Wednesday, September 14, 2016

Junk and Dead Ender Pilgrim: "Communication Has Become Terrible With The Fire Department"

They are probable losing employees hands over fist. Who wants their careers tainted by this terribly operating plant.
Hydrogen gas leak forces investigation at Pilgrim nuke plant
"Pilgrim Nuclear Power Station leaked 2,680 cubic feet of hydrogen gas into Plymouth skies Friday from its turbine building, once again forcing plant operators to file reports with state and federal regulators.
“One local agency that should have been contacted never got the call, according to Plymouth Fire Chief Ed Bradley.
The event was just one more in a string of mishaps the 44-year-old reactor has experienced over the past month, and the plant owner plans to closely look at what happened.
“While this is an infrequent occurrence, it does not meet our standards and a prompt investigation is underway to determine the cause and to preclude recurrence,” Entergy Corp.’s spokesman Patrick O’Brien wrote in an email to the Times.
Pilgrim operators notified the Massachusetts Department of Environmental Protection of the event late Friday afternoon, and submitted a short event report to the Nuclear Regulatory Commission on Monday, in which it stated the required notice was also given to the Plymouth Fire Department.
The plant license holder must report any hydrogen releases greater than 1,900 cubic feet during a 24-hour period.
Bradley was unhappy about the lack of notice but said it's become typical behavior. "In the past three months, communication has become terrible," the fire chief said Monday. "And I don't know why." He said he made a phone call to plant managers Monday, who confirmed the release had taken place.
DEP spokesman Edmund Coletta said his agency received the phone call shortly before 6 p.m. Friday. “They are now required to hire a licensed site professional, which they have done, to submit a closure report on what happened, how it happened and why it happened,” he said. “They have 60 days to do that.””

Junk and Dead Ender Pilgrim plant: Shutdown Again From 9% Power

The ISO must consider these guys unreliable. Imagine the rescheduling going on here... 
NUCLEAR POWER
Pilgrim almost back online after eight days
Mechanical malfunction forces another shutdown
Posted Sep. 13, 2016 at 7:52 PM
PLYMOUTH — Pilgrim Nuclear Power Station was slowly powering up Tuesday and reached 9 percent of its full capacity when yet another mechanical malfunction forced operators to shut the reactor back down, marking the eighth day the plant has been offline.
A turning gear that helps spin the turbine and maintain it in proper balance was not functioning properly, according to Neil Sheehan, spokesman for the Nuclear Regulatory Commission. Sheehan said it will have to be repaired before the reactor can be restarted.
Since the problem is on the turbine side, rather than on the nuclear reactor side of the operation, public safety is not a big concern, according to the NRC and Entergy, the plant's owner-operator.
Entergy spokesman Patrick O’Brien said the plant will return to full power when repairs are completed. “Information on when we expect to return to 100 percent power is business sensitive and proprietary, and we are therefore not at liberty to make it public.”
Operators shut down the reactor on Sept. 6 because a faulty regulator valve was allowing too much water into the reactor building. That valve, and a second one, have been repaired, Sheehan said Monday.
Last Friday, while the plant was still in shutdown, there was a leak of 2,680 cubic feet of hydrogen gas in the turbine room which then went into the atmosphere, forcing plant operators to file reports with state and federal regulators.
Pilgrim was also shut down for four days last month due to a malfunctioning steam isolation valve designed to prevent radioactivity from leaking into the environment during a nuclear accident. Problems in that same valve system had caused a shutdown in August 2015.
Pilgrim, ranked by the NRC as one of the three worst performers in the country’s fleet of 100 reactors, is slated to close on May 31, 2019.
Meanwhile Entergy spokesman Joseph Lynch told a group of Plymouth officials Tuesday that the company has notified federal regulators that Pilgrim is ready for a full inspection, the final one in a series of three special inspections required because of the plant's poor performance.
Lynch said a team of NRC inspectors will arrive Nov. 28 for a two-week scrutiny of Pilgrim. Inspectors then return in January to wrap up, Lynch said.
— Follow Christine Legere on Twitter: @ChrisLegereCCT

Monday, September 12, 2016

Dead Ender Junk Pilrim: Releasing in excess of 10 Pounds of Hydrogen

Right, in recent times, two MSIVs and a feed water regulation valve malfunctions...now this. This is a indication of financial starvation and a lack of hope for the staff.

There are fans in the roof of the turbine building. The gas most likely was dispersed through this manner. The amount of hydrogen here carries a lot of energy and there always is a fear of detonation. It could blow off the siding and injure a lot of people. How would you like the end of plant operations to be precipitated by this kind of explosion or event? There is a possibility the leak began in the stator cooling system in the basement.  

A uncontrollable cascade of plant problems...
Wiki: The butterfly effect is the concept that small causes can have large effects. Initially, it was used with weather prediction but later the term became a metaphor used in and out of science.[1]
In chaos theory, the butterfly effect is the sensitive dependence on initial conditions in which a small change in one state of a deterministic nonlinear system can result in large differences in a later state. The name, coined by Edward Lorenz for the effect which had been known long before, is derived from the metaphorical example of the details of a hurricane (exact time of formation, exact path taken) being influenced by minor perturbations such as the flapping of the wings of a distant butterfly several weeks earlier. Lorenz discovered the effect when he observed that runs of his weather model with initial condition data that was rounded in a seemingly inconsequential manner would fail to reproduce the results of runs with the unrounded initial condition data. A very small change in initial conditions had created a significantly different outcome...

This isn't a normal release of hydrogen. This was a unintentional release due to operator error or a equipment malfunction.

Chaotic and erratic plant operations!!!!

