank you, please let me know if you need any additional information Kind Regards,


Sarah
From: Michael Mulligan [mailto:steamshovel2002@yahoo.com]
Sent: Wednesday, December 18, 2013 1:22PM
To: Holmes, Sarah (Shaheen)
Subject: Re: Seabrook issues
 Sarah, If you don't talk tough to these guys, they will allow Seabrook to deteriorate into a Vermont Yankee. This is very similar to their concrete problem where it took much more NRC action. I never have any confidentiality or anonymity needs what so ever! Mike  

Dear Senator Shaheen, These comments below are from the NH Union Leader newspaper by Seabrook Station's Local 555 Union President Ted Janis on Nov 26, 2013. They were negotiating a union contract.

"Their battle cry is 'natural gas' is killing us. We are not making the money we were making five years ago,'" said Jenis. "But it's hard for us to sit here and see these raises go out to management."
"This is a workplace that has been beaten down over the last few years," he said."

"There seems to be a total attitude change toward the workers from the corporate level."

"This is a workplace that has been beaten down over the last few years," he said."

Seabrook nuclear plant was brought on line in 1990 with cheap and non-corrosion resistant carbon steel service water piping. Within two years, piping integrity problems began showing up with pitting and local corrosion. And this problem has only gotten worst and it's running out of control as I write. It is corrupting the staff of this organization.

In 2011 they replaced a 30 year old 8 foot section of 24 inch {huge) width pipe qn the service water strainer by pass line. I think because of corrosion issues. It seemingly had a secret failure of some sort in 2011, as the NRC didn't disclose it in their most recent inspection report (2013001).

They replaced it with new carbon steel piping that was lined with so called super epoxy material Belzona. It failed within three years during August of this year. This is called progress. How do we know if the Belzona isn't going to clog again the emergency diesel generator cooling water orifices?

As it stands right now, the pipe only has a Band-Aid over the wound till the next outage {late spring 2014). Seabrook and the NRC will tell you they ultrasonically tested the hell out of this section of pipe once they detected it leaking. This device shows you the thickness of the metal piping. This is a nuclear plant and a crucial nuclear safety component...one which just failed mysteriously after 2 years ... why weren't they UTing the hell out the pipe before it leaked, as they knew the carbon steel service water piping was seriously corrosion prone? Why wasn't there an intense program to uncover any corrosion throughout the system and especially on the strainer bypass line that already failed?

Why didn't they catch the defect before it first leaked ... then catch it before the tinfoil thickness pipe wall burst and the leak got even bigger threatening the design of the plant? This is a matter of trusting them and their integrity. This is a matter of the NRC prodding them over and over again about following their procedures and using conservative engineering ethics. 
Seabrook through August this year didn't want to shut down over a pipe leak fearing a summer grid emergency with limited electricity and in a heat wave with expensive replacement electricity. Was this all about money and very little about public safety?

Seabrook obtained regulatory good will and forbearance to not shutdown to fix this dangerous leak even after botching the UT reading. The American Society of Mechanical Engineers sets the engineering standards that the NRC requires Seabrook to abide by. The ASME nuclear piping codes requires Seabrook to repair the pipe ... not a temporary repair like the NRC gave them permission to do. I bet you they want Seabrook to actually see the damage inside by eye to make certain they know what is going on ... not guessing. They could have kept this plant up at power if they first designed this plant prior to construction with sufficient extra service water capacity and flexibility in this area.

ASME Standards used in over 100 countries

ASME members provide engineering and technical expertise to policy makers in Congress, the White House Office of Science and Technology policy, and key federal agencies"

You get it, the poor initial plant design of the service water system sets Seabrook up to cry tike a baby to the NRC with the burdens of code and agency compliance. Your brother Pilgrim (Entergy) plant up north and the NRC doesn't have a care in the world with any "shutting the plant down in mid-cycle creates undue and unnecessary stress on plant systems, structures, and components" during the last year over all the multitudes of shutdowns and scrams they had caused by their poor plant upkeep and maintenance. These are nothing but excuses of convenience and it borders on another falsification in federal documents. 

It is impractical to complete a Code-acceptable repair to the identified SW leak at Seabrook Station without shutting the plant down. Shutting the plant down in mid-cycle creates undue and unnecessary stress on plant systems, structures, and components." (Sept 4, 2013)

I don't think these guys deserved any regulatory forbearance. They should have prepared their service water system years before for the rigors of summertime operations. This is how you protect the consumers from the potential of electricity shortages and maintain nuclear safety. Nuclear safety never comes from undeserving regulatory good will. Honestly, they need to spend big bucks to fix their service water. Course, the grid might be more vulnerable in winter time operations and with our limited natural gas piping capacity. They should have spent our good money towards the aims of making this plant reliable without regulatory nuclear safety forbearance during these critical summer months. Do you think the NRC's regulatory good will and forbearance will get us a reliable service water system for the rest of the life of this plant?

The service water cooling system supports all the reactor core cooling and the emergency diesel generator. This is certainly their Fukushima nuclear safety system. I spent considerable time talking to the NRC senior resident inspector and his boss the branch chief. The senior NRC resident frames the quality of the carbon steel service water piping system as "crap". Every professional in the field knows this is grossly inappropriate material for a salt water system.

