Wednesday, May 31, 2017

Junk Plant TMI Shutting Down Perminantly


What if this was a two plant facility? Did the meltdown really cause this shutdown? If it was a two plant facility, would it be more profitable? Would it have survived another few years? 

Exelon Announces Three Mile Island Nuclear Plant to Close in 2019

Exelon Corp. said it plans to retire the Three Mile Island (TMI) nuclear power plant around September 30, 2019, unless policy reforms are enacted in Pennsylvania.
The company used a similar ploy in Illinois to pressure lawmakers into passing the state’s Future Energy Jobs bill, which provides subsidies for nuclear power plants. In that case, Exelon announced the closure of the Clinton and Quad Cities stations, only to reverse the decision once the legislation received the necessary support.
TMI has been in jeopardy for some time. Last year, TMI failed to clear PJM’s 2019–2020 capacity auction. At the time, Exelon CEO Chris Crane said, “The capacity market alone can’t preserve zero-carbon emitting nuclear plants that are facing the lowest wholesale energy prices in 15 years.”
This year, PJM’s prices were even lower. Last week the regional transmission organization announced a 2020–2021 base residual auction price of $76.53/MW-day for most resources in its footprint. Both TMI and Quad Cities failed to clear the PJM auction.
“Today is a difficult day, not just for the 675 talented men and women who have dedicated themselves to operating Three Mile Island safely and reliably every day, but also for their families, the communities and customers who depend on this plant to produce clean energy and support local jobs,” Crane said in a press release.
Exelon said it is taking the first steps to shut down the plant. Items include sending PJM a deactivation notice and making permanent shutdown notifications to the Nuclear Regulatory Commission within 30 days, terminating capital investment projects needed for long-term operation of the plant, and canceling 2019 fuel purchases and outage planning.
One solution the company suggested was amending Pennsylvania’s Alternative Energy Portfolio Standard to include nuclear power. According to Exelon, nuclear power provides 93% of the state’s emissions-free electricity and avoids 37 million tons of carbon emissions, but its zero-emission attributes are not properly rewarded. Another option would be to establish a zero-emissions credit program, similar to the approach implemented in Illinois and New York.
“Like New York and Illinois before it, the Commonwealth has an opportunity to take a leadership role by implementing a policy solution to preserve its nuclear energy facilities and the clean, reliable energy and good-paying jobs they provide. We are committed to working with all stakeholders to secure Pennsylvania’s energy future, and will do all we can to support the community, the employees and their families during this difficult period,” Crane added.
The Illinois and New York subsidies are being contested, however. A group of generators filed suit in federal court last October to block the New York incentive program. The plaintiffs argue that the plan interferes with wholesale power prices in violation of the Federal Energy Regulatory Commission’s authority over interstate power sales.
In mid-February, the Electric Power Supply Association, Dynegy, Eastern Generation, NRG Energy, and Calpine Corp. filed a federal lawsuit against the State of Illinois, challenging its nuclear subsidies too. Monitoring Analytics—PJM’s independent market monitor—filed a motion with the U.S. District Court for the Northern District of Illinois about a month later to intervene as a plaintiff in the lawsuit as well.
If the subsidies were to be overturned in either case, it would be a huge loss for Exelon and could put at least a few nuclear plants back at risk for early retirement.

Junk Plant Hope Creek/Salem In Serous Decline and NRC Allegation  

It sounds like they think they don't have enough information to make a probe. I know Allegations has been asking questions to the inspectors. I ask the NRC to scrub the SRVs for information...

So I have raised the temperature? 
What next???

We know this facility is under grave financial pressure and blackmailing the community with trying to keep the plant operating. 

To Michael Mulligan

Wednesday, May 24, 2017

Junk Plant Cooper's Bum Meteorological Towers.

Remember Pilgrim's meteorological tower problems (google Popperville, pilgrim and meteorological tower). It stated out like this failing for days in a blizzard. It took a year before the NRC admitted both towers have been acting erratic for years and now both are in dire need of replacement.