How do we get here? Right, high ocean temperatures forced the unit to cycle up and down. We had a feedwater adventure at 91% power. Now this. Erratic plant operations!!! This is how the lessor nations operate their nuclear power plants.
Plant design has a pipe going to way above the roof, where the hydrogen get dispersed in this way.
Power ReactorEvent Number: 52231
Facility: PILGRIM
Region: 1 State: MA
Unit: [1] [ ] [ ]
RX Type: [1] GE-3
NRC Notified By: JOHN WHALLEY
HQ OPS Officer: STEVE SANDIN
Notification Date: 09/09/2016
Notification Time: 20:01 [ET]
Event Date: 09/09/2016
Event Time: 17:39 [EDT]
Last Update Date: 09/09/2016
Emergency Class: NON EMERGENCY
10 CFR Section:
50.72(b)(2)(xi) - OFFSITE NOTIFICATION
Person (Organization):
MEL GRAY (R1DO)
BERN STAPLETON (NSIR)

UnitSCRAM CodeRX CRITInitial PWRInitial RX ModeCurrent PWRCurrent RX Mode
1NN0Refueling0Refueling
Event Text
OFFSITE NOTIFICATION - RELEASE OF HYDROGEN GAS IN EXCESS OF THE REPORTABLE QUANTITY OF TEN POUNDS

"At 1739 [EDT] on Friday September 9, 2016 the Massachusetts Department of Environmental Protection and the Plymouth Massachusetts Fire Department were notified of a Hydrogen release in accordance with plant procedures and 310CMR40.300, Massachusetts Contingency Plan Notification for Oil and Hazardous Material; Identification and Listing of Oil and Hazardous Material, due to a release of hydrogen gas to the environment exceeding the reportable quantity of ten pounds. The Massachusetts DEP Tracking Number is RTN4-26311. The release was from the generator hydrogen cooling system. There was no plant damage. Hydrogen system pressure has been restored to the normal operating band with the Main Generator secured and is stable. The cause of the event is under investigation.

"This event posed no danger to the health and safety of plant personnel or members of the general public.

"The NRC Resident Inspector has been notified.''





Junk Plant Salem 1 & 2: Indication Of Rough Seas For The Nuclear Industry

I see this as a indicator of heighten risk of a nuclear plant meltdown. Or an accident that's going to be on the doorstep of a meltdown, could turn into meltdown. At best, the Salem and Hope facility will tar the industry's reputation

As a professional, the reliability of the operation of the Salem and Hope facility is a disgrace to the nation. An indication of the problem with Hope Creek is their Safety Relief Valves. They can't quickly clear weak designed SRVs from the plant. For the last few years, this facility is in deep decline and this indicates the system can't quickly clear emergent problem across the board. This facility's operations has been chaotic and erratic. I think this is a indicator for the industry in general. The whole industry is moving towards the condition of Hope Creak and the Salem units.

I remind everyone we don't have the god's eye view of the safety of the massively complex organization and the massively complex machine, components and parts and material conditions. Outsider only see a sliver of the extent of these problems. One plant may have up to a million or more components...this is the second largest nuclear facility in the USA with three plant. The complexity here is mind boggling. This is why I spend so much of my time studying the documents of this facility. I am just a tea leaf reader.

Salem 1 63%
Salem 2 100%

  

Friday, September 09, 2016

Junk Salem 1&2: Both Plants Stuck At 60% Again


Honestly, on this second largest nuclear facility in the USA, when have all three plants been at 100% this summer? Bet you for this facility, its the worst summer capacity history on the record.

Thursday, September 08, 2016

Junk Plant Pilgrim: Forged Signature On Safety Document Not A NRC Violation


Where the hell are we heading!!!
Mr. John Dent, Jr.
Site Vice President
Entergy Nuclear Operations, Inc.
Pilgrim Nuclear Power Station
600 Rocky Hill Road
Plymouth, MA 02360-5508
SUBJECT: NRC INVESTIGATION REPORT NO. 1-2015-008
Dear Mr. Dent:
This letter refers to the subject investigation by the U.S. Nuclear Regulatory Commission (NRC) Office of Investigations (OI) involving the Pilgrim Nuclear Power Station (Pilgrim), owned by Entergy Nuclear Operations, Inc. (Entergy). The investigation,
Was the former planning manager fired for cause?
which was completed on December 18, 2015, was conducted, in part, to determine whether a (former) planning manager at Pilgrim caused Entergy to violate NRC requirements related to work planning or risk assessment. As described below, the NRC determined that the circumstances of the case did not result in a violation of NRC requirements.
The non-outage work planning process at Pilgrim is conducted in accordance with Entergy procedure EN-WM-101, “On-Line Work Management Process.” The scope of work for a given workweek is finalized 16 weeks before the start of the actual workweek. After that point, any proposed scope changes must be documented on a form (Attachment 9.1 to the procedure). The form records the desired work scope change and its impact (manpower and operational), and requires signatures from designated Operations and Work Control contacts.
In October 2014, Pilgrim staff identified that six forms authorizing work scope changes included signatures for the Operations and Work Control personnel that had apparently been forged by the planning manager. Pilgrim staff initiated an internal investigation and notified the NRC of the concern. The NRC conducted an independent investigation of the matter to determine whether the planning manager’s actions resulted in any violations of NRC requirements. In particular, the NRC evaluated whether the planning manager caused work to be performed without being properly evaluated for risk, as required by Title 10 of the Code of Federal Regulations, Section 50.65(a)(4).
Based on the evidence gathered during the OI investigation, the NRC concluded that, although the planning manager forged the names of Operations and Work Control personnel on the forms, this action did not result in a violation of NRC requirements. Specifically, the NRC determined that the work scope changes did not involve or potentially affect the performance of safety-related equipment; and that the planning manager’s actions did not cause the licensee to improperly perform unplanned work, remove required work from the schedule, or fail to perform a required risk evaluation.