Because of the poor quality of the carbon steel and its reckless susceptibility to early failure and all sorts of corrosion, they have lined (inside) portions of the piping with concrete, plastisol and Belzona. Seabrook began using plastisol in 1992 two years after first operation of the plant. The station was oblivious to the fact that the plastisol only has a service life of fifteen years. The NRC had to remind them of this. The brittle and pitted plastisol then sheeted off the piping and clogged a cooling orifice into a Fukushima emergency diesel generator. The machine didn't have enough cooling water and the station botched the "operability determination" over this twice. The big event you should be worrying about is any of the cement, plastisol or Belzona detaching from the inside of the piping and clogging up the water flow or damaging any of the valves.


I believe Seabrook knowingly falsified internal paperwork (prompt operability determination (POD)) the NRC depends on it to make a regulatory judgment. Is it safe to stay up at power orshould they shut down? Seabrook has made a string of bad "operability determinations" over the recent years and nothing the NRC does seem to turn these guys around into making accurate operability determinations. Seabrook had a leak in their service water system and they used a ultrasonic detector to measure the nature of hole in the pipe. They had information the hole was a very dangerous type which could leak big amounts of water ... but they put on the POD document it was a safe and stable hole. Within weeks the hole widened and leaked significant amount of water inside the plant threatening other safety equipment.

I questioned the Branch Chief and senior NRC inspector. They tell me Seabrook didn't adequately support their prompt operability determination (POD). This is a basic operation's safety function at a nuclear plant and they are all trained much on it. What are they even up at power for if they can't perform this simple determination? These guys are all extremely educated and there are many employees with advanced engineering degrees who ultimately make these determinations. It doesn't wash with these really smart and educated people making these kinds of simple mistakes. What they are really good at is covert-ups and playing stupid. Like I said, this plant has had lots of bum service water safety operability determinations lately ... why isn't the punishment cumulative? They had at least two stupid and inaccurate operability determinations with erratic cooling water flow indication to an emergency diesel generator. The dangerous brittle and over aged so called protective plastisol that sheeted off the sw pipes. What does it take to turn their hearts? What does it take to make accurate and safe operability determination? How will this faux stupidity end? This revolved around
an accurate UT scan of the pipe hole on day one and the staff blowing it with getting the information into the "Prompted Operability Determination".(wink wink)

I questioned the NRC inspector Mr. Cataldo about if it was a falsification of documents or if the NRC interpretation was Seabrook didn't adequately support the POD. How could these really smart and highly trained employees ever make that kind of simple mistake? He said, "Mike, it was just gross staff incompetence" surrounding the reading of the UT and getting the correct information into the POD." I still believe it was an intentional willful! falsification of documentation and the NRC is sweet talking this event into a poor support of the POD. But the great problem now is; why didn't the NRC accurately characterize this event as "gross Seabrook staff incompetence" surrounding the UT and the characterization of the hole in the NRC's inspection report? Does the NRC have two tiers of reporting, the prettified talk in the inspection reports for the community and the actual events at the plant?

I have real issues with the early failure of the new carbon steel piping and its super epoxy material Belzona. The nuclear industry is riddled with issues of improper heat treatment of metals and using the wrong type of metal. Remember, the old section of pipe failed mysteriously after 30 years. You get it, they never depressurized this section of piping. They never eyeballed the flaw inside the pipe and taken samples for sophisticated metallurgical analysis at an approved engineering laboratory. And these guys are terrible at guesswork. It could be related to microbial corrosion, electrochemical reactions with dissimilar metals and cement is a great worry.

"As previously stated in Section 7.2, the cause of the degradation is from localized corrosion.The typical corrosion rate used in Seabrook Station Service Water piping evaluations is 30 mils per year (mpy). However, the current identified wall defect resides in piping which was recently replaced during Refueling Outage 14 during April 2011, concluding that an accelerated (presently unknown) mechanism exists within the bounding area." (Sept 4, 2013)

The new carbon steel and the super coating failed after two years. The NRC's branch chief says the seawater in the bypass line is stagnant, but is open at the downstream connection. Nowhere in their documentation does it explain why the new section of piping failed so quickly other than to imply it is the same corrosion mechanism that destroyed the 30 year old first pipe. I think it is a new failure mechanism and other areas of the pipe could also fail quickly.

And believe me, there is no way to get an objective and independent interpretation of what went on here. The NRC and Seabrook have dog in this race with protecting their credibility ... you would need a recording (voice, visual) of the initial control room discussion about this hole with the NRC and then a recording of any subsequent discussion on this. Can you even imagine in a nuclear plant's safety cooling water piping, the NRC would allow the metal destruction mechanism to remain unknown?

Senior inspector Paul Cataldo told me he fought like hell with his bosses trying to get a bigger violation over this. He talked to me about the burdens the agency only gives him with a very limited weekly or month time budget with events at the plant. He put in a lot of time with this non violation. No overtime and certainly no paid overtime. I got the impression he thinks his bosses don't fully support him as they should and he is worried Seabrook's management doesn't respect him for his Federal oversight role at the plant.

I have called Seabrook's security gate and left a message asking to speak to an engineer about the sw strainer piping leaks. 
Better, somebody in the know within the operations department. I am still waiting for that call back?