The issues here is why the main and backup tower are not working at the same time. Basically not having any tower available occurred for only about a hour...  
Power ReactorEvent Number: 52768
Facility: COOPER
Region: 4 State: NE
Unit: [1] [ ] [ ]
RX Type: [1] GE-4
NRC Notified By: RANDY KOUBA
HQ OPS Officer: JEFF HERRERA
Notification Date: 05/23/2017
Notification Time: 15:57 [ET]
Event Date: 05/23/2017
Event Time: 08:30 [CDT]
Last Update Date: 05/23/2017
Emergency Class: NON EMERGENCY
10 CFR Section:
50.72(b)(3)(xiii) - LOSS COMM/ASMT/RESPONSE
Person (Organization):
JEREMY GROOM (R4DO)

UnitSCRAM CodeRX CRITInitial PWRInitial RX ModeCurrent PWRCurrent RX Mode
1NY100Power Operation100Power Operation
Event Text
LOSS OF METEOROLOGICAL TOWER PRIMARY AND BACKUP COMMUNICATION EQUIPMENT

"This notification is being made due to a loss of emergency assessment capability in accordance with 10 CFR50.72(b)(3)(xiii). On [May, 23, 2017] at 0830 (CDT), the meteorological tower primary and backup communication equipment failed, which resulted in a loss of meteorological data to the plant. Information technology and communications personnel investigated and restored the primary system to service. Meteorological data to the plant was restored at 0925 on [May 23, 2017].

"The NRC Senior Resident Inspector has been informed."

Our Electric system Is In A Full Scale Severe Economic Depression

‘Gas apocalypse’ looms amid power plant boom
The glut of cheap natural gas from a single, gigantic, shale basin that straddles the Northeast, mid-Atlantic and Midwest has sparked a massive construction boom of power plants. Dozens have been built in the past two years alone.
There’s just one problem: There isn’t nearly enough electricity demand to support all the new capacity. And as wholesale electricity prices plunge, industry experts are anticipating a fire sale of scores of plants in the region. Many, in fact, have already been sold along the PJM Interconnection LLC grid, the nation’s largest, encompassing 13 states from Virginia to Illinois.
“Everything in fossil fuels is for sale,” said Ted Brandt, chief executive officer at Marathon Capital LLC, a mergers-and-acquisitions adviser in Chicago. “People are bleeding.”
Drawing from abundant, cheap and nearby natural gas in the country’s most prolific shale field, the new plants are adding a gigantic amount of power generation — more than 20 gigawatts — to a region that arguably has more than it needs. The new gas-fired plants are also coming online at a time of market turmoil, buffeted by Obama administration efficiency policies that have helped tamp down demand and by the Trump administration’s determination to keep old coal-fired plants going.
Spot wholesale prices at PJM’s benchmark Western hub slumped to an average of $28.79 per megawatt-hour last year, falling by more than half since 2008 as the shale boom took hold. Many players are exiting the market.  Calpine Corp. — the highly leveraged Houston-based independent power producer with a more than $4 billion market value and 17 plants in the PJM grid — is exploring a sale of its facilities. The company has attracted interest from private-equity firms, Bloomberg reported this month. And FirstEnergy Corp. and American Electric Power Co. took more than a combined $11 billion in 2016 charges for plants. They’re exiting production to focus on buying and distributing electricity. Dynegy Inc. has also been reported as a takeover target.
“It’s a gas-driven apocalypse in the power market,” said Toby Shea, a New York-based analyst at Moody’s Investors Service.
As prices slip, some see a buying opportunity. Blackstone Group LP and ArcLight Capital Partners LLC bought four Midwest plants from American Electric for $2.17 billion in September. That implies an average sale price of $417 a kilowatt, a fraction of the $1,000 a kilowatt cost to build a new gas plant.
“It suddenly becomes a buyer’s market if the summer disappoints,” said Paul Pace, who heads KeyCorp’s energy lending team.
Contributing to the glut is the slowdown in coal-plant closures resulting from more favorable policies under the Trump administration. Some of the country’s smartest investors, including Blackstone, are buying these facilities at discounts, betting that a few hot or cold days each year will yield enough money to justify keeping them operating.
Patches of extreme weather are also a motive for the building boom. The polar vortex sidelined a fifth of PJM’s power plants in the game-changing winter of 2014, when frigid weather forced some plants to suspend production. This resulted in a huge, if temporary, spike in electricity rates for consumers. Preventing another such shutdown is a primary focus for PJM: Now, power plants must be both efficient and reliable in extreme weather or face steep penalties.
Finally, advances in efficiency, reducing demand for electricity, are converging with the gas glut to further depress the industry. Everything from the advent of LED light bulbs to Energy Star-certified refrigerators and appliances prompted PJM to slash its long-term growth forecasts to just 0.2 percent a year from 1 percent in 2014. Add in wind and solar, which are providing ever more energy to the grid, and the demand for new power plants looks even shakier.
Given lackluster demand for energy, it’s surprising that power-plant valuations haven’t fallen more, said Ravina Advani, a New York-based managing director at BNP Paribas SA. One reason: Developers continue to attract new investors, including from Japan and Korea. Still, it’s just a matter of time before prices break lower, said Dean Murphy, a Cambridge, Massachusetts-based principal at the Brattle Group.
“It’s like the housing market that is oversupplied and it takes longer to move your house,” he said. “Buyers have tons and tons of options.”