Unlimited Qualities of Natural Gas In The USA?

Oil! Massive shale discovery in Texas

Published  1:18 PM EDT Sep 08, 2016
An overlooked corner of West Texas is believed to contain billions of barrels of newly-discovered shale oil.
Apache (APA) revealed the huge find this week after more than two years of stealthily buying up land, extensive geological research and rigorous testing.  
The Houston company estimates the discovery, dubbed "Alpine High," could be worth at least $8 billion.

Apache believes the new shale play spans at least five formations, contains over three billion barrels of oil and 75 trillion cubic feet of rich natural gas.  
"We feel very confident with what we have and believe this is a story that's only going to get better," Apache CEO John Christmann IV told CNNMoney.  
Wall Street is already seeing dollar signs, sending Apache's stock price surging 10% in the two trading days since the find was unveiled.  
"The play has the potential to be a transformative event for the company," Raymond James analyst John Freeman wrote in a research report. "Apache sees an incredible opportunity to establish the next big resource play in the U.S."  
Apache Energy's huge shale oil discovery in West Texas, named "Alpine High," is estimated to contain three billion barrels of crude. 

Related: OPEC's dire finances fuel oil freeze talks 
Apache has identified at least 2,000 drilling locations, and estimates an initial value of between $4 million to $20 million per well. That translates to at least $8 billion in value for the company, but potentially a lot more. The company has already drilled 19 wells in the play, with nine currently producing "limited quantities" due to infrastructure constraints. 

Rob Thummel, a portfolio manager at energy investment firm Tortoise Capital, said the announcement will "definitely open investors' eyes" and could lead his firm to make an investment in Apache. 

However, Thummel also urged caution, noting that Apache's management team doesn't have the long track record of more established shale companies like EOG Resources (EOG) or Pioneer Energy. (PES) 

"It's going to be more of a prove-it story," Thummel said.
Christmann, the Apache boss, said his company looks forward to "proving the significance of this discovery over time." He added that the find is the result of "intense technical work," including 3D seismic research.  
Related: Oklahoma orders shutdown of wells after earthquake
So what's next? Apache will need to continue testing the land to decide where it makes the most sense to start drilling at current prices. Both oil and natural gas prices remain depressed due to a huge glut, mostly fueled by excessive shale production from the U.S. over the past decade.  
Apache will also need to build infrastructure to handle all the potential oil and gas coming out of Alpine High. The company is expected to install a temporary processing facility later this year and eventually build a more permanent presence. 

"Rome wasn't built in a day, neither are major oil and gas fields," Thummel said.

Heroin: I Think It Is The Foreign Drug Kingpins Blackmailing Us

Back off USA, or 10,000 people will drop dead in the streets in one week...

Coroner: Heroin dealers using Cincinnati as a 'test tube'
Published: 09/07/16 04:09 pm EDT.
CINCINNATI, Ohio
Authorities suspect the Cincinnati area has been treated as a "test tube" by heroin dealers for use of a powerful animal tranquilizer, a county coroner said on Tuesday.
Tests have confirmed carfentanil in the bodies of eight recent overdose casualties, Hamilton County's Dr. Lakshmi Sammarco said, and more cases are suspected. The drug, used to sedate elephants, can be thousands of times stronger than morphine.
Sammarco said the sudden surge in overdose cases raised concerns that dealers wanted to see what would happen in a community when they mixed carfentanil with heroin or sold it outright.
"The very intense and focused spike brought up a lot of fears .... that our community was being used as a test tube," she said. "What are they learning from it? Are they looking to see how many people it's going to kill or how quickly our first responders can respond? And how many customers is that going to generate for them?"
Authorities have said nearly 300 overdoses have been reported in the Cincinnati area since Aug. 19, with 174 reported in a six-day period. Communities in West Virginia, Kentucky and Indiana also saw overdose spikes in recent weeks.
Carfentanil has been blamed in other overdose surges, such as in Akron this summer. Cincinnati area authorities warned publicly in July that carfentanil was beginning to show up locally.
Sammarco said the office of Republican U.S. Sen. Rob Portman reached out to the Cleveland Zoo and the Summit County coroner's office to help her obtain carfentanil samples for testing. She said more overdose cases since July are being reviewed for carfentanil.
U.S. Drug Enforcement Administration officials have said they believe much of the carfentanil is being shipped from China to Mexico, where traffickers are mixing it with heroin and other drugs such as the painkiller fentanyl.
Cincinnati firefighters said they sometimes had to use multiple doses of the overdose-reversal drug naloxone to save users during the spike.
Newtown police Chief Tom Synan, who heads the Hamilton County Drug Coalition task force, said Tuesday he wants Ohio to declare an emergency and free up more resources to help local authorities cope.
"We're bleeding profusely, and we need a tourniquet," Synan said.
A spokeswoman for Republican Gov. John Kasich, Emmalee Kalmbach, said the state is continuing to work with Cincinnati area officials to strengthen prevention, treatment and other resources.
"Making progress in our fight against drug abuse requires a determined, community-based commitment and a shared purpose that brings all of us together to find and implement the right solutions," Kalmbach said.
The state last week expedited a shipment of naloxone to Cincinnati to rebuild supplies as the spike slowed.
©2016 by The Associated Press. All rights reserved. This material may not be published, broadcast, rewritten or redistributed.

Junk Plant Grand Gulf-Continued Terrible Capacity Factor

They are losing money hands over fist. Bet you it is run to failure...