Sincerely,
Mike Mulligan
Hinsdale, NH
(Ce11)16032094206

'The Popperville Town Hall'
http://steamshovel2002.blogspot.com/
On Friday, December 13, 2013 2:35 PM, Michael Mulligan wrote:
Sarah,
There we go!
Mike


On Friday, December 13, 2013 2:27PM, "Holmes, Sarah {Shaheen)" wrote:

Hi Mike,
Let's try this one more time.
Sarah

From: Holmes, Sarah (Shaheen)
Sent: Thursday, December 12, 2013 10:17 AM
To: 'steamshovel2002@yahoo.com'
Subject: Seabrook issues
Mike, 
Nice talking with you today. As we discussed, can you please send me a summary of the issues with leaks at Seabrook, that would be very helpful. I will forward along to the NRC with a cover note from the Senator asking for a response and additional information.

Kind Regards,
Sarah
Sarah Holmes
Special Assistant for Policy and Projects
Office of U.S. Senator Jeanne Shaheen
340 Central Avenue, Suite 205
Dover, NH 03820
P: (603) 750-3004
F: (603) 750-4046
sarah holmes@shaheen.senate.gov
s1gn up '"or
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"Their battle cry is 'natural gas' is killing us. We are not making the money we were making five years ago,'" said Jenis. 
"But it's hard for us to sit here and see these raises go out to management."
"There seems to be a total attitude change toward the workers from the corporate level."
ASME Standards used in over 100 countries
ASME members provide engineering and technical expertise to policy makers in Congress, the White House Office of Science and Technology policy, and key federal agencies"
"6. Burden Caused by Compliance
"As previously stated in Section 7.2, the cause of the degradation is from localized corrosion. The typical corrosion rate used in Seabrook Station Service Water piping evaluations is 30 mils per year (mpy). However, the current identified wall defect resides in piping which was recently replaced during Refueling Outage 14 during April 2011, concluding that an accelerated (presently unknown) mechanism exists within the bounding area." (Sept 4, 2013)

5

More Crap Service Water Piping At Seabrook!


“replace degraded SW piping with a corrosion resistant material: AL-6XN austenitic stainless steel material
SeabrookNuclear Station's "Crap" Service Water Piping System
Senator Shaheen's Help With Seabrook's Deteriorated Service Water Piping

Seabrook's Crap Service Water System
So now the truth comes out. I have gone over a lot of Seabrook’s documents with degraded service water pipes. I knew Seabrook used inappropriate piping materials leading to premature corrosion and pipe leaks. The Seabrook solution was to put a ban aid on the gaping pipe wound...the cement liner and plastisol lined pipe. The foreign material lined piping caused a flow reduction and the material has sloughed off causing blockage in other areas of the plant including the diesel generator.
"...replaced degraded Plastisol-lined service water (SW) piping on the supply and return of the ‘A’ and ‘B’ emergency diesel generator (EDG) heat exchangers and degraded cement-lined SW piping on the supply side of the ‘A’ primary component cooling water (PCCW) heat exchanger..."

Most troubling in all the Seabrook and NRC degraded service water documents...the NRC and Seabrook never admitted the root cause of their trouble was inappropriate pipe metal. Because if they admitted it, all the piping would have needed to be replaced.

Just to be clear, if all of the service water piping was made of AL-6-XN austenitic stainless steel, there never would have been a need of any plastisol or cement service water piping liners. The NRC says this piping was degraded, why wasn't this in a LER and why wasn't Seabrook forced into a tech spec LCO?  

It just  gets you wonder how much more safety information they withhold from the public because it reflects bad on the agency. 
April 28, 2015: SUBJECT: SEABROOK STATION, UNIT NO. 1 – NRC EVALUATION OF CHANGES,  TESTS, AND EXPERIMENTS AND PERMANENT PLANT MODIFICATIONSTEAM INSPECTION REPORT 05000443/2015007 Service Water Piping Replacement for the Diesel Generator and Primary ComponentCooling Water Heat Exchangersa. Inspection Scope The team reviewed EC 274172 which replaced degraded Plastisol-lined service water (SW) piping on the supply and return of the ‘A’ and ‘B’ emergency diesel generator (EDG) heat exchangers and degraded cement-lined SW piping on the supply side of the ‘A’ primary component cooling water (PCCW) heat exchanger. NextEra performed the modification to replace degraded SW piping with a corrosion resistant material to ensure long-term system pressure boundary integrity. NextEra replaced the carbon steel lined piping with AL-6XN, an austenitic stainless steel material, suitable for seawater service without the need for internal lining or protective coating. 

The team reviewed the modification to determine if the design basis, licensing basis, or performance capability of the EDG, PCCW, and SW systems had been degraded by the modification. The team interviewed design engineers and reviewed design drawings and calculations to determine if the new SW piping met design and licensing requirements.
Additionally, the team reviewed non-destructive examination (NDE) results and associated maintenance work orders to determine if NextEra appropriately implemented the modification. The team performed several walkdowns of the accessible portions of the replaced SW piping, including a walkdown during a prolonged ‘A’ EDG run on March 5, 2015, to verify that NextEra had adequately implemented the modification, maintained pressure boundary integrity and configuration control, and had not impacted the function of other safety-related SSCs located in the vicinity. The team also reviewed corrective action CRs and the EDG, PCCW, and SW system health reports to determine if there were reliability or performance issues that may have resulted from the modification. Additionally, the team reviewed the 10 CFR 50.59 screen and engineering evaluation associated with this modification. The documents reviewed are listed in the Attachment.