...The NEISO electric prices has been in steep decline for the last few years. It really has never translated into lower prices for the ratepayers. The PJM is a huge system. It is a bellwether indicator for electric prices in the nation.

In other words, the system is indicating wholesale electric prices will decline 25% in three years. How much will it decline this year, next year and year two?

This is very very bad news for the nukes and indicates safety is gravely compromised...

Another nuclear plant, Quad Cities in Illinois, also failed to clear PJM's capacity auction. In a written statement, Dominguez said Exelon "remains fully committed to keeping the Quad Cities plant open."

1
Updated on May 24, 2017 at 8:42 AM Posted on May 24, 2017 at 8:00 AM

PJM Interconnection's annual auction to determine which power plants will best be able to serve customers three years from the auction date shows that coal and nuclear plants continue to have problems competing against gas turbine plants but that the pace of new gas plants entering the market is slowing.(PJM)
0 shares
CLEVELAND, Ohio -- Add another monkey wrench to Ohio's debates about saving nuclear reactors and big coal-fired power plants from the growing fleet of gas turbine plants and wind farms.
PJM Interconnection's annual auction to guarantee there will be enough power plants in business three years from now to provide electricity to customers in Ohio, 12 other states and the District of Columbia has wrapped up with a healthy reserve committed to generate in June 2020.
The auction showed a reserve generating capacity margin of more than 23 percent higher than what PJM projects the demand will be from June 2020 through May 2021.
And perhaps the best news for consumers, the auction closing prices -- what PJM will pay power plants that commit to be operating in three years -- are lower than expected, about 25 percent lower over most of the PJM territory.
"The results show that PJM markets continue to achieve what they were originally intended to accomplish, ensuring reliability at the lowest reasonable cost," said Andrew L. Ott, PJM president and CEO, in a prepared release. 
There are exceptions in parts of the East Coast where demand is high and transmission capability constricted.
The one exception in Ohio is the Greater Cincinnati area served by Duke Energy, where power prices are expected to be significantly higher because there is a chance of plant closings and power imports, said Adam Keech, executive director of PJM market operations, in a news conference.
The auction capacity charges are not a complete guarantee of future prices, however, because they account for only about 10 percent of the final price of power. Fuel prices, competition and unexpected declines or increases in demand also play a role…