Power ReactorEvent Number: 52225
Facility: GRAND GULF
Region: 4 State: MS
Unit: [1] [ ] [ ]
RX Type: [1] GE-6
NRC Notified By: SEAN DUNFEE
HQ OPS Officer: JEFF ROTTON
Notification Date: 09/08/2016
Notification Time: 04:27 [ET]
Event Date: 09/08/2016
Event Time: 03:00 [CDT]
Last Update Date: 09/08/2016
Emergency Class: NON EMERGENCY
10 CFR Section:
50.72(b)(2)(i) - PLANT S/D REQD BY TS
Person (Organization):
THOMAS HIPSCHMAN (R4DO)

UnitSCRAM CodeRX CRITInitial PWRInitial RX ModeCurrent PWRCurrent RX Mode
1NY100Power Operation82Power Operation
Event Text
TECHNICAL SPECIFICATION SHUTDOWN DUE TO LOSS OF RESIDUAL HEAT REMOVAL PUMP

"On September 4, 2016 at 0258 [CDT], Grand Gulf Nuclear Station entered three [Technical Specification] Limiting Conditions for Operations (LCOs) due to residual heat removal pump 'A' (RHR 'A') being declared inoperable.

"LCOs entered:
1) 3.5.1 for one low pressure ECCS injection/spray subsystem,
2) 3.6.1.7 for one RHR containment spray subsystem, and
3) 3.6.2.3 for one RHR suppression pool cooling subsystem.

"Station management has made the decision to shutdown the plant to repair the RHR 'A' pump prior to the end of the 7 day LCO completion time based on troubleshooting and testing performed on the RHR 'A' pump.

"Grand Gulf Nuclear Station initiated plant shutdown required by Tech Spec Actions 3.5.1, 3.6.1.7, and 3.6.2.3, at 0300 CDT on 09/08/2016 due to expected inability to restore RHR 'A' to operable status prior to exceeding the LCO time of 7 days."

The unit is currently at 82 percent power. There are no other systems out of service that would complicate the orderly shutdown to Mode 4.

The licensee will notify the NRC Resident Inspector.

Junk Plant Polo Verde Has A Special Way To Discover Maintenence Problems.

Basically setting up for maintenance issue then uncovering two additional maintenance problems not detected by the plant.

1) Seems something is wrong the breakers during the bus transfer. There are a lot of breaker problems in the industry. Was the busses in synch upon the transfer? Big chance of a electrical explosion.

2) The stuck open relief valve. The is what caused TMI. 

Power ReactorEvent Number: 52226
Facility: PALO VERDE
Region: 4 State: AZ
Unit: [1] [ ] [ ]
RX Type: [1] CE,[2] CE,[3] CE
NRC Notified By: MIKE JONES
HQ OPS Officer: DANIEL MILLS
Notification Date: 09/08/2016
Notification Time: 04:27 [ET]
Event Date: 09/07/2016
Event Time: 21:31 [MST]
Last Update Date: 09/08/2016
Emergency Class: NON EMERGENCY
10 CFR Section:
50.72(b)(2)(iv)(B) - RPS ACTUATION - CRITICAL
Person (Organization):
THOMAS HIPSCHMAN (R4DO)

UnitSCRAM CodeRX CRITInitial PWRInitial RX ModeCurrent PWRCurrent RX Mode
1M/RY100Power Operation0Hot Standby
Event Text
MANUAL REACTOR TRIP DUE TO STUCK OPEN PRESSURIZER MAIN SPRAY VALVE

"On September 7th, 2016 at approximately 2131 Mountain Standard Time (MST), Palo Verde Unit 1 was manually tripped due to a stuck open main spray valve. Unit 1 was operating at 100 percent power at normal operating temperature and pressure prior to the event. A 120 VAC non-class instrument distribution panel was being transferred to its alternate power supply to establish maintenance conditions. The distribution panel failed to transfer. The panel remained energized from its normal power supply; however, multiple components powered from the distribution panel began to exhibit uncharacteristic behavior. At this time, it was noted that a reactor coolant system main spray valve was open. The alarm response procedure was followed; however, the actions taken were unsuccessful at closing the main spray valve. The plant was then manually tripped due to pressurizer pressure continuing to lower. The reactor coolant pumps were turned off to terminate main pressurizer spray flow to control pressurizer pressure due to the inability to close the main spray valve. No ESF [Engineered Safety Features] actuations occurred and none were required. No emergency classification was required per the emergency plan. Safety related buses remained energized during and following the reactor trip. The emergency diesel generators did not start and were not required. The offsite power grid is stable. Limiting condition for operation 3.4.1 was entered due to low pressurizer pressure. No major equipment was inoperable prior to the event that contributed to the event.

"Unit 1 is stable at normal operating temperature and pressure in Mode 3. Reactor coolant pumps are secured and natural circulation has been verified. Primary pressure is being maintained at its normal operating pressure manually with pressurizer heaters and auxiliary spray, from the charging system. The event did not result in any challenges to fission product barriers and there were no adverse safety consequences as a result of this event. The minimum RCS pressure was approximately 2070 psia (normal 2250). The event did not adversely affect the safe operation of the plant or the health and safety of the public."

All rods inserted and the trip was uncomplicated. Units 2 and 3 were not affected and continue to run at full power.

The NRC Resident Inspector has been notified.

Junk Plants Salem 1&2 Stuck At 60% For two Days.

Man, its a long and troublesome summer for these guys?

Hope keeps chugging along...