Tuesday, April 28, 2015

Fuel Failures At Garbage Dresden?

Who gives a shit why it happen? 

April 27, 2015: DRESDEN NUCLEAR POWER STATION, UNITS 2AND 3  INSPECTION REPORT05000237/2015001; 05000249/2015001
Unit 3 began the inspection period at full power. On January 9, 2015, reactor chemistry sampling confirmed that a small fuel failure existed in the core. On January 17 operators reduced power to 82 percent to conduct testing as part of fuel failure identification and verification efforts, and returned to full power on January 18. On January 29, 2015, operators lowered power to 50 percent to conduct power suppression testing and identify the core location of the failed fuel. The failed fuel was identified and mitigated, and Unit 3 returned to full power on February 3. On February 28, 2015, the operators reduced power to 58 percent to conduct control rod sequence exchange, and full power was restored on the same day. With the exception of short periods for routine maintenance and surveillances, Unit 3 operated at or near full power for the remainder of the inspection period.

What a disgrace? 
Green. A finding of very-low safety significance, and an associated NCV of 10 CFR 20.1701 was self-revealed during work activities associated with the failure to effectively implement planned radiological engineering controls during reactor head reassembly that resulted in personal contaminations and unintended radiological intakes to workers. On November 14, 2014, during the cleaning of the reactor head studs, several workers on the refuel floor were contaminated, and received unplanned and unintended intakes of radioactive material. Corrective actions included revising applicable procedures to improve the engineering and contamination controls during reactor head reassembly.

Monday, April 27, 2015

Russia: The Global Walmart of Revolutionary Uranium Centrifuging?

Why isn't the USA the Walmart of Revolutionary Uranium Centrifuges?

Man, is Russia more transparent than the USA?  
Russia 1st to test 10Gen uranium enrichment centrifugesPublished time: April 27, 2015 11:37
Edited time: April 27, 2015 12:26
RIA Novosti / A. Solomonov
Rosatom, Russia’s nuclear agency, confirms scientists are testing 10th generation centrifuges. No other country even possesses 9th gen tech, putting Rosatom years ahead of the competition. 
“We’re on to 10 Gen,” announced Aleksandr Belousov, general director of Urals Integrated Electrochemical Plant (UIEP), a Rosatom subsidiary in Novouralsk, Sverdlovsk Region, in the Urals. 
“Scientists and engineers are solving technical issues, which is quite difficult. Any kind of new research and technological development is a venture undertaking, you can either succeed or fail... Any new machinery must be economically efficient. [10Gen] is being developed out of economic expediency, not for mere modernization. The more energy-intensive the machinery is, the more technical problems emerge,” Belousov said.
A gas centrifuge uses principles of centrifugal force to perform radioisotope separation of gases, by accelerating molecules to such an extent that particles of different masses are physically separated within a rotating container. 

The centrifugal separation of isotopes is used for various purposes. First of all for production of low-enriched (up to 3-4 percent) uranium to be used as fuel at nuclear power plants. It also is used to produce weapons-grade, highly-enriched uranium (90 percent of U-235). Centrifuges are also needed to produce radioisotopes for medicine and various technical issues.  View image on Yahoo website
Centrifuges are operated in cascades of hundreds and thousands units. Manufacturer supplies centrifuges in assemblies of 20 units in two rows, and at the factory they are placed on the columns in tiers, one above the other. 
Last week the second cascade unit of 9 Gen gas centrifuges has become operable at
9GEN makes Russia the world leader?
the UIEP, with the first 9 Gen unit introduced in late December 2013. Having two 9 Gen centrifuge cascades means that UIEP is the leader in the industry, making up to 48
48% of the Russian market and 20% of the global market?
percent of Russian radioisotope market and 20 percent of the global market, RIA Novosti reports. Image from sdelanounas.ru
The 9 Gen centrifuges are four times more productive than 8 Gen centrifuges, which means a similar productivity pace should be applied to 10 Gen units, Belousov said.
Development of nuclear enrichment centrifuges in the Soviet Union began in 1952. Over the time general dimensions of the machinery changed a little yet the productivity has augmented by 14 times, whereas operating costs have diminished by at least 10 times, aide to the UIEP head, Gennady Solovyov, said. 
The modern Russian centrifuge is a state-of-the-art component made of composite materials and special aluminum alloy. Its rotor spins with unbelievable speed of 1,000 rotations per second and can do it without a single stop for 30 years. Mechanical malfunctions are extremely rare, no more than 0.1 percent (one failure per 1,000 units) per year. 
 
Russia’s TVEL Fuel Company (TENEX for operations abroad) is the largest operator of nuclear enrichment centrifuges and absolute leader of world’s radioisotope market, possessing about 30,000 separative work units (SWU), which is almost half of the world’s total 65,000 SWUs. Russian centrifuges are also the most advanced and have higher output capacity than SWUs from rival companies in France, US or Japan.View image on Twitter
Starting from 2009 Russia is supplying 7 and 8 Gen centrifuges to China.The second-largest operator of uranium enrichment centrifuges after Rosatom is URENCO, a joint German, Dutch and UK enterprise operating 14,200 SWUs.
Rosatom is heavily investing in nuclear enrichment at the UIEP. In 2014, the corporation allocated 7.5 billion rubles (nearly $150 million), whereas for 2015-2019 Rosatom plans to spend on the UIEP no less than 34 billion rubles (about $667 million).