Tuesday, May 23, 2017

Columbia Nuclear Plant: Trump Just killed His First Nuclear Plant

Ok, I don't know what it is. Its a hybrid of municipal, state and federal ownership. Its way too top heavy and indicates they spend way too much on bureaucracy. Its a political jobs authority.
Energy Northwest (formerly Washington Public Power Supply System) is a United States public power joint operating agency formed by State law in 1957 to produce at-cost power for Northwest utilities. Headquartered in Richland, Washington, the WPPSS became commonly known as "Whoops"[1] due to over-commitment to nuclear power in the 1970s which brought about financial collapse and the second largest municipal bond default[2] in U.S. history. WPPSS was renamed Energy Northwest in November 1998. Agency membership includes 28 public power utilities, including 23 of the State’s 24 public utility districts.
Energy Northwest is governed by two boards: an executive board and a board of directors. The executive board has 11 members: five representatives from the board of directors, three gubernatorial appointees and three public representatives selected by the board of directors. The board of directors includes a representative from each member utility.
The consortium’s nuclear, hydro, wind, and solar projects deliver nearly 1,300 megawatts of electricity to the Northwest power grid. Current power projects include White Bluffs Solar Station, Packwood Lake Hydroelectric Project, Nine Canyon Wind Project, and Columbia Generating Station nuclear power plant.

Ok, ok...Columbia is owned by a private corporation... 

The dams subsidize this nuclear plant. It definitely won't be able to stand up on its own with the cheap hydro power. Who is going to buy the nuke plant? It basically is a extremely isolated nuke plant in the northwest. Then they had a whistleblower recently who was right. The plant is tainted over this to any new owner.

The very same logic would throw off TVA into the private market.
2016 presidential election results: Clinton, Trump and Gary whats-his-name.
1,742,718,  1,221, 747, 160,879
I bet you this is just Trump punishing Washington for not voting for him. The area surrounding TVA is deep in Trump area. Is there a little hypocrisy between selling off BVA versus TVA??? 

Hmmm, would this get liberal or antis votes next election if Trump canned the plant.     

Trump proposes sell-off of most Bonneville Power assets


Why Has Columbia been at 65% For A month And A Half


Originally published 5/2

It just doesn't make sense to "coast down" for this time frame. I doubt the below from the NRC is truthful.   
"REDUCED FOR ECONOMIC DISPATCH COASTDOWN TO REFUELING OUTAGE"
Update: I talked to the senior resident inspector about this. Man, the Washington state electric system is a beast. The grid is owned by all of us and the DOE (Bonneville Power). Columbia is owned by Northeast Power. Bet you this setup is a artifact of the cold war and nuclear weapons production. The vast proportion of the juice in Washington is produced by their dams. As this time, there is extreme winter melt off. The dams can go full power at this time. Dams electricity is very cheap and Washington electricity is also cheap. They found it very economical to ramp down power from the Columbia nuclear plant and supply all of electricity from the dams in heavy meltdown. I wonder how they compensate Columbia for all the capacity factor it lost? This kind of dispatch(for this long) is very infrequent.

Meet Our New NRC Commissioners

Deep state bureaucrats with no hands on nuclear experience. Southern ideological good old boys.  A continuation of the same.
President Trump announced three nominations Monday evening to keep the nation's nuclear energy watchdog from effectively shutting down on July 1.
Trump announced that he intends to nominate Annie Caputo, a senior Senate environment panel adviser and nuclear engineer, and David Wright, a former state utility regulator from South Carolina, to serve five-year terms on the five-member Nuclear Regulatory Commission. 

Sunday, May 21, 2017

What a South Korean Terrorism Plant Meltdown Would Look Like

It would drastically change the world if a North Korean Submarine launched missile hit a south Korean nuke plant, but did not lead to a meltdown.

It would be a grand North Korean last ditch suicide military strike.    

South Korean nuclear power plant accident would heavily taint western Japan: simulation

The Japan Times

Kyodo

A nuclear accident at a power plant in South Korea could cause wider radiation contamination in western Japan than on its home soil, a study by a South Korean scientist has shown.
If a cooling system fails at the spent-fuel storage pools at the Kori power plant’s No. 3 reactor in Busan, massive amounts of cesium-137 would be released that could potentially reach western Japan, according to a simulation by Jungmin Kang of the Natural Resources Defense Council, a U.S. think tank.
In the worst-case scenario, up to 67,000 sq. km of Japanese soil would be contaminated and 28.3 million people would be forced to evacuate, the study said, though the fallout’s spread would depend on the season.
As for South Korea, an accident at the plant could taint more than half of the nation by contaminating up to 54,000 sq. km, it said.
A total of 818 tons of spent nuclear fuel were stored in pools at the site as of the end of 2015, Kang said. He said an accident could be triggered not only by natural disasters but by terrorism or a missile from North Korea.