Wednesday, September 07, 2016

Junk and Dead Ender Oyster Creek Plant-91% Power For A Week

You got to be careful this time of year with plants not at 100% power. The plants might to heading to a refueling outage and power is slowing going down as they run out of fuel.

Tuesday, September 06, 2016

Junk Plant Pilgrim Second Scram On Ocean High Temperature Cycling

Update

Neal told me, in fact, there are two separate 23 kilovolts lines going into Pilgrim. One going to waste treatment plant and the other attached to the emergency shutdown transformer. Within a few weeks both shorted and created a small brush fire in the owner controlled area. Neal didn't seem to think there is a connection to each grounded event. I Told him if I worked a Pilgrim or the NRC, I'd be digging as hard as I could looking for a connection or link to both events. He said he would pass that onto the resident.
Pilgrim Nuclear Power Plant Shuts Down Following Valve Problem

September 6, 2016

PLYMOUTH – The Pilgrim Nuclear Power Station in Plymouth experienced an unplanned shutdown this morning, according to the Nuclear Regulatory Commission.

A statement from the agency said it was caused by a high water level resulting from a problem with a regulating valve.

Water is pumped into the reactor so that it can be boiled, converted to steam and then piped to the turbine to generate electricity.

The NRC said their onsite inspectors responded to observe operator responses and verify the safe shutdown of the plant just after 8:30 a.m.
 
Feed water regulation valve malfunctions are the types of problems you expect to see with jumping up and down in power.
Spokesman Neil Sheehan said plant owner Entergy will need to identify the cause of the valve fluctuations and make any needed repairs before the reactor can return to service.  
It’s just the latest equipment issue with the troubled plant that is listed as one of the worst in the nation by the NRC.

On Monday, the plant’s power was reduced to 90 percent because of elevated water intake temperatures.
 
I believe they use the 23 kilovolt line as a backup electricity source if the lose all electricity at the site. It is a value safety system. 
There was also a downed tree on the 23-kilovolt power line to the plant’s waste-treatment facility on Sunday evening which caused a small fire near Rocky Hill Road.

The NRC said the line outage did not impact any safety-related equipment at the plant.

Entergy announced last year that they would close Pilgrim by 2019





Junk Plant And Grossly Obsolete Dresden HPIC Questions

Update

Talked to the senior: They basically had resistors needing adjustment for the particular duty...they shot themselves in the foot by not doing the pre use adjustment. They are other troubles with component. GE procures the motor from another vendor...


Dresden Nuclear Power Station, Unit 3 Renewed Facility Operating License Nos. DPR-25 NRG Docket No. 50-249

Subject: Licensee Event Report 249/2016-001-00, Alert Declared from Unit 3 HPCI Auxiliary Oil Pump Motor Fire

See, poor maintenance leads to a failure, then the new motor fails almost emediately. This is a repeated pattern throughout the industry…

Think about all the intermediaries the motor components are made from.

Why wasn’t there a LER written out for the 2015 event?  

2016-001-00 -The Root Cause of the HPCI AOP motor failure is inadequate control of critical parameters when installing a DC shunt wound motor. The Failure Mechanism was high armature current with a stalled rotor. The Contributing Cause of the HPCI AOP motor failure is historical motor procurement evaluation standards were not rigorous enough. 
Previous Occurrences:
In 2015, the U3 HPCI AOP motor failed during planned maintenance due to carbon dust buildup inside the motor as a result of inadequate cleaning and inspection of the motor and commutator.

Junk Plant Salem/ Hope Creek: These Guys Are A Distrace

So something besides the charging pump leak caused the downpower. At least unit 2 is on the way up?

Friday (late Thursday)
unit 1 60%
unit 2 0%

Monday
unit 1 60%
unit 2 2%

Power ReactorEvent Number: 52222
Facility: SALEM
Region: 1 State: NJ
Unit: [1] [ ] [ ]
RX Type: [1] W-4-LP,[2] W-4-LP
NRC Notified By: MIKE BRUMMITT
HQ OPS Officer: STEVEN VITTO
Notification Date: 09/03/2016
Notification Time: 12:47 [ET]
Event Date: 09/03/2016
Event Time: 09:02 [EDT]
Last Update Date: 09/03/2016
Emergency Class: NON EMERGENCY
10 CFR Section:
50.72(b)(3)(ii)(B) - UNANALYZED CONDITION
Person (Organization):
RAY POWELL (R1DO)

UnitSCRAM CodeRX CRITInitial PWRInitial RX ModeCurrent PWRCurrent RX Mode
1NY60Power Operation60Power Operation
Event Text
UNIDENTIFIED LEAKAGE GREATER THAN TECHNICAL SPECIFICATIONS

"At 0902 EDT, on September 3, 2016, a leak developed from 13 Charging Pump seals that resulted in an unidentified leak rate of 1.3 gpm. Salem Unit 1 entered Technical Specification 3.4.6.2.b for unidentified leakage greater than 1 gpm. The Technical Specification requires the leak rate to be restored to below 1 gpm in a 4 hour period or place the Unit in Hot Standby in the next 6 hours and Cold Shutdown within the following 30 hours. In addition there is an allowable total ECCS leakage outside of Containment value of 0.45 gpm associated with Control Room habitability to comply with GDC-19 [General Design Criteria] limits. 12 Charging Pump was placed in service and 13 Charging Pump was removed from service and isolated. The unidentified leak rate lowered to below the 0.45gpm requirement for the total ECCS leakage outside of containment and the Technical Specification value of 1 gpm.

"This event is being reported under the requirements of 10CFR50.72(b)(3)(ii)(B) as 'the nuclear power plant being in an unanalyzed condition that significantly degrades plant safety' for exceeding the 0.45gpm total ECCS leakage allowable in accordance with GDC-19 limitations.