Thursday, April 23, 2015

Brunswick Junk Norberg Diesel Generator.

Brunswick NRC Inspectors Finding DG Day Tank Vent Pipe Violation Like Waterford?

So we are now heading towards a 2.206 on Waterford...(The 2.206 was going to be about missing missile protection on the DG day tank. I just found the NRC identified it on their CDBI inspection. So now the 2.206 is unnecessary.)

Does Waterford have tornado protection on day tank vent lines?
Roof- both A and B
dg fan-B
Dam CDBI- Specifically, between October 8 and 16, 2014, the licensee failed to initiate a condition report to evaluate the lack of missile protection on the emergency diesel generator A and B storage tank vents, a nonconformance that is a condition adverse to quality. In response to this issue, the licensee performed an operability determination to address the team’s concerns and initiated a separate condition report to document the failure to initiate a report for a condition adverse to quality.
So I am not going to have the issue Brunswick got a violation over not missile shields and the NRC ignored it in Waterford.
Bottom line, with the absent missile shield on the day tank vent lines, the DG vent fan being inop since the bugled maintenance on the B in 1999 and the corrosion on the dg day tank vent lines...the operability of the the diesel generators was impaired on multiple causes for decades. The NRC paper whips these guys on the isolated issues, they don't look at these things holistically, with  poor maintenance over multiple issue has cast a terrible possible reliability problem over both diesel generators. Basically thy don't hit Entergy with a big enough hammer to get they to globally change their tune.
You notice post CDBI missile protection finding they have picked it up at another plant-Brunswick. After all these years, why hasn't the NRC caught the divergent from licencing condition across multiple plants. Why is the industry so lackadaisical  with maintaining their original licencing conditions.
Waterford on the broken DG  fan picked up by luck, they weren't positively monitoring the DG ventilation flow...they by procedure didn't have a positive way to immediately detect a DG fan was broken.  
Bottom line, I doubt the NRC knows the totality of all the broken or degraded safety components and the deficiencies in the plant's organization at WaterFord...it is very worrisome. 
Just saying, the probability of tornado winds capable of damaging the DG day tank vent piping is not transparent.
No extent of condition with is the site within the plant design on severe weather.
I still say heavy winds could drive up debris onto the roof above the DG day tank and clog up the roof drain?  
I still say the adequate punishment would have been, you need to assume that the NRC didn't catch this, Waterford was incapable of catching it. The assumption should have been in some future both vent pipes would have rotted through, or tornado or hurricane winds would have picked up missile debris knocking off the badly corroded vent pipe...in a hurricane with a LOOP WaterFord would have lost both DGs on water intrusion into the day tank and been in a blackout. It should have been a red finding.

The worst this to do in plant accident is to tie the hands of the operators around their back...have degraded or broken equipment show up way down the EOPs. 

What you see on the big picture, the NRC has to bail them out with violations or exemptions, equipment fails over poor maintenance...Waterford can't catch problems on their own before accidents and failed equipment shows up.
As an interim action, a stainless steel pipe clamp with a rubber liner was installed around EDG Feed Tank
vent pipe to prevent water intrusion

http://www.tornadohistoryproject.com/tornado/Louisiana/map

Tornadoes in Louisiana

Date(s) (yyyy-mm-dd)TornadoesFatalitiesHighest FatalitiesInjuriesHighest InjuriesLongest PathWidest Path
1950-02-12 - 2013-12-211827206 people47 people3339 people510 people234.7 miles3080 yards

Mike, so is there a difference between a day tank ventilation piping (Brunswick) and a day tank vent pipe (Waterford). They both fill of the Diesel Generator day tank and could take out the DG.

They really never mention specifically the DG  fuel oil. Bastards.

With ventilation you are usually talking moving air, bigger pipes and a motorized fan???

I am calling vent piping and ventilation piping the same...

Waterford's DG day tank vent pipe fiasco:
January 22, 2015 WATERFORD – NRC COMPONENT DESIGN BASES INSPECTION REPORT 05000382/2014007 AND PRELIMINARY GREATER THAN GREEN FINDING
 April 09, 2015: WATERFORD UNIT 3 – NRC SUPPLEMENTAL INSPECTION REPORT 05000382/2015010
See how incredibly erratic the NRC is with violating a plant. Two plants with NRC inspectors finding issues of the possible unreliability of the diesel generators that the plant staff's didn't find.

So Waterford repaired the corroded DG vent piping with rubber and hose clamp...how can that stand up to a tornado. Why didn't the NRC inspectors violate Waterford on tornado protection like Brunswick?