Friday, May 12, 2017

Junk Plant Browns Ferry: All Violations Related To Not Following Procedures


May 10, 2017
REPORT 05000259/2017001, 05000260/2017001, AND 05000296/2017001
Cornerstone: Barrier Integrity
• Green. An NRC identified non-cited violation (NCV) of 10 Code of Federal Regulations (CFR) 50, Appendix B, Criterion XVI, Corrective Action, was identified for the licensee’s inadequate corrective actions to preclude repetition (CAPR) of a significant condition adverse to quality (SCAQ). The licensee’s failure to take appropriate CAPRs for a SCAQ that resulted in an inoperable RCIC containment isolation check valve was a performance deficiency. The licensee entered the condition into their corrective action plan as condition report (CR) 1265552, performed repairs to the valve, and initiated a new root cause analysis. This performance deficiency was more than minor, because it was associated with\ the configuration control attribute of the Barrier Integrity cornerstone and adversely affected the cornerstone objective because the misalignment of the stem to disc for 2-CKV-71-14 resulted in a loss of reliability. The finding screened as Green because the RCIC subsystem remained operable. The finding was not assigned a cross-cutting aspect because the cause was not related to current licensee performance. (Section 1R15)


Cornerstone: Mitigating Systems


• Green. An NRC identified NCV of 10 CFR Part 50, Appendix B, Criterion VI, Document Control, was identified after maintenance on safety-related 4kv to 480 volt transformers TS1A and TS1B (Unit 1) resulted in the windings tap setting being misconfigured. The licensee’s failure to develop work instructions to change TS1A and TS1B transformer configuration was a performance deficiency. This performance deficiency was more than minor because it impacted the Mitigating Systems cornerstone attribute of configuration control in that the loads supplied by 480 volt shutdown boards 1A and 1B were challenged by this misconfiguration. The finding screened as Green because the electrical system remained operable. The licensee entered the condition into their corrective action plan as CR 1221265 and corrected the tap setting. The finding was not assigned a cross-cutting aspect because the cause was not related to current licensee performance. (Section 4OA3)


Cornerstone: Occupational Radiation Safety
• Green. A self-revealing NCV of Technical Specifications (TS) 5.7.1 was identified for a worker who entered a High Radiation Area (HRA) (Unit 1 reactor building steam tunnel) without proper authorization. This performance deficiency was determined to be greater than minor because it was associated with the Occupational Radiation Safety Cornerstone attribute of Human Performance and adversely affected the cornerstone objective of ensuring adequate protection of worker health and safety from exposure to radiation from radioactive material during routine civilian nuclear reactor operation. The inspectors determined the finding to be of very low safety significance (Green). The licensee entered the issue into their Corrective Action Program (CAP) as CR 1219539 and took immediate
corrective actions including restricting Radiologically Controlled Area (RCA) access for the individuals involved and performing confirmatory surveys of the area. This finding involved the cross-cutting aspect of Human Performance, Teamwork, [H.4], because a significant contributor to this event was poor communication between different work groups (workers entering the reactor building steam tunnel and RP personnel at the control point). [Section 2RS1]


• Green. An inspector-identified NCV of TS 5.4.1 was identified for the licensee’s failure to obtain an air sample while performing work in an area with smearable contamination levels greater than 50,000 disintegrations per minute (DPM) per 100cm2. This performance deficiency was determined to be greater than minor because it was associated with the Occupational Radiation Safety Cornerstone attribute of Human Performance and adversely affected the cornerstone objective of ensuring adequate protection of worker health and safety from exposure to radiation from radioactive material during routine civilian nuclear reactor operation. The inspectors determined the finding to be of very low safety significance (Green). The licensee entered the issue into their CAP (CR 1219539) and, since the work created airborne radioactivity in the area, performed in-vivo monitoring on the affected workers to assess doses from the intake of radioactive material. This finding involved the cross-cutting aspect of Human Performance, Avoid Complacency, [H.12], because, considering the contamination levels present, RP staff underestimated the risk for potential airborne radioactive material in the area. [Section 2RS1]

Watts Bar 1: Suspiciously Slow Startup

Come on, started up on the 9th, but still at 56% power...