"The Licensee has notified the NRC Resident and the Lower Alloways Creek Township."

Monday, September 05, 2016

FBI Crime Data and Hinsdale, NH

The Hinsdale ex police chief hit me up with the Hinsdale, NH crime stats or data. "It seen no rise in crime" is what he said. Any professional level police executive would tell you the FBI's crime data isn't auditable. Its a totally voluntary system, there is political fallout if you report the bad news of crime. Plus the police don't have the money to report all crime to the FBI.   

The Boston Globe is writing this up in a controversial prose in order the boost circulation.  A ethical paper would have disclosed the shortcoming of the FBI's crime data and pounder if the data was trustable.

Stats on drugs, race refute Maine governor

PORTLAND, Maine — No law enforcement statistics even come close to backing up Republican Gov. Paul LePage’s assertion that blacks and Hispanics account for ‘‘90-plus percent’’ of heroin-trafficking arrests in Maine.

LePage, who previously told the Portland NAACP chapter to ‘‘kiss my butt’’ and blamed out-of-state drug dealers for impregnating ‘‘young white’’ girls, sparked another racial uproar when he said Aug. 24 that data he’d collected indicates out-of-state black and Hispanics accounted for ‘‘90-plus percent’’ of heroin-trafficking arrests in Maine.

FBI data contradict his assertion, and a criminologist called the governor’s data ‘‘laughable.’’ Meanwhile, members of the African-American community in Maine, the whitest state, fear his comments strengthen racial stereotypes and tacitly approve of racial profiling.

‘‘I think this fear-mongering, and these us-against-them kind of statements, do not advance the community conversation, do not address the real issue of drug abuse,’’ said the Rev. Kenneth I. Lewis Jr., pastor at the Green Memorial A.M.E. Church, Maine’s oldest African-American congregation, in Portland.

The Maine Department of Public Safety doesn’t include race when compiling and analyzing crime data. And the most recent crime data from the FBI suggest the governor’s claim doesn’t pass muster.

The FBI data show that blacks accounted for 14 percent of a total of 1,211 drug sale and manufacturing arrests and 7.4 percent of 5,791 total drug arrests in Maine in 2014, the most recent numbers available.

Broken down by type of offense, the data showed that blacks accounted for 35.5 percent of arrests for selling opium-derived drugs including heroin, morphine and cocaine, and 26 percent when synthetic narcotics including most prescription narcotics were included in the tally. The FBI doesn’t include a category for Hispanics in its statistics...


 

Hinsdale Heroin and the Phony Treatment Scam

 The heroin treatment sucks around here...
Michael Mulligan <steamshovel2002@yahoo.com>


Aug 17 at 1:19 PM

Everything by the politicians is treatment, treatment, treatment in the media today. It been like that for years. The heroin addiction problem is very expensive for the town's police, the courts and jails. It is debilitating to town and city budget across the state. There is now an enormous wait to get into treatment. The more the politicians are talking their solution to the heroin problem is treatment, the longer the waiting time  is to get into treatment. NH is one of the worst states in the nation with taking care of the mentally ill. It is basically warehousing addicts as a way to save money.