Introduction. The NRC identified a Green NCV of 10 CFR Part 50, Appendix B, Criterion III,
Design Control, for failure to ensure adequate tornado missile protection for the EDG 4-day
Actually this is the first mention of fuel oil tank...I am certain its the vent line. Well, 99.5% certain.
fuel oil tank ventilation piping.
Description. On May 8, 2014, during a walkdown, the inspectors noted that the EDG 4-day fuel oil tank ventilation piping was not protected from tornado-borne missiles. The inspectors questioned the licensee on the whether this piping needed to be tornado protected, and if so, could it withstand the design basis tornado and rain event. On August 14, 2014, under WO 13421302, the licensee took corrective actions to place concrete blocks around the ventilation piping. An engineering evaluation was then performed that identified the worst case design basis tornado and rainfall scenario conditions and what effect those would have on EDG operation. It was determined that with the maximum 24-hour rainfall rate and a tornado missile shearing the ventilation piping at the roof level, the worst case scenario was the EDG1 4-day tank filling with Water  which would be transferred over to the EDG1 saddle tank. The saddle tank would fill to a level high enough to impact EDG operation in less than two hours. Following this evaluation, the licensee completed engineering change (EC) 96860 to install concrete barrier pads around the ventilation piping at the 4-day tank roof level to preclude a tornado missile impact at the most vulnerable part of the piping, and also preclude water accumulation on the roof from entering the EDG 4-day tanks. The inspectors reviewed the engineering evaluation, EC, and interviewed engineering personnel to understand the scenario and the impact to plant operation.
The Brunswick Original Final Safety Analysis Report (Appendix F) and Updated Final Safety Analysis Report (UFSAR), Chapter 3, contain the language of the regulatory requirements for the general design criteria listed in 10 CFR Part 50, Appendix A, and how the licensee complies with those criteria. Criterion 2 for protection against natural phenomena states, in part, that structures, systems, and components (SSCs) important to safety shall be designed to withstand the effects of natural phenomena such as earthquakes, tornadoes, hurricanes, floods, tsunami, and seiches without loss of capability to perform their safety functions. The licensee’s statement of compliance states, “SSCs important to safety have been designed with appropriate margin for uncertainties, to permit safe plant operation or shutdown even under conditions of the most severe natural phenomena which have been conservatively postulated to occur at the site.” Criterion 4 for missile design bases states, in part, that SSCs important to safety shall be appropriately protected against dynamic effects, including the effects of missiles, which may result from events and conditions outside the nuclear power unit. The licensee’s statement of compliance states, “SSCs important to safety have been designed with full consideration of the combined effects of the normal and postulated accident environment, including the effects of pipe whipping or other dynamic effects resulting from the accidents.” Section 3.5.1.4 of the UFSAR contains the specific analysis of four potential tornado-borne missiles and the effects on the plant. The impact of one of these missiles, shearing the EDG 4-day fuel oil tank ventilation line, along with water intrusion into the system from the design basis rainfall event, would prevent the EDG (an SSC important to safety) from performing its required safety function of providing a reliable source of AC power to the engineered safety features for safe shutdown of the plant or during design basis accidents.

Analysis. The inspectors determined the failure to ensure adequate tornado missile protection
There is the first mention of a fuel tank
for the EDG 4-day fuel oil tank ventilation piping was a performance deficiency that warranted a significance determination. The inspectors determined that the finding was more than minor in accordance with IMC 0612, “Power Reactor Inspection Reports,” Appendix B, “Issue Screening,” dated September 7, 2012, because it is associated with the Mitigating Systems Cornerstone attributes of Protection Against External Factors and Equipment Performance, and adversely affected the cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, it was determined that the ventilation piping could be sheared with a design basis tornado missile at the 4-day fuel oil tank building roof level and water intrusion into the EDG fuel oil system would occur during a design basis rain event that would prevent the EDG from performing its required safety function. Using IMC 0609, Appendix A, issued June 19, 2012, The Significance Determination Process (SDP) for Findings At-Power, the inspectors determined the finding screened to a detailed risk evaluation since the EDG1 fuel oil system was assumed to be completely failed due to a tornado, and it would degrade one or more trains of a system that supports a risk significant system or function. The regional Senior Reactor Analyst performed a detailed risk evaluation by using a qualitative screening analysis to determine the significance of the finding. Tornado initiating event frequency was derived from Nation Weather Service data. Because of the low likelihood of a tornado powerful enough to throw an object of sufficient size to damage the piping, the remote chance the thrown object would strike the vent
Sounds like Fukushima reasoning...
pipe, and because the remaining EDGs would not be impacted in the same way by the tornado, the finding was determined to be Green. The inspectors did not identify a cross-cutting aspect associated with this finding because the finding is an old design issue that has been in place since original plant construction.
Enforcement: Title 10 CFR Part 50, Appendix B, Criterion III, “Design Control,” requires, in part, that measures be established to assure that applicable regulatory requirements and the design basis, as defined in Part 50.2 and as specified in the license application, for those structures, systems, and components to which this appendix applies, are correctly translated into specifications, drawings, procedures, and instructions.
Contrary to the above, since the initial construction of both units, until August 14, 2014, the licensee failed to translate the appropriate tornado missile protection requirements into the design of the EDG 4-day fuel oil tank ventilation piping. The licensee performed corrective actions to install concrete blocks around the tank ventilation piping. This violation is being treated as an NCV, consistent with Section 2.3.2.a of the Enforcement

Policy. The violation was entered into the licensee’s CAP as CR 686589. (NCV 05000324; 325/2014005-01, Failure to Protect Emergency Diesel Generator 4-Day Fuel Oil Tank Ventilation Piping from Tornado Missiles) 1R18 Plant Modifications (71111.18 – 1
Waterford
January 22, 2015 WATERFORD – NRC COMPONENT DESIGN BASES INSPECTION REPORT 05000382/2014007 AND PRELIMINARY GREATER THAN GREEN FINDING











New CDBI Inspection at Waterford, NRC says they could have melted down in Hurricane?