Tuesday, May 09, 2017

Junk Plant Grand Gulf: Congratulation After More Than two Weeks, They Reached 100%

Update

This guys are going to have another deep down power event before another month is out based on their history.

***The overarching issue here is if you follow the rules and procedure to the letter of the law, the start-up will take four of five time longer than ignoring the rules and procedures. This is the root of all violation, incidents and accident all across the nation. You temporarily make more money by violating the rules and procedures.

I don’t buy it for a second that mass retirement diluted the skills of the employees. Many senior employees won’t transfer deep skills to their underlings because this dilutes their own value to upper management. I just think Entergy nuclear is a shitty company to work for, this the high turnover.

Again, a high population of employees nearing retirement based on first startup, it is what all plants have to go through. It is a common phenomena. All good management plans for this.

We are going to talking about the NRC’s victimology of bad actor plants. This is enabling bad behavior that never ends, with bad actor plants all across the USA.   

Monday, May 08, 2017

Junk Plant Cooper: Six "Slap On The Wrist" Violations Associated with Procedures

The magnitude of it is eye popping. It is a Entergy managed plant. The Risk Perspectives based violation is just not big enough to change behavior at Cooper or any other plant is the USA.

I mean, does the NRC broadly keep a tract of procedure related problems? If it continues to go up, it means the ROP is ineffective...
 May 1, 2017

(fixed bad link) 

Green. The inspectors reviewed a self-revealed, non-cited violation of Technical Specification 5.4.1.a, for the licensee’s failure to implement Maintenance Procedure 7.3.16, “Low Voltage Relay Removal and Installation,” Revision 22, for relay replacement work. Specifically, on October 28, 2016, the licensee failed to evaluate the potential impact of primary containment isolation system relay PCIS-REL-K27 work on shutdown cooling relay PCIS-REL-K30, which was mounted next to K27 and shared a common mounting rail. As a result, the licensee did not identify the potential of losing residual heat removal shutdown cooling, and while installing the K27 relay and snapping it into the mounting rail, workers caused a momentary actuation of relay K30 and a loss of residual heat removal shutdown cooling. Corrective actions to restore compliance included restoration of shutdown cooling, completion of the K27 relay maintenance with shutdown cooling out of service, and an outage risk management procedure change that prohibited work on or near shutdown cooling relays while the system was required to be in service. The licensee entered this deficiency into the corrective action program as Condition Report CR-CNS-2016-07645.
The licensee’s failure to implement Maintenance Procedure 7.3.16, in violation of Technical Specification 5.4.1.a, was a performance deficiency. The performance deficiency was more than minor, and therefore a finding, because it was associated with the equipment performance attribute of the Initiating Events Cornerstone and affected the associated cornerstone objective to limit the likelihood of those events that upset plant stability and challenge critical safety functions during shutdown operations.

Green. The inspectors identified a non-cited violation of Technical Specification 5.4.1.a for the licensee’s failure to maintain Emergency Procedure 5.1ASD, “Alternate Shutdown,” Revision 17, for establishing reactor equipment cooling system flow to the high pressure coolant injection system fan coil unit. Specifically, the licensee failed to maintain Emergency Procedure 5.1ASD with adequate instructions to place the reactor equipment cooling system north or south critical loop in service and verify reactor equipment system flow to the high pressure cooling injection system fan coil unit during some control room evacuation scenarios. The immediate corrective actions were to assess operability of the high pressure coolant injection system during control room evacuations that are not related to fire scenarios, and to revise Emergency Procedure 5.1ASD with instructions to open the critical loop supply valves (REC-MOV-711 or REC-MOV-714) in the control room or locally, and verify reactor equipment system flow to the high pressure coolant injection fan coil unit. The licensee entered this deficiency into the corrective action program as Condition Report CR-CNS-2017-01403.