I think this is basically a ploy by all the politicians to talk up “I am fixing the heroin problem by treatment treatment up the ying yang to gain votes. But behind the scene, the ideological politicians don’t want to jack up funding for high quality treatment to get ahead of the ball because they hate everything government. It’s all political penny ante talky, talky bs, with no intention to raise the budgets to deal with the problem. There are now a lot of fly-by-night heroin and addiction treatment center operators who are just out to make big bucks in a crisis.  They have no real skills and education to deal with this intractable problem.
What a joke for addicts, 28 day treatment... 
Mayor-appointed drug solutions committee releases final report before dissolving
Posted: Saturday, September 3, 2016 8:00 am
By Xander Landen Sentinel Staff SentinelSource.com
Keene does not have enough treatment facilities and licensed alcohol and drug counselors to meet demand from addicts seeking help, according to a new report by Keene’s ad-hoc Committee on Drug Addiction Solutions.
In a separate action earlier that afternoon, Fire Chief Mark F. Howard offered another sobering glimpse of the crisis. In August, two more people in the city died of opioid overdoses, according to the latest data Howard releases each month.
Presenting the report at Thursday's meeting was the committee’s last task after spending a year investigating the impact of the opioid epidemic in Keene and identifying gaps in local resources for preventing and treating addiction.
Mayor Kendall W. Lane appointed the committee — comprised of local law enforcement officers, doctors, substance abuse counselors and public officials — after the City Council voted for him to do so in the spring of 2014.
Keene Police Chief Brian Costa, a committee member, said the committee's dissolution doesn't mean members think their work is done.
Costa said ad-hoc committees last only one year, but both the members and the community at large won't be any less dedicated to fighting the crisis.
“There’s an absolute need — not interest — in continuing this work. ... I think I guaranteed (the City Council) that this work would continue whether or not this committee was in existence,” Costa told The Sentinel.
Committee members stressed during their presentation that Keene offers limited treatment options for people struggling with substance abuse disorders.
According to the committee’s report, medical detoxification, medication-assisted treatment, 28-day
28 day treatment is basically criminal behavior  by the system for Heroin addiction. We are talking upwards of a year and a half to two years of intensive . And Axander doesn't even ask of the proper question of how long should the treatment be.
residential treatment programs and residential treatment programs longer than four weeks are all services that are “very limited or not available” in Keene.
The report didn't specify which types of treatment are completely unavailable in the city or to what extent other treatment options are limited.
Committee member Dr. Jose Montero, vice president of population health and health system integration at Cheshire Medical Center/Dartmouth-Hitchcock Keene, said more needs to be done to expand services for drug addicts. 
“We know that we do not have enough places where people with these chronic conditions, these drug disorders, can go to be diagnosed, to be treated,” said Montero, who was formerly public health director for the N.H. Department of Health and Human Services. 
And data on overdose deaths in Keene support the argument.  
Between 2000 and 2011, there were 21 fatal drug overdoses in Keene, according to Costa.
The latest statistics from Howard show that five people have died so far this year from opioid overdoses. Two were in the past three weeks, Costa said.
Last month also saw a slight uptick in the number of recorded overdoses for which Keene firefighters used the opioid antagonist drug Narcan. 
In August, the Keene Fire Department administered Narcan to 10 people in likely opioid overdoses. This tally is higher than the average so far for 2016 of about seven patients per month.  
Part of what limits access to treatment in Keene is a small workforce trained and licensed to treat drug addicts, according to Montero.
There are only 15 licensed alcohol and drug counselors practicing throughout the city, according to the report.
Worsening the strain is Medicaid expansion and expanded reimbursement under commercial health insurance, which have encouraged an increase in demand for addiction and recovery services, the report says.
Treatment options in Keene “have not grown at nearly the same pace” as that demand, according to the report.
Another challenge to expanding treatment options and services in the city is there are no hard statistics for how many people in Keene need treatment, Montero said. 
“We don’t know how many patients are waiting in a long-term framework so we can ... plan for what type of expansions those services need,” he said.
The committee has heard anecdotal information about people waiting between two and eight weeks to get a bed in local treatment facilities, but members don’t know the total number of people waiting to get into services like residential treatment, Montero said.
Keene should create a centralized service where drug addicts can go to be treated for the variety of issues they face, according to Montero; aside from their addictions, he noted, addicts often face a variety of physical and mental health problems.
“We need to figure out a better system to provide care for all of those different situations, hopefully in one place,” he said.
While the report pointed out gaps in Keene's resources to tackle the opioid crisis, it also acknowledged effective efforts the city and community organizations have made in recent years. 
It mentioned how Narcan is more accessible to law enforcement agencies and community health centers than ever before, how there is a push for more recovery-coach training and how a Heroin Anonymous group launched in June. 
Costa also lauded work Keene is already doing to help streamline treatment for those who want get into recovery.
He spoke about the Cheshire County Addiction Assistance and Recovery Initiative (ChAARI) which launched in May as part of Southwestern Community Services’ Coordinated Access Point Program (CAPP). The program is an 18-month pilot, focused on providing support to addicts who want to start their recovery.
ChAARI established a 24/7 hotline number that first responders can call to get a trained recovery coach dispatched to the emergency room at Cheshire Medical Center/Dartmouth-Hitchcock Keene to help people begin addiction treatment.
ChAARI has received substantial financial support from the community, which shows how dedicated Keene is to fighting the opioid crisis, according to Costa. 
"The end result for the police department, like everybody else, is to get people off this stuff," he said, "so that crimes come down and families come back home."

Xander Landen can be reached at 352-1234 ext. 1420 or at xlanden@keenesentinel.com. Follow him on Twitter @XLandenKS

Friday, September 02, 2016

US Nuclear Plants Catastrophic 51% Increase Of Outages From Last Year?

   

September 1, 2016  
U.S. nuclear power plant outages have been higher this summer (June through August), averaging 4.3 gigawatts (GW), or 51% more than in 2015. Summer outages were at their highest in June, reaching 9.9 GW, or about 10% of total U.S. nuclear capacity, on June 17 and averaging 6.2 GW for the month. Outages dropped to an average of 4.4 GW in July and 2.4 GW in August.
Nuclear power plants, which provide baseload generation, account for nearly 20% of total U.S. electricity generation on an annual basis. Nuclear power plants provide power at a steady rate rather than in response to daily or hourly fluctuations in electricity demand. Nuclear outages typically arise from refueling and maintenance, power uprates, and unplanned shutdowns. EIA's Status of Nuclear Outages maps the generating capacity and outage status of each nuclear plant in the United States each day. Nuclear outages reached the lowest level since 2007 last year, when outages totaled just 0.1 GW during four days in August 2015.
Nuclear power plants typically refuel every 18 to 24 months during fall or spring. Other noncritical maintenance work is often scheduled at the same time as refueling to minimize downtime. In the early 1990s, refueling-related outages lasted about 12 weeks. More recently, refueling outage durations have been reduced to fewer than six weeks



Junk Plants Salem 1 & 2 and Hope Creek: The Second Largest Nuke Facility In USA Train Wreck

Unit 1 seems to be heading to a shutdown at 10% power last night and Unit 2 is shutdown...
By Bill Gallo Jr. | For NJ.com Today's Sunbeam
Email the author | Follow on Twitter
on September 01, 2016 at 2:54 PM, updated September 01, 2016 at 3:53 PM

LOWER ALLOWAYS CREEK TWP. — Pump problems have caused the shutdown of one of PSEG Nuclear's reactors and a cut in electrical production at another, an official says.

Both of the reactors are located at PSEG Nuclear's generating complex on Artificial Island in Lower Alloways Creek Township.

Salem 2 automatically shut down Wednesday at 3:13 p.m. after one of the reactor coolant pumps tripped offline according to Joe Delmar, spokesman for PSEG Nuclear.

The reactor has four of the pumps which circulate water to cool the nuclear reactor. All four must be in service for the reactor to run.

Officials from the federal Nuclear Regulatory Commission, which oversees the operations of the nation's nuclear reactors, are monitoring the situation according to NRC Spokesman Neil Sheehan.

He said it appears that the pump shutdown may have been caused by water leaking onto the pump's electrical system from a cooling unit inside the reactor containment building.

The Early Site Permit issued to PSEG Nuclear is good for 20 years, but numerous other approvals would first be needed for a new reactor to be built.

The Salem 2 reactor is already under heightened NRC scrutiny because of a number of unplanned shutdowns in the past year.

Meanwhile, the neighboring Salem 1 reactor was operating at around 47 percent power Thursday because of an issue with one of the feed pumps on the unit's steam generator.

The unit has two feed pumps which pump water from the condenser back to the steam generator. The plant can continue to operate with just one of those pumps in service.

Delmar said technicians were working to determine the cause of the problem and fix it.

He said there was no estimate when Salem 1 could be ramped back up to full power.

A third reactor operated by PSEG Nuclear at Artificial Island, Hope Creek, remains at full power Thursday, Delmar said

Junks Plants Watts Junk Capacity Factors?

 
This is so embarrassing for the industry. Unit 1 has borrowed Sequoyah LP turbine to stay up at reduced power…Now both Watts Bar plants have been knocked off line because of the poor quality of the Unit 2’s new transformer. 
TVA idles both Watts Bar reactors
Transformer fire forces plant shutdown for assessment
September 1st, 2016
Less than two days after a transformer fire forced TVA's newest reactor to shut down, the other reactor at the Watts Bar Nuclear Plant was also shut down today to help plant workers perform needed tests and equipment repairs in the switchyard following the Tuesday night blaze.
TVA spokesman Jim Hopson said the Unit 1 reactor at Watts Bar was idled to allow plant workers to safely assess the main bank transformers and other equipment without the switchyard being energized with electricity.
"The safest way to do the assessment we need to do is to de-energize the switchyard and the only way to that is to take the unit off line," Hopson said. "We wanted to ensure the safety of our employees while they do this necessary work."
Hopson said TVA hopes to complete the evaluation and to be able to restart the Unit 1 reactor "within a few days." But in the meantime, TVA is getting no power from either reactors at Watts Bar even as summertime temperatures keep power demand relatively high in the Tennessee Valley.
It is unclear when TVA may be able to restart its Unit 2 reactor.
During high-demand periods, TVA generates nearly $1 million a day worth of power from each of its nuclear units.
TVA was in the midst of a series of power ascension tests on its new Unit 2 reactor on Tuesday when a fire erupted in a main bank transformer on the non-nuclear side of Watts Bar. The fire triggered a trip of the Unit 2 reactor, which was operating at about 99 percent of its rated 1,150-megawatt capacity at the time.
TVA and Nuclear Regulatory Commission crews are still evaluating the cause of the fire and any corrective actions TVA needs to take to ensure the safety of the plant when it resumes power generation. The fire-damaged transformer will be replaced with one of the spare units on site at Watts Bar, Hopson said.
TVA began limited power generation from the Unit 2 reactor at Watts Bar in May. The unit is the first new reactor added to America's power grid in 20 years. But the newest unit has not yet achieved full power and has yet to officially be declared a commercial reactor and brought into TVA's rate base.
That achievement, which TVA said earlier this year should occur by June, now appears unlikely until next month at the earliest. That will push the start of the capital recovery for the $5 billion reactor into fiscal 2017.

Thursday, September 01, 2016

Junk Plant Salem, Hope Creek: Here We Go Again With Aother Trip




Power ReactorEvent Number: 52213
Facility: SALEM
Region: 1 State: NJ
Unit: [ ] [2] [ ]
RX Type: [1] W-4-LP,[2] W-4-LP
NRC Notified By: JOHN OSBORNE
HQ OPS Officer: MARK ABRAMOVITZ
Notification Date: 08/31/2016
Notification Time: 18:12 [ET]
Event Date: 08/31/2016
Event Time: 15:11 [EDT]
Last Update Date: 08/31/2016
Emergency Class: NON EMERGENCY
10 CFR Section:
50.72(b)(2)(iv)(B) - RPS ACTUATION - CRITICAL
50.72(b)(3)(iv)(A) - VALID SPECIF SYS ACTUATION
Person (Organization):
RAY POWELL (R1DO)

UnitSCRAM CodeRX CRITInitial PWRInitial RX ModeCurrent PWRCurrent RX Mode
2A/RY100Power Operation0Hot Standby
Event Text
AUTOMATIC REACTOR TRIP ON LOW REACTOR COOLANT FLOW

"This 4-hour and 8-hour notification is being made to report that Salem Unit 2 had an unplanned automatic reactor trip and automatic actuation of the auxiliary feedwater system. The trip occurred due to the loss of the 21 reactor coolant pump [RCP] resulting in a reactor trip on low reactor coolant flow. The 21 RCP remains unavailable. The cause of the loss of the 21 reactor coolant pump is unknown at this time.

"All control rods inserted on the reactor trip. All emergency core cooling systems and engineered safety feature systems functioned as expected. The auxiliary feed pumps started as expected.

"Salem Unit 2 is currently in Mode 3. Reactor coolant system pressure is at 2235 psig and temperature is 547 degrees Fahrenheit with decay heat removal via the main steam dumps and auxiliary feedwater systems. Unit 2 has no active technical specification action statements in effect requiring a lower mode of operation due to the transient.

"The 21 and 22 containment fan coil units (CFCU) were out of service for surveillance testing prior to the event. There was no major secondary equipment tagged for maintenance prior to the event. There were no personnel injuries as a result of this event.

"Normal offsite power is available to the site. There is no effect on Unit 1."

The licensee notified the NRC Resident Inspector.