Updated on Apr 23: 0500382

See how in Brunswick the NRC inspectors discovered DG day tank vent pipe vulnerabilities... 

On Waterford's corroded DG day tank vent pipe, why wasn't it protected from tornadoes?  

Originally posted on 1/7/2015
This really ask us how close we are to a international incident. We are walking on a lot thinner ice as a nation than we realize.
By the way, even having safety related DG fuel oil tubing the operators have never been up to the roof?

More embarrassing than anything, Entergy's staff didn't catch this on their own. You notice the shadowy way the NRC hints the New Orleans severe weather and excessive rainfall could be outside the norms of anywhere else in the country. Stick that is risk perspective pipe and smoke it.





Hurricanes of Category 3 or greater passing within 100 miles of New Orleans 1852–2005. from NOAA

Waterford had in excess of 10 inches of rainfall in Katrina...had similar amounts in more recent hurricanes. Basically the NRC says, Waterford had corroded and leaking  fuel oil day tank(s) roof vent tubing. In a large rainfall, water on the roof would have ponded...would have covered the corrode tubes that had holes in it. You notice they don't show us pictures

The ponding water would have leaked into the diesels fuel oil tank and that would have permanently shutdown both diesel generator. The below is how the NRC frames it ( they don't say how many rainfall event). 
'Engineering review of the available meteorological tower data shows peak rain rates of 3.8 inches per hour have been experienced at the site in in the last two years." 
Per the NRC:
"It is unknown how long this corrosion has existed."  
So the huricane winds vibrates the thin wall corroded DG tubing, maybe the wind picks up debis and hit the tubing...this creates the break.

I believe all communication to the outside was lost in Katrina at Waterford. The grid was down for weeks and the plant was on the diesel generators for weeks. Here below the NRC says they would have stopped working:
"If required to operate after a Design Basis rainfall event over the past 3 years both the train A and B EDGs could have been inoperable due to water intrusion into the EDG Feed Tanks through the corroded holes." 
Here is the scenario. I wonder what size hurricane would now take take out the the transmission system surrounding Waterford. Did they upgrade the transmission?
1) The front side of the hurricane quickly takes out the transmission system.
2) The plant would immediately get re-energized by both diesel generators starting up and connecting to the buses. 
3) The eye wall would go over the plant...copious amounts of water would overwhelm the roof drains on the Reactor Auxiliary Building  roof in this first swipe. It would ensue huge ponding of water.
4) All during the front end of the hurricane, rain water would be draining into the the diesel generator local fuel oil tanks through the corroded vent line tube(s)
5) Shortly after eye wall would passes, both diesels generator would start sputtering. They would both trip and can't be started. Nobody would know why the DGs stopped. It would haunt the operators with not knowing why the DGs tripped.
6) It would be the first time a nuclear plant in the USA had to cycled into a station blackout procedure (SBO). If the accident gets under control at this point, can you imagine the hullabaloo with  the outsiders, that the roof corroded  DG fuel oil tubing got a plant into this position.
7) It would be the first time in the history of the world where the nuclear power plant staff tried to perform a SBO procedure in 110 MPH winds and copious rain.
8) Now how long does those emergency safety system batteries work?  I have no faith the portable dg would get
Can you even imagine how the cable networks and the newspapers would interpret this event? I believe maybe it would come to a fuel melt...probably not as bad a Fukushima. I don't  think you can get into a more complex event as this.

Here below is the LER on it. It doesn't seem the CDBI inspection report has come out yet.

By the way, they had three or four other dg fuel tubing leak through the years and poor maintenance leading to other leaks. You would think a nuclear plant would have high quality thick tubing who doesn't corrode in the weather? Where is the protective covering?
Emergency Diesel Generators Rendered Inoperable By Potential Water Intrusion Into Diesel Fuel Oil Feed Tanks 
LER-2014-04-00
During a walkdown of the Emergency Diesel Generator Feed Tank A and B vent lines on October 22, 2014, an NRC Component Design Basis Inspection inspector identified corrosion on the Emergency Diesel Generator Feed Tank A and B vent lines where the vent lines pass through the roof. A visual inspection was performed and revealed that the corrosion had created through wall holes that could allow water into both the train A and B Emergency Diesel Generator Feed Tanks. Follow up analysis has determined that some rainfall amount less than the postulated Probable Maximum Precipitation event could have resulted in water intrusion into the Emergency Diesel Generator A and B Feed Tanks that exceeds the 0.1 percent water content allowed by the vendor technical manual. This could have potentially affected the operability of both the A and B Train Emergency Diesel Generator Feed Tanks and subsequently both trains of the Emergency Diesel Generators. It is unknown how long this corrosion has existed. Compensatory measures were put in place to prevent water ingress should a large rainfall event occur. Follow up analysis has determined that some amount of rainfall less than the postulated Probable Maximum Precipitation (PMP) event could have resulted in sufficient water ponding on the Reactor Auxiliary Building (RAB) [NF] roof to allow water intrusion into the EDG A and B Feed Tanks that could exceed the 0.1 percent water content allowed by the vendor technical manual. This could have affected the operability of both the A and B Train Emergency Diesel Generator Feed Tanks and Emergency Diesel Generators. Engineering review of the available meteorological tower data shows peak rain rates of 3.8 inches per hour have been experienced at the site in in the last two years. Based on the follow-up evaluation, these rainfall rates could have potentially resulted ponding on the RAB roof that would allow in water ingress into the EDG Feed tanks. These rain events have been followed by successful EDG monthly tests. If required to operate after a Design Basis rainfall event over the past 3 years both the train A and B EDGs could have been inoperable due to water intrusion into the EDG Feed Tanks through the corroded holes.