Green. The inspectors identified a non-cited violation of 10 CFR Part 50, Appendix B, Criterion V, “Instructions, Procedures, and Drawings,” associated with the licensee’s failure to identify a condition adverse to quality associated with Station Procedure 2.2.24.1, “250 Vdc Electrical System (Div 1),” Revision 14, in accordance with Station Procedure 0-CNS-LI-102, “Corrective Action Process,” Revision 6. Specifically, the licensee failed to identify that Station Procedure 2.2.24.1 contained inadequate instructions to ensure the oncoming charger 1C output voltage was matched with the bus 1A voltage when transferring bus 1A from charger 1A to charger 1C, so that technical specification bus voltage requirements would remain met. This resulted in an unexpected and initially unrecognized decline in voltage on the bus to below the required minimum of 260.4 Vdc.

Green. The inspectors identified a non-cited violation of 10 CFR Part 50, Appendix B, Criterion V, “Instructions, Procedures, and Drawings,” associated with the licensee’s failure to identify a condition adverse to quality for Division 1 residual heat removal service water booster pump A, in accordance with Station Procedure 0-CNS-LI-102, “Corrective Action Process,” Revision 6. Specifically, on January 5, 2017, the inspectors identified an oil level lower than normally expected, oil on the pump skid, and an oil droplet formed on the Division 1 residual heat removal service water booster pump A inboard bearing sight glass. The inspectors informed the control room of this condition, and the licensee determined the oil leakage from the pump’s sight glass would have prevented the pump from operating for the required 30 days during a design basis accident. The immediate corrective action was to repair the Division 1 residual heat removal service water booster pump A inboard bearing sight glass, restoring operability of the pump. The licensee entered this deficiency into the corrective action program as Condition Report CR-CNS-2017-00054.
The licensee’s failure to identify a condition adverse to quality for Division 1 residual heat removal service water booster pump A, in violation of Station Procedure 0-CNS-LI-102, was a performance deficiency.


Green. The inspectors identified a non-cited violation of 10 CFR 50.55a(g)(4) for the licensee’s failure to use an approved method to disposition an American Society of Mechanical Engineers Code nonconforming condition in the residual heat removal service water system. Specifically, the licensee identified multiple locations with localized pipe thinning below the American Society of Mechanical Engineers Code B31.1 design minimum pipe-wall thickness during an ultrasonic examination but failed to use an approved method to calculate a new acceptable pipe-wall thickness. As a corrective action to restore compliance, the licensee replaced this section of piping on November 1, 2016, during Refueling Outage 29. The licensee entered this issue into the corrective action program as Condition Reports CR-CNS-2016-05558 and CR-CNS-2016-05963.


Green. The inspectors reviewed a self-revealed, non-cited violation of Technical Specification 3.0.4 for the licensee’s failure to install the correct reactor core isolation cooling pressure control valve, RCIC-AOV-PCV23, mechanical stop and verify proper operation of the system prior to entering a mode of applicability for Technical Specification 3.5.3. This condition resulted in RCIC-AOV-PCV23 going fully open during surveillance testing following Refueling Outage 29, causing a pressure transient. This transient caused a failure of the reactor core isolation cooling turbine lube oil cooler gasket, lifting of a pressure relief valve, and a water leak. The licensee immediately shut down the reactor core isolation cooling system and declared it inoperable. The immediate corrective actions were to restore RCIC-AOV-PCV23 from the closed mechanical stop to the required open mechanical stop and to replace the turbine lube oil cooler gasket to restore operability of the system. The licensee entered this deficiency into the corrective action program as Condition Report CR-CNS-2016-08122 and initiated a root cause evaluation to investigate this condition.

Junk Facility Browns Ferry: TVA Doesn't Use Procedures

There are two procedures problems here, one address and one not.

The techs should have had a procedure for this. They setting up lower level employees to failure without having procedures. The "corrective action" procedure wasn't followed in that no procedures set this event up?   

On October 8, 2016, during the performance of preventive maintenance of the transformer winding turns ratio test on the 480V Shutdown Board transformer TS1 B, it was discovered that the transformer was set on the incorrect tap. This would result in lower than minimum required voltages at the electrically downstream buses and equipment during a postulated loss of coolant accident coincident with degraded voltage conditions. Transformers TS1A and TS1 Band their associated 480V shutdown boards were determined to be inoperable since installation prior to Unit 1 restart from an extended outage in 2007. This event is being reported as a condition which was prohibited by the plant's Technical Specifications, a condition that could have prevented the fulfillment of the safety function of structures or systems that
are needed to shut down the reactor and maintain it in a safe shutdown condition, remove residual heat, or mitigate the consequences of an accident, and a condition that resulted in the nuclear plant being in an unanalyzed condition that significantly degrades plant safety.
The cause of this event was the technicians did not use the correct drawings to install the transformers because they were incorrectly classified and listed as "documentation only" drawings. There were no steps in the work order to correctly set the taps. Corrective actions were to re-set the taps for the transformers in accordance with the applicable drawing, validate other similar transformer settings, and revise the classification for the applicable drawing.

 Junk Plant RIver Bend: Following Grand Gulf Into The "Not Following" Procedure Abyss

Basically three "slap on the wrist" procedure violations at River Bend this inspection cycle. How prevalent is bum procedures in River Bend??? It just might be River Bend is maliciously not following procedures to inflate profits or minimize losses?
May 1, 2017


Green. The inspectors identified a non-cited violation of Technical Specification 5.4, “Procedures,” for the licensee’s failure to follow station maintenance procedures related to the control of scaffolding in the reactor building. Specifically, the licensee installed scaffolding less than two inches from safety-related containment unit cooler HVR-UC1B without completing an engineering evaluation. The licensee entered this issue into their corrective action program as Condition Report CR-RBS-2016-07963. Corrective actions included removing the scaffolding.

Green. The inspectors identified a non-cited violation of Technical Specification 5.4, “Procedures,” for the licensee’s failure to properly pre-plan and perform maintenance on safety-related components in accordance with documented instructions appropriate to the circumstances. Specifically, the licensee used work order instructions that did not contain sufficient detail for the reassembly of SWP-PVY32C, a safety-related valve in the control building ventilation system. As a result, SWP-PVY32C developed a refrigerant leak, and on November 17, 2015, the valve failed. This in turn caused the control building ventilation system to fail, and the high pressure core spray system was consequently declared inoperable. The licensee entered this condition into their corrective action program as Condition Report CR-RBS-2017-02364. Corrective actions included incorporating the torque values into the model work order instructions for future maintenance and reassembly.


Green. The inspectors identified a non-cited violation of Technical Specifications 3.8.4, “DC Sources - Operating,” 3.8.7, “Inverters – Operating,” and 3.8.9, “Distribution Systems – Operating,” for the licensee’s failure to either restore inoperable electrical power subsystems, inverters, and distribution subsystems to operable status within the applicable completion times, or be in Mode 3 in 12 hours and Mode 4 in 36 hours. Specifically, electrical power systems required by the above limiting conditions for operation were inoperable due to the associated division of the control building chilled water system chillers being out of service and therefore unavailable to provide the technical specification support function of attendant cooling that is needed for the associated electrical systems to perform their specified safety functions. As a result of this deficiency, the station reduced the reliability and availability of systems cooled by control building chilled water system chillers by allowing configurations that did not conform to the single failure criterion. The licensee entered this issue into their corrective action program as Condition Report CR-RBS-2015-02525. Corrective actions included entering the appropriate limiting conditions for operation of affected safety-related systems when the non-safety related support system were non-functional.



Junk Plant Grand Gulf: One Of The Most Dangerous Plants In USA.

I thought over the weekend these guys would be at 100% after the weekend. I think these guys got the world record on a slow start-up from a outage to 100% power. They were some 96% power thurs and fri, now they backed down to 85% power. What a cascade of problems these guys have had in the last year.

Basically, inadequate maintenance, extremely poor training of licensed control employees and unclear start-up procedures. I think the whole Entergy fleet has problems with procedures. They should have never allowed these guys to start-up from a four month safety shutdown until all procedures were scrubbed and they get guys in the control room who got the balls to keep their procedures clean of problems, clarity and are comprehensively trained on their procedures...

Fundimentally behind this all is a staff who is under severe management intimidation from a republican domination (management ) and submission (employees) system.