This it the first swipe with Waterford's reporting to the NRC. Can't you hear Entergy's bitching over wildy excessive regulatory burderns including the CDBI. 

SUBJECT: UPDATE - NOTICE OF UNUSUAL EVENT, PLANT SHUTDOWN, AND LOSS OF OFFSITE POWER AT WATERFORD-3 DESCRIPTION: 
This Preliminary Notification is being issued to update recipients of the Notice of Unusual Event(NOUE), plant shutdown, and loss of offsite power at the Waterford-3 facility in response to Hurricane Katrina. As of August 30, 2005, at 9:00 a.m. (CDT), Waterford-3 remains in the NOUE, because of the loss ofoffsite power. The plant is no longer under a hurricane warning which was the original basis for the emergency declaration. Preliminary assessment of the Waterford-3 plant identified no significant damage to safety systems and structures. The plant is currently in Mode 4 or “hot shutdown,” with both trains of shutdown cooling operable. Onsite safety-related electrical power continues to be provided by the emergency diesel generators. The licensee is continuing efforts to evaluate the condition of the electrical distribution network in the vicinity of the plant which is energized and supplying balance of plant loads. The licensee is planning inspections of electrical transmission facilities in the next 24 hours. Two regional inspectors remain onsite and are monitoring licensee recovery activities.
All NRC CDBI inspections at Waterford. The problem I got, was why wasn't the DG fuel oil day tank roof vent line problem picked up in the first inspection in 2007. The risk based priority system on picking what component system to inspect makes no sense...it's gone haywire.



NH PUC Launches Investigation Into Soaring New England Energy Price

Investigation into Potential Approaches to Ameliorate Adverse Wholesale Electricity Market Conditions in New Hampshire 
New Hampshire Public Utilities Commission

Northeast Forum on Regional Energy Solutions 
Remarks by Gordon van Welie, President & CEO, ISO New England
April 23, 2015
Gets you to wondering, what are the implication of this?  

NEISO:  ‘Global oil prices dropped dramatically, making it more economical at times to burn oil than natural gas. This dampened gas and electricity price volatility.”
I find it implausible NH does know what is causing the price spikes...
NH PUC launches investigation into soaring New England energy price 
By ALLIE MORRIS
Monitor staff
Thursday, April 23, 2015
The state Public Utilities Commission is launching an investigation into the state’s high electricity costs, hoping to find solutions.

“Overall, the average retail price of electricity in New England is the highest in the continental United States, posing a threat to our region’s economic competitiveness,” said the PUC order, dated last Monday. “The commission has a fundamental duty to ensure that the rates and charges assessed by (electric distribution companies) are just and reasonable.” 
The cost of energy has become a hot-button topic in New Hampshire, as lawmakers, businesses and citizen groups seek solutions to bring down prices.

Utilities announced rate increases across the board last fall, and many customers saw spikes in their winter electric bills. 
Electricity costs in January averaged 19 cents per kilowatt-hour for New Hampshire residents, according to the U.S. Energy Information Administration. That compares with the national average of 12 cents per kilowatt-hour. 
Many in the energy industry have attributed the high costs to constraints in the region’s natural gas supply. The fuel has risen in popularity because of its cheap cost and abundance. Nearly half of New England’s electricity is now generated by natural gas, compared with just 15 percent in 2000. 
The staff investigation will study the gas-resource constraint problem, seeking solutions. The order adds that the “potential development of additional natural gas resources for the benefit of the electricity supply in our region should be carefully considered.”

All New Hampshire utilities will be required to participate in the investigation, including Eversource Energy, Unitil and Liberty Utilities.

The commission will hold a public meeting May 12. Regulators will issue a report by Sept. 15 outlining their findings.

The PUC is already investigating energy efficiency proposals and reviewing how utilities purchase power.

Several natural gas pipeline projects have popped up recently, including a Kinder Morgan proposal that would send about 70 miles of pipeline through southern New Hampshire.

A separate plan, known as Access Northeast, would expand an existing natural gas pipeline that passes along the Seacoast.

Meanwhile, the six New England states are eying measures to reduce energy costs.

Five of the region’s governors will meet in Connecticut today for a forum focused on Regional Energy Solutions.

Democratic Gov. Maggie Hassan is attending Sheriff Michael Downing’s memorial service today, and is unable to be at the regional meeting. 
Staff from the New Hampshire PUC and Office of Energy and Planning will be at the Connecticut forum on Hassan’s behalf, said spokesman William Hinkle.

“Governor Hassan will continue to work to protect the interests of New Hampshire and ensure that our regional partners understand that Granite Staters will have a voice on proposed projects that wish to be sited in our state,” he